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Well ID: 34-121-22263 | Loading map...
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Country: United States | |
State: Ohio | |
County: Noble | |
Municipality: Elk Township | |
Operator Name: BECK ENERGY CORPORATION | |
Well Pad ID: | |
Farm/Lease Name: BAKER-MURRAY | |
License Status: Final Restoration | |
License Date: 2008-11-13 | |
Spud Date: 1980-03-23 | |
Spud Drilling Contractor: WARREN DRLG | |
Final Drill Date: 1980-04-01 | |
Well Total Depth: 2856.00 ft | |
Configuration: Vertical | |
Latitude: 39.690000 | |
Longitude: -81.290000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Completed | 1923-04-01 | |
Original Spud | 1980-03-23 | |
Reached Total Depth | 1980-04-01 | |
Completion Report Received | 1980-06-16 | |
CO | 1981-10-14 | 3927 WILMAR OIL & GAS GeoDate 10/14/81 |
Change of Owner | 2003-01-27 | Operator changed from 3927, WILMAR OIL & GAS to 1888, BECK ENERGY CORP |
APP | 2008-11-13 | Proposed Formations:OHIO SHALE, Issued Date:11/13/2008, Expired Date:11/13/2009 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2008-12-16 | |
Construction Permit Expires | 2009-11-13 | |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2003-08-26 | 2414 | 2420 | 6 |
2003-08-26 | 2320 | 2328 | 8 |
2320 | 2328 | 8 | |
2414 | 2420 | 6 | |
2461 | 2471 | 10 | |
2477 | 2483 | 5 | |
2320 | 2328 | 8 | |
2003-08-26 | 2477 | 2483 | 5 |
2003-08-26 | 2461 | 2471 | 10 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
N2 | 0 | 190 Mscf | 60000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | L & M OIL & GAS DEV CO | 3572.00 | 1.00 | 0 |
1985 | ZILKHA ENERGY INC | 2331.00 | 0.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | L & M OIL & GAS DEV CO | Brine | 5 | 0 |
1985 | ZILKHA ENERGY INC | Brine | 126 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-544730999 | 2010-1-28 0:00: | FR | No Violations | |
-91020792 | 2007-4-9 0:00:0 | PW | No Violations | |
0091020792 | 2007-04-09 | Production Wells | No Violations | Inspected site again and found well still idle,noted that some plumbing had been changed on wellhead since my last inspection,well is still incapable of producing in its present state of repair.
Consulted with supervisor and requested that owner be placed on permit hold list. |
0544730999 | 2010-01-28 | Final Restoration | No Violations | Restoration work at site satisfactory pit has been filled in and site restored and vegetation has been established. |
1167241495 | 2006-12-27 | Production Wells | Violations Noted | Complaint called in to inspectors phone of idle well on landowners property(Gary Nurvine),upon inspecting well site found well to be idle and no production reported on said well for quite some time well is equipped with 4.5 casinf anging on clamp no domestic hookup noted called and talked to David Beck concerning well informed him that a NOV was in order for said well have had conversations with Ray Beck concerning well with no results. |
1175027783 | 2007-03-27 | Production Wells | Violations Noted | |
1177022679 | 2007-04-19 | Production Wells | Violations Noted | Upon inspecting well site again found well back into production (swab well) valves on wellhead were open and meter box has chart on it and tank has been painted and properly I.D.ed resolving previous NOV. |
1904746947 | 2006-04-03 | Preliminary Restoration | No Violations | Upon inspecting site found well to be shut in,will call company and discuss status of well with Mr.Beck,well is equipped with 8 surface casing&4.5 production sting hanging on pipe clamp on top of surface casing. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1167241495 | US-OH-104437 | 2006-12-27 | Failure to legibly identify well | |
1167241495 | US-OH-104438 | 2006-12-27 | Well shall be plugged | |
1175027783 | US-OH-104630 | 2006-12-27 | Failure to legibly identify well | |
1175027783 | US-OH-104631 | 2006-12-27 | Well shall be plugged | |
1177022679 | US-OH-104702 | 2006-12-27 | Failure to legibly identify well | |
1177022679 | US-OH-104703 | 2006-12-27 | Well shall be plugged |
For data sources see[9]