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Well ID: 34-119-24893 | Loading map...
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Country: United States | |
State: Ohio | |
County: Muskingum | |
Municipality: Rich Hill Township | |
Operator Name: JHC II LLC | |
Well Pad ID: | |
Farm/Lease Name: FOUNDS | |
License Status: Final Restoration | |
License Date: 2012-07-13 | |
Spud Date: 1979-09-03 | |
Spud Drilling Contractor: | |
Final Drill Date: 1979-09-06 | |
Well Total Depth: 1513.00 ft | |
Configuration: Vertical | |
Latitude: 39.860000 | |
Longitude: -81.760000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1979-09-03 | |
CO | 1979-09-04 | 412 GEM ENERGY CORP GeoDate 9/4/79 |
Completed | 1979-09-06 | |
Reached Total Depth | 1979-09-06 | |
Change of Owner | 2006-04-11 | Operator changed from 412, GEM ENERGY CORP to 1, HOPEWELL OIL & GAS |
APP | 2007-06-04 | Proposed Formations:BEREA, Issued Date:6/4/2007, Expired Date:6/3/2008 6:00:00 AM, Drilling unit acres:187, Proposed Well Type:OG, Proposed Well Class: |
Change of Owner | 2008-10-15 | Operator changed from 1, HOPEWELL OIL & GAS DEVELOPMENT to 6224, JHC II LLC |
APP | 2012-07-13 | Proposed Formations:BEREA, Issued Date:7/13/2012, Expired Date:7/13/2014 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2012-08-22 | |
Record Last Modified | 2013-05-22 | |
Construction Permit Expires | 2014-07-13 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 1350 | 1408 | 12 |
1350 | 1408 | 12 | |
1350 | 1408 | 12 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
0 | 0 | 30000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2006 | HOPEWELL OIL & GAS DEVELOPMENT | 0.00 | 0.00 | 365 |
2007 | HOPEWELL OIL & GAS DEVELOPMENT | 0.00 | 0.00 | 0 |
2008 | JHC II LLC | 0.00 | 0.00 | 365 |
2009 | JHC II LLC | 2.00 | 0.00 | 365 |
2010 | JHC II LLC | 0.00 | 0.00 | 365 |
2011 | JHC II LLC | 0.00 | 0.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2006 | HOPEWELL OIL & GAS DEVELOPMENT | Brine | 0 | 365 |
2007 | HOPEWELL OIL & GAS DEVELOPMENT | Brine | ||
2008 | HOPEWELL OIL & GAS DEVELOPMENT | Brine | 0 | 365 |
2009 | JHC II LLC | Brine | 85 | 365 |
2010 | JHC II LLC | Brine | 0 | 365 |
2011 | JHC II LLC | Brine | 19 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0828715765 | 2007-05-08 | Production Wells | Violations Noted | well is not producing. Pump Jack. Produce or plug. Failure to comply with this order may result in forfeiture of bond. |
1076433276 | 2004-02-10 | Production Wells | No Violations | |
1270375708 | 2009-10-01 | Production Wells | No Violations | NOV cancelled well changed owners. |
1345648883 | 2012-08-22 | Plug / Plug Back | No Violations | Knox energy rig is plugging well for JHC. Cemenco is spotting bottom plug thru 4.5casing in a bull plug method and ran 25 sacks of cement. The rig could not get telegraph with the ripping tools until 300 which is inside the 7surface at bottom. Set large 300 plug back to surface. Good circulation was established. |
1367927867 | 2013-04-30 | Final Restoration | No Violations | Final Restoration passed on 4-30-13 by Patrick Shreve. |
828715765 | 2007-5-8 0:00:0 | PW | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0828715765 | US-OH-129445 | 2007-05-08 | Well shall be plugged |
For data sources see[9]