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Well ID: 34-121-21818 | Loading map...
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Country: United States | |
State: Ohio | |
County: Noble | |
Municipality: Olive Township | |
Operator Name: ENERVEST OPERATING LLC | |
Well Pad ID: | |
Farm/Lease Name: MORRIS R | |
License Status: Final Restoration | |
License Date: 2015-02-05 | |
Spud Date: 1976-06-08 | |
Spud Drilling Contractor: | |
Final Drill Date: 1976-06-14 | |
Well Total Depth: 5951.00 ft | |
Configuration: Vertical | |
Latitude: 39.710000 | |
Longitude: -81.500000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1975-12-26 | 2143 CARLESS RESOURCES INC GeoDate 12/26/75 |
Original Spud | 1976-06-08 | |
Completed | 1976-06-14 | |
Reached Total Depth | 1976-06-14 | |
Change of Owner | 1998-07-06 | Operator changed from 2143, CARLESS RESOURCES INC to 1388, NORTH COAST ENERGY INC |
Change of Owner | 2009-12-14 | Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC |
APP | 2015-02-05 | Proposed Formations:CLINTON, Issued Date:2/5/2015, Expired Date:2/4/2017 12:00:00 PM, Drilling unit acres:44, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2015-06-15 | |
Construction Permit Expires | 2017-02-04 | |
Record Last Modified | 2017-02-10 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 5738 | 5782 | 13 |
5738 | 5782 | 13 | |
5738 | 5782 | 13 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1410 Bbl | 50000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1986 | ZILKHA ENERGY INC | 2073.00 | 111.00 | 292 |
1987 | ZILKHA ENERGY INC | 1455.00 | 36.00 | 181 |
1988 | CARLESS RESOURCES INC | 1475.00 | 92.00 | 330 |
1989 | CARLESS RESOURCES INC | 1382.00 | 0.00 | 355 |
1990 | CARLESS RESOURCES INC | 2482.00 | 73.00 | 365 |
1991 | CARLESS RESOURCES INC | 2191.00 | 173.00 | 365 |
1992 | CARLESS RESOURCES INC | 2287.00 | 95.00 | 365 |
1993 | CARLESS RESOURCES INC | 1885.00 | 99.00 | 365 |
1994 | CARLESS RESOURCES INC | 1641.00 | 0.00 | 365 |
1995 | CARLESS RESOURCES INC | 1678.00 | 155.00 | 365 |
1996 | CARLESS RESOURCES INC | 1720.00 | 0.00 | 365 |
1997 | CARLESS RESOURCES INC | 1816.00 | 101.00 | 365 |
1998 | EXCO - NORTH COAST ENERGY INC | 1800.00 | 0.00 | 365 |
1999 | EXCO - NORTH COAST ENERGY INC | 2243.00 | 52.00 | 365 |
2000 | EXCO - NORTH COAST ENERGY INC | 1031.00 | 0.00 | 365 |
2001 | EXCO - NORTH COAST ENERGY INC | 853.00 | 0.00 | 365 |
2002 | EXCO - NORTH COAST ENERGY INC | 669.00 | 0.00 | 365 |
2003 | EXCO - NORTH COAST ENERGY INC | 570.00 | 0.00 | 365 |
2004 | EXCO - NORTH COAST ENERGY INC | 804.00 | 0.00 | 365 |
2005 | EXCO - NORTH COAST ENERGY INC | 673.00 | 78.00 | 365 |
2006 | EXCO - NORTH COAST ENERGY INC | 820.00 | 0.00 | 365 |
2007 | EXCO - NORTH COAST ENERGY INC | 666.00 | 56.00 | 365 |
2008 | EXCO - NORTH COAST ENERGY INC | 472.00 | 54.00 | 366 |
2009 | EXCO - NORTH COAST ENERGY INC | 448.00 | 0.00 | 365 |
2010 | ENERVEST OPERATING LLC | 810.00 | 114.00 | 365 |
2011 | ENERVEST OPERATING LLC | 661.00 | 0.00 | 0 |
2012 | ENERVEST OPERATING LLC | 685.00 | 0.00 | 366 |
2013 | ENERVEST OPERATING LLC | 471.00 | 0.00 | 365 |
2014 | ENERVEST OPERATING LLC | 529.00 | 6.00 | 365 |
2015 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 303 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1422786378 | 2012-4-18 0:00: | PW | No Violations | |
-1514027759 | 2015-9-1 0:00:0 | FR | No Violations | 1.00 |
-1516789880 | 2014-12-29 0:00 | PW | No Violations | 2.00 |
1258663680 | 2009-11-17 | Production Wells | No Violations | Inspection revealed that well is equipped with pumping unit and tubing and rods and 1-210 bbl tank located in dike area. |
1422786378 | 2012-04-18 | Production Wells | No Violations | Inspection of well found the following equipment -8.625 surface casing -4.5 production casing -2.375 tubing with the production valves open and the well being produced by means of a pumping unit , 210 tank and separator located in a shared dike with other wells in area ,identification present on well and tank . |
1434478631 | 2015-06-15 | Plug / Plug Back | No Violations | My inspection today finds Berry Well Service pulled the casing up to 1760 where Petroset spotted a 50 sack class A 2% gel plug. The casing was then pulled up to 200 and Petroset pumped a 60 sack plug to surface. The cement was topped off and the cement stayed at surface. |
1510864169 | 2015-06-22 | Plug / Plug Back | No Violations | The well has been plugged resolving the previous violation. |
1514027759 | 2015-09-01 | Final Restoration | No Violations | My inspection today finds the well site meets the requirements of 1509.072(B). |
1516789880 | 2014-12-29 | Production Wells | Violations Noted | I received a telephone call from the landowner Lamar Dowling indicating that the well casing failed and he was forced to disconnect from the well due to H2S. I called the well tender David Williams and he corroborated the landowners statements. Upon arrival I found the well was equipped with 4.5 casing with a 4.5 ball valve in the closed position. All valves were closed at the time of inspection. Upon the discovery that the casing in a well is defective or that a well was not adequately constructed, the owner of the well shall notify the Chief of the Division of Oil and Gas Resources Management within twenty-four hours of discovery, and the owner shall immediately repair the casing, correct the construction inadequacies, or plug the well. The well shall be repaired or plugged within 180 days. |
1578471921 | 2015-06-12 | Plug / Plug Back | No Violations | On site to witness rig crew rip pipe and set lime plug they cut pipe off at 4010 and pulled one joint of casing and set 200 plug and pipe became stuck in the well bore had to work hard to get pipe freed up and they pulled 32 joints today and will resume plugging operation on Monday 6/15/15. |
1629458513 | 2015-06-10 | Production Wells | No Violations | I received a voice mail from Donnie with Barry Well Service indicating that the company was preparing to plug the well. My inspection of the site finds Barry Well Service has moved a service rig onto location. Upon arrival I was given twenty four hour notice of intent to plug. |
1813578794 | 2015-06-11 | Plug / Plug Back | No Violations | My inspection today finds the service contractor, Barry Well Service, ran 5729 of 1.5 tubing into the well. Petroset pumped a 30 sack class A plug to 5738 and displaced with 14.2 barrels of water. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1516789880 | US-OH-114395 | 2015-06-22 | Defective casing, leaking well |
For data sources see[9]