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Well ID: 34-121-21850 | Loading map...
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Country: United States | |
State: Ohio | |
County: Noble | |
Municipality: Sharon Township | |
Operator Name: JADCO ENERGY INC | |
Well Pad ID: | |
Farm/Lease Name: WILEY N | |
License Status: Producing | |
License Date: 1980-11-01 | |
Spud Date: 1976-05-20 | |
Spud Drilling Contractor: | |
Final Drill Date: 1976-07-01 | |
Well Total Depth: 5511.00 ft | |
Configuration: Vertical | |
Latitude: 39.710000 | |
Longitude: -81.630000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1976-05-20 | |
Completed | 1976-07-01 | |
Reached Total Depth | 1976-07-01 | |
CO | 1980-11-01 | 295 DAVID OIL CO GeoDate 11/1/80 |
Record Last Modified | 2013-10-03 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 5397 | 5438 | 19 |
5397 | 5438 | 19 | |
5397 | 5438 | 19 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1450 Bbl | 35000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1987 | DAVID OIL CO | 2005.00 | 0.00 | 365 |
1988 | DAVID OIL CO | 2274.00 | 0.00 | 365 |
1989 | DAVID OIL CO | 1959.00 | 0.00 | 365 |
1990 | DAVID OIL CO | 1517.00 | 0.00 | 365 |
1991 | DAVID OIL CO | 1881.00 | 0.00 | 365 |
1992 | DAVID OIL CO | 1984.00 | 0.00 | 365 |
1993 | DAVID OIL CO | 1801.00 | 0.00 | 365 |
1994 | DAVID OIL CO | 1838.00 | 0.00 | 365 |
1995 | DAVID OIL CO | 1525.00 | 0.00 | 365 |
1996 | DAVID OIL CO | 1385.00 | 0.00 | 365 |
1997 | JADCO ENERGY INC | 1453.00 | 0.00 | 365 |
1998 | JADCO ENERGY INC | 1512.00 | 0.00 | 365 |
1999 | JADCO ENERGY INC | 1984.00 | 0.00 | 365 |
2000 | JADCO ENERGY INC | 1855.00 | 0.00 | 365 |
2001 | JADCO ENERGY INC | 3037.00 | 0.00 | 365 |
2002 | JADCO ENERGY INC | 2860.00 | 0.00 | 365 |
2003 | JADCO ENERGY INC | 2837.00 | 0.00 | 365 |
2004 | JADCO ENERGY INC | 2762.00 | 0.00 | 365 |
2005 | JADCO ENERGY INC | 2042.00 | 0.00 | 365 |
2006 | JADCO ENERGY INC | 913.00 | 0.00 | 365 |
2007 | JADCO ENERGY INC | 2655.00 | 0.00 | 365 |
2008 | JADCO ENERGY INC | 2013.00 | 0.00 | 365 |
2009 | JADCO ENERGY INC | 2426.00 | 0.00 | 365 |
2010 | JADCO ENERGY INC | 1926.00 | 0.00 | 365 |
2011 | JADCO ENERGY INC | 1754.00 | 0.00 | 365 |
2012 | JADCO ENERGY INC | 1320.00 | 0.00 | 366 |
2013 | JADCO ENERGY INC | 1582.00 | 0.00 | 365 |
2014 | JADCO ENERGY INC | 1379.00 | 0.00 | 365 |
2015 | JADCO ENERGY INC | 1414.00 | 0.00 | 365 |
2016 | JADCO ENERGY INC | 1130.00 | 0.00 | 365 |
2017 | JADCO ENERGY INC | 1241.00 | 0.00 | 365 |
2018 | JADCO ENERGY INC | 2101.00 | 0.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1987 | DAVID OIL CO | Brine | 0 | 365 |
1988 | DAVID OIL CO | Brine | 0 | 365 |
1989 | DAVID OIL CO | Brine | 0 | 365 |
1990 | DAVID OIL CO | Brine | 0 | 365 |
1991 | DAVID OIL CO | Brine | 0 | 365 |
1992 | DAVID OIL CO | Brine | 0 | 365 |
1993 | DAVID OIL CO | Brine | 0 | 365 |
1994 | DAVID OIL CO | Brine | 0 | 365 |
1995 | DAVID OIL CO | Brine | 0 | 365 |
1996 | DAVID OIL CO | Brine | 0 | 365 |
1997 | JADCO ENERGY INC | Brine | 0 | 365 |
1998 | JADCO ENERGY INC | Brine | 0 | 365 |
1999 | JADCO ENERGY INC | Brine | 0 | 365 |
2000 | JADCO ENERGY INC | Brine | 0 | 365 |
2001 | JADCO ENERGY INC | Brine | 0 | 365 |
2002 | JADCO ENERGY INC | Brine | 68 | 365 |
2003 | JADCO ENERGY INC | Brine | 0 | 365 |
2004 | JADCO ENERGY INC | Brine | 0 | 365 |
2005 | JADCO ENERGY INC | Brine | 0 | 365 |
2006 | JADCO ENERGY INC | Brine | 0 | 365 |
2007 | JADCO ENERGY INC | Brine | 30 | 365 |
2008 | JADCO ENERGY INC | Brine | 0 | 365 |
2009 | JADCO ENERGY INC | Brine | 0 | 365 |
2010 | JADCO ENERGY INC | Brine | 0 | 365 |
2011 | JADCO ENERGY INC | Brine | 0 | 365 |
2012 | JADCO ENERGY INC | Brine | 0 | 366 |
2013 | JADCO ENERGY INC | Brine | 0 | 365 |
2014 | JADCO ENERGY INC | Brine | 37 | 365 |
2015 | JADCO ENERGY INC | Brine | 0 | 365 |
2016 | JADCO ENERGY INC | Brine | 0 | 365 |
2017 | JADCO ENERGY INC | Brine | 0 | 365 |
2018 | JADCO ENERGY INC | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-230622763 | 2011-9-21 0:00: | PW | No Violations | |
0230622763 | 2011-09-21 | Production Wells | No Violations | FOLLOW UP TO NOV # 1316647724 Received complaint from land owner, Connie Stack, of leaking well on property. I inspected site and found well leaking from production casing. It has a repair clamp on it but it is not sealed properly. Well is equipped with 8 surface casing, 4.5 production casing and 1.5 tubing. There is one 210 barrel holding tank on-site. Properly seal leakage on casing whether by new clamp or have service rig pull stretch on casing and repair faulty pipe. Failure to comply may result in bond forfieture. |
1083459954 | 2016-05-11 | Production Wells | No Violations | My inspection today finds the well is equipped with 2 tubing and a plunger lift system. The tank battery is comprised of one100 barrel tank, a horizontal separator and a meter with a current chart. A domestic gas assembly is located at the separator. The production equipment is located in an earthen dike. |
1316647724 | 2011-09-21 | Production Wells | Violations Noted | Received complaint from land owner, Connie Stack, of leaking well on property. I inspected site and found well leaking from production casing. It has a repair clamp on it but it is not sealed properly. Well is equipped with 8 surface casing, 4.5 production casing and 1.5 tubing. There is one 210 barrel holding tank on-site. Properly seal leakage on casing whether by new clamp or have service rig pull stretch on casing and repair faulty pipe. Failure to comply may result in bond forfieture. |
1881292555 | 2011-12-14 | Production Wells | No Violations | Well has been repaired, resolving the previous compliance notice issued on 9/21/2011. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1316647724 | US-OH-109020 | 2011-09-21 | Well insufficiently equipped to prevent escape of oil and gas | |
1316647724 | US-OH-109021 | 2011-09-21 | Defective casing, leaking well |
For data sources see[9]