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34-119-27899

Well Details

Well ID: 34-119-27899
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Country: United States
State: Ohio
County: Muskingum
Municipality: Jackson Township
Operator Name: MORAN RONALD F
Well Pad ID:
Farm/Lease Name: COPELAND CONSTANCE L
License Status: Final Restoration
License Date: 2014-05-01
Spud Date: 1994-09-16
Spud Drilling Contractor: LBJ DRILLING
Final Drill Date: 1994-10-24
Well Total Depth: 5390.00 ft
Configuration: Vertical
Latitude: 40.160000
Longitude: -82.110000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1994-07-22 Issued Date 7/22/94 Expired Date 7/22/95 Acres 0099000 Tool Type RTAF Proposed Formation ROSE RUN Proposed Depth 05390 Proposed Drill Depth 05390
Original Spud 1994-09-14
Completed 1994-10-24
Reached Total Depth 1994-10-24
CO 1994-11-25 565 MORAN RONALD F GeoDate 7/22/94
Completion Report Received 1995-01-27
APP 2014-05-01 Proposed Formations:CLINTON, Issued Date:5/1/2014, Expired Date:4/30/2016 12:00:00 PM, Drilling unit acres:99, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2014-06-13
Construction Permit Expires 2016-04-30
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 5329 5390 0
5329 5390 0
5329 5390 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
0 0 0 NONE

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1995 MORAN RONALD F 0.00 823.00 0
1997 HOPEWELL OIL & GAS DEVELOPMENT 0.00 230.00 180
1998 HOPEWELL OIL & GAS DEVELOPMENT 0.00 226.00 180
1999 MORAN RONALD F 0.00 338.00 365
2000 MORAN RONALD F 0.00 0.00 365
2001 MORAN RONALD F 0.00 153.00 365
2002 MORAN RONALD F 0.00 356.00 365
2003 MORAN RONALD F 0.00 266.00 365
2004 MORAN RONALD F 0.00 228.00 365
2005 MORAN RONALD F 0.00 187.00 365
2012 MORAN RONALD F 0.00 0.00 366
2013 MORAN RONALD F 0.00 0.00 365
2014 MORAN RONALD F 0.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1995 MORAN RONALD F Brine 0 0
1997 HOPEWELL OIL & GAS DEVELOPMENT Brine 0 180
1998 HOPEWELL OIL & GAS DEVELOPMENT Brine 180
1999 MORAN RONALD F Brine 80 365
2000 MORAN RONALD F Brine 0 365
2001 MORAN RONALD F Brine 0 365
2002 MORAN RONALD F Brine 90 365
2003 MORAN RONALD F Brine 90 365
2004 MORAN RONALD F Brine 40 365
2005 MORAN RONALD F Brine 45 365
2012 MORAN RONALD F Brine 0 366
2013 MORAN RONALD F Brine 0 365
2014 MORAN RONALD F Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1229821557 2014-6-12 0:00: PB No Violations 1.50
0583597858 2014-03-25 Production Wells Violations Noted Well is idle well with large pumping unit, 5.5x 2.375upset wellhead complete with rods. All production valves are closed. There are 2-100 barrel tanks with no dike or identification. There has been no production records filed since 2005. Failure to plug within 180 days may result in further enforcement action.
1229821557 2014-06-12 Plug / Plug Back No Violations Rig was checking to see if well had hole in 4.5casing. They were bleeding off the annulus. This notates that there is no hole in the 4.5casing. The rig also was filling up the 4.5casing with brine water checking the level.
1402425592 2014-06-10 Plug / Plug Back No Violations Gene Matheny well service is plugging well for Moran. Cemenco is placing plug thru 2.375upset tubing . The cemenco company pumped brine ahead and could not pump because of parafin build up on inside of tubing. Pump truck pumped on tubing several times taking pressure up to 1300 psi. Rig is pulling out tubing to clean and rerun for bottom plug.
1408200560 2014-06-13 Plug / Plug Back No Violations Rig ripped off at 3780. They pulled two joints at 42.4 each putting bottom of pipe at 3695. Set rip plug at 3695-3495. Clinton plug was set at 3377-3185. Big Lime plug was set at 2200-2000. Set plug at Bottom of surface to 1082-882. Surface plug was set at 300-0. The well never circulated but fluid stayed at 300. Set bridge plug and set top plug of 300.
1461257039 2014-10-27 Plug / Plug Back No Violations Well has been plugged back to surface by my inspections. This resolves the Compliance Notice # 583597858.
583597858 2014-3-25 0:00: PW No Violations 2.00
iANGE00040 1997-07-31 Final Restoration No Violations
iANGE000401 1997-7-31 0:00: FR No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0583597858 US-OH-126552 2014-11-19 Failure to legibly identify well
0583597858 US-OH-126553 2014-11-19 No SPCC dike/or failure to keep dike free of water or oil
0583597858 US-OH-126554 2014-11-19 Well shall be plugged
0583597858 US-OH-126555 2014-11-19 Statement of annual production not filed

For data sources see[9]

References