X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-119-23950

Well Details

Well ID: 34-119-23950
Loading map...
Country: United States
State: Ohio
County: Muskingum
Municipality: Hopewell Township
Operator Name: MELLON RICHARD L
Well Pad ID:
Farm/Lease Name: OSBURN ETHEL C
License Status: Final Restoration
License Date: 2014-03-07
Spud Date: 1977-12-12
Spud Drilling Contractor: LOTHES & LOTHES
Final Drill Date: 1978-01-20
Well Total Depth: 3248.00 ft
Configuration: Vertical
Latitude: 39.920000
Longitude: -82.200000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1977-12-12 R.I. 12-7-77, SECT-7(S)
Completed 1978-01-20 R.I. 12-7-77, SECT-7(S)
Reached Total Depth 1978-01-20 R.I. 12-7-77, SECT-7(S)
Completion Report Received 1978-08-10 R.I. 12-7-77, SECT-7(S)
Change of Owner 2014-02-13 Operator changed from 9998, HISTORIC OWNER to 9236, MELLON RICHARD L. WELL TRANSFERRED PER OWNERSHIP AFFIDAVIT. SEE OWNER FILE FOR DOCUMENTATION.
APP 2014-03-07 Proposed Formations:CLINTON, Issued Date:3/7/2014, Expired Date:3/6/2016 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2014-09-12 R.I. 12-7-77, SECT-7(S)
Construction Permit Expires 2016-03-06 R.I. 12-7-77, SECT-7(S)
Record Last Modified 2017-02-15 R.I. 12-7-77, SECT-7(S)

For data sources see[2]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 SHAMROCK EQUIPMENT CO 181.00 0.00 0
1986 SHAMROCK EQUIPMENT CO 0.00 83.00 360

For data sources see[3] [4]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 SHAMROCK EQUIPMENT CO Brine 87 0
1986 SHAMROCK EQUIPMENT CO Brine 90 360

For data sources see[5] [6]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1154172517 2014-9-12 0:00: AM No Violations
-116402971 2014-11-21 0:00 PB No Violations
-2098893042 2015-1-21 0:00: FR No Violations 1.50
-2125583806 2014-9-10 0:00: PB No Violations 11.00
-423239104 2014-9-13 0:00: PB No Violations
0116402971 2014-11-21 Plug / Plug Back No Violations I will stop back later to perform a Final Restoration on well. Site has been graded back. It is at the edge of a corn field.
0134143679 2013-09-18 Administrative Inspection No Violations Research indicated that this case does not meet Orphan Well Program requirements and will be referred back to Pat Shreve for further action.
0317722913 2013-02-27 Production Wells No Violations I met with Mike Corp on well. Northwood did not know they had well. Northwood will apply for plugging permit.
0423239104 2014-09-13 Plug / Plug Back No Violations Well has been plugged according to 1501:9-11. This resolves the Compliance Notice # 1595625479.
0615371123 2013-10-24 Production Wells No Violations I stopped by to visit with the Mellons on getting bonded and registered with well. I will give extension if needed.
1154172517 2014-09-12 Administrative Inspection No Violations Don Strange with Berrys well service called and stated that they tagged the top of the cement with tubing and then placed a cement plug from 603-403. Then pulled up to 200-0. Set a cement plug and the plug did not drop back.
134143679 2013-9-18 0:00: AM No Violations
1357578698 2013-01-07 Production Wells No Violations Well is equipped with 3casing,4x3 reducer,4.5casing nipple,4x2reducer,drip tank and valves are shut in. Well is an HAD well and is not hooked up. There is an old dog house to a rig left on location. I will contact well owner.
1379507830 2013-09-17 Production Wells No Violations An inspection conducted with Pat Shreve revealed an idle gas well that was listed as Historic Owner in RBDMS. The well consisted of an 8.63 wellhead partially buried below ground level with a welded plate on top. A section of 3.5 casing extended from the top of wellhead into a 4.5 collar and reduced with a 4-2 swage routed into 2 gas piping and valve. A 1.25 plastic gas line was routed from top of well and disappeared below ground and located next to a drip. The gas line from the drip was routed towards the direction of an area with several sections of gas line. All valves were closed and the well did not contain pressure. An approx 2 plastic line with fitting on end was also situated next to the well and disconnected. The well location contained oilfield debris that consisted of steel and plastic lines, steel cable and a old dog house. Research will be conducted to determine well ownership.
1379963027 2013-09-17 Production Wells Violations Noted Well is not producing. There are 8.625casing and 3.5casing in well. There is no capability to the well at all. Richard and Elizabeth Melon are the owners from the courthouse research. Well needs a temporary Bond. The well needs to produce or be plugged. The identification is incomplete. Well is located at head waters to an intermittent run.
1385395254 2013-11-20 Administrative Inspection No Violations Courthouse research was performed on well at Muskingum County Courthouse on well for the title search from Shamrock to Ethel Osburn .
1595625479 2013-11-15 Production Wells No Violations I stopped by Richard Mellons property and was helping him out with his paperwork on his well for bonding and registering. I agreed to give an extension on the Compliance Notice due to the location of where the well is located. Richard was going to swab well and test for gas volume and capability .
2098893042 2015-01-21 Final Restoration No Violations Final Restoration passed on 1-21-15 by Patrick Shreve. Vegetation has been established to prevent substantial erosion. All Compliance Notices with the numbers 615371123,1379963027 has been resolved.
2125583806 2014-09-10 Plug / Plug Back No Violations 9-10-14 Berrys well service had rig over the well and set bottom hole plug at 3115-2665 over the Clinton. Formation Cementing placed the cement plug of 20 sacks of cement thru 1.5tubing in the 3.5casing. Appalachain wireline shot off casing at 2296. The lime plug was set at 2296-2096. Formation Cementing set plug of 24 sacks. Rig pulled 3.5tubing up to Berea and set plug at 980-780. They ran 60 sacks of regular cement. At 680-530 Formation Cementing set 45 sack plug at the bottom of the 8.625casing. The rig pulled all the 3.5 casing out. They shut down and will finish on 9-12-14. 11hrs.
317722913 2013-2-27 0:00: PW No Violations 1.00
615371123 2013-10-24 0:00 PW No Violations 1.50

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1379963027 US-OH-111283 2015-03-13 Well shall be plugged
1379963027 US-OH-111284 2015-03-13 Failure to register/obtain or maintain bond/insurance

For data sources see[7]

References