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34-119-28696

Well Details

Well ID: 34-119-28696
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Country: United States
State: Ohio
County: Muskingum
Municipality: Rich Hill Township
Operator Name: ARTEX OIL COMPANY
Well Pad ID:
Farm/Lease Name: MENZIE-FRICK UNIT
License Status: Final Restoration
License Date: 2010-01-25
Spud Date: 2010-03-14
Spud Drilling Contractor: WARREN DRLG
Final Drill Date: 2010-03-27
Well Total Depth: 7036.00 ft
Configuration: Vertical
Latitude: 39.910000
Longitude: -81.760000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2010-01-25 Proposed Formations:OHIO SHALE THRU KNOX, Issued Date:1/25/2010, Expired Date:1/25/2011 6:00:00 AM, Drilling unit acres:88, Proposed Well Type:OG, Proposed Well Class:EDPW
Plugged/Abandoned 2010-03-26
Reached Total Depth 2010-03-27
Completion Report Received 2010-05-10
Construction Permit Expires 2011-01-25
Record Last Modified 2013-03-14

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
0 0 0 NO PRODUCTION CASING WAS RUN …

For data sources see[3]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1559337349 2010-3-18 0:00: DD No Violations
-1625495916 2010-8-24 0:00: FR No Violations
-1812695390 2010-3-17 0:00: DD No Violations
1559337349 2010-03-18 Drill / Deepen / Reopen No Violations Ran 37 joints of 8-/8 casing and Schlumberger cemented with 260 sx of lite cement w/ 2% gel and 2% CaCl2. And 150 sx 0f Regular Class A w/ 3% CaCl2. Good cement returned to surface, did not drop back.
1625495916 2010-08-24 Final Restoration No Violations FR passed
1812695390 2010-03-17 Drill / Deepen / Reopen No Violations During suface job, 8-5/8 casing parted 3 joints down. Fished and TIH with bit and conditioned hole

For data sources see[4]

References