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34-119-28774

Well Details

Well ID: 34-119-28774
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Country: United States
State: Ohio
County: Muskingum
Municipality: Licking Township
Operator Name: DERRICK PETROLEUM INC
Well Pad ID:
Farm/Lease Name: HILLBILLY
License Status: Producing
License Date: 2012-10-31
Spud Date: 2013-07-24
Spud Drilling Contractor: KILBARGER DRLG
Final Drill Date: 2013-07-30
Well Total Depth: 3018.00 ft
Configuration: Vertical
Latitude: 40.090000
Longitude: -82.180000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2012-10-31 Proposed Formations:CLINTON, Issued Date:10/31/2012, Expired Date:10/31/2014 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:POOL
Reached Total Depth 2013-07-30
Completion Report Received 2014-07-01
Construction Permit Expires 2014-10-31
Record Last Modified 2017-02-15

For data sources see[2]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2014 DERRICK PETROLEUM INC 0.00 1295.00 189
2015 DERRICK PETROLEUM INC 0.00 725.00 189
2016 DERRICK PETROLEUM INC 0.00 749.00 365
2017 DERRICK PETROLEUM INC 0.00 670.00 365
2018 DERRICK PETROLEUM INC 0.00 584.00 365

For data sources see[3] [4]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2014 DERRICK PETROLEUM INC Brine 181 189
2015 DERRICK PETROLEUM INC Brine 289 189
2016 DERRICK PETROLEUM INC Brine 110 365
2017 DERRICK PETROLEUM INC Brine 88 365
2018 DERRICK PETROLEUM INC Brine 108 365

For data sources see[5] [6]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1579411392 2014-10-15 0:00 PL No Violations 1.00
-1937288801 2016-11-7 0:00: PW No Violations 0.50
1374838509 2013-07-25 Casing String Witnessed No Violations Killbarger rig 4 is drilling and setting surface pipe. There is 433of 12.25open hole and 398of 8.62524lb/ft. There were 2 centrilizers ran on bottom and in the middle. The mud was at a 50 viscosity and had good circulation. There were no cement returns at all. The fluid did not fall back. Will pressure test in 8 hours.
1375244522 2013-07-26 Casing String Witnessed No Violations On day of pressure testing the surface pipe the pressure would not hold. The required bond log was going to be ran because of cement slurry not being circulated back to surface. The bond log revealed that the cement top was down 38. And the pressure leak was at the landing joint and the joint below that. The company would top off with Quick crete.
1579411392 2014-10-15 Preliminary Restoration No Violations Preliminary Restoration passed by Patrick Shreve on 10-15-14.
1937288801 2016-11-07 Production Wells No Violations

-100 barrel steel tank batteries that is enclosed within an impoundment.

For data sources see[7]

References