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Well ID: 34-121-23062 | Loading map...
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Country: United States | |
State: Ohio | |
County: Noble | |
Municipality: Jackson Township | |
Operator Name: G-R CONTRACTING INC | |
Well Pad ID: | |
Farm/Lease Name: D MORRIS | |
License Status: Final Restoration | |
License Date: 2016-10-25 | |
Spud Date: 1983-11-29 | |
Spud Drilling Contractor: J & B DRILLING | |
Final Drill Date: 1983-12-07 | |
Well Total Depth: 6129.00 ft | |
Configuration: Vertical | |
Latitude: 39.610000 | |
Longitude: -81.540000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1983-09-22 | 6 BENATTY CORP GeoDate 9/22/83 |
Oil and Gas | 1983-09-22 | Issued Date 9/22/83 Expired Date 3/20/84 Acres 0040000 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 06129 Proposed Drill Depth 06129 |
Original Spud | 1983-11-29 | UPDATE COORDINATES PER DOGRM SURVEYOR-ALE 12/13/17. |
Completed | 1983-12-07 | UPDATE COORDINATES PER DOGRM SURVEYOR-ALE 12/13/17. |
Reached Total Depth | 1983-12-07 | UPDATE COORDINATES PER DOGRM SURVEYOR-ALE 12/13/17. |
Completion Report Received | 1984-01-18 | UPDATE COORDINATES PER DOGRM SURVEYOR-ALE 12/13/17. |
CO | 1995-01-20 | 182 BELDEN & BLAKE CO GeoDate 9/22/83 |
Change of Owner | 1998-06-12 | Operator changed from 182, BELDEN & BLAKE CORPORATION to 5352, ARTEX OIL COMPANY |
Change of Owner | 2003-05-06 | Operator changed from 5352, ARTEX OIL COMPANY to 952, G-R CONTRACTING INC |
Last Compliance Report | 2016-08-22 | UPDATE COORDINATES PER DOGRM SURVEYOR-ALE 12/13/17. |
Plugged/Abandoned | 2016-10-13 | UPDATE COORDINATES PER DOGRM SURVEYOR-ALE 12/13/17. |
APP | 2016-10-25 | Proposed Formations:CLINTON SAND, Issued Date:10/25/2016, Expired Date:10/25/2018 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:TAAD, Proposed Well Class: |
Record Last Modified | 2017-12-13 | UPDATE COORDINATES PER DOGRM SURVEYOR-ALE 12/13/17. |
Construction Permit Expires | 2018-10-25 | UPDATE COORDINATES PER DOGRM SURVEYOR-ALE 12/13/17. |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 5830 | 5884 | 18 |
5830 | 5884 | 18 | |
2006-09-11 | 5940 | 5951 | 12 |
5940 | 5951 | 12 | |
5830 | 5884 | 18 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
N2 | 0 | 152500 Mscf | 0 | MEDINA | ||
H2O | 0 | 39000 Gal | 35000 | CLINTON | ||
H2O | 0 | 39000 Gal | 40000 | FRAC; FLUID,SAND,&N2 | ||
N2 | 0 | 133 Mscf | 0 | CLINTON |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | BENATTY CORP | 14283.00 | 0.00 | 0 |
1985 | BENATTY CORP | 7479.00 | 0.00 | 0 |
1986 | BENATTY CORP | 3605.00 | 0.00 | 365 |
1987 | BENATTY CORP | 4281.00 | 0.00 | 365 |
1988 | BENATTY CORP | 3243.00 | 0.00 | 365 |
1989 | BENATTY CORP | 3348.00 | 0.00 | 365 |
1990 | BENATTY CORP | 2469.00 | 0.00 | 365 |
1991 | BENATTY CORP | 2245.00 | 0.00 | 365 |
1992 | BENATTY CORP | 1463.00 | 0.00 | 365 |
1993 | BENATTY CORP | 1513.00 | 0.00 | 365 |
1994 | BELDEN & BLAKE CORPORATION | 1100.00 | 0.00 | 31 |
1995 | BELDEN & BLAKE CORPORATION | 384.00 | 0.00 | 49 |
1999 | ARTEX OIL COMPANY | 0.00 | 0.00 | 0 |
2000 | ARTEX OIL COMPANY | 0.00 | 0.00 | 365 |
2001 | ARTEX OIL COMPANY | 0.00 | 0.00 | 365 |
2002 | G-R CONTRACTING INC | 0.00 | 0.00 | 365 |
2003 | G-R CONTRACTING INC | 0.00 | 0.00 | 365 |
2004 | G-R CONTRACTING INC | 0.00 | 0.00 | 365 |
2005 | G-R CONTRACTING INC | 0.00 | 0.00 | 365 |
2006 | G-R CONTRACTING INC | 0.00 | 0.00 | 365 |
2012 | G-R CONTRACTING INC | 0.00 | 0.00 | 366 |
2013 | G-R CONTRACTING INC | 131.00 | 0.00 | 365 |
2014 | G-R CONTRACTING INC | 0.00 | 0.00 | 365 |
2015 | G-R CONTRACTING INC | 0.00 | 0.00 | 365 |
2016 | G-R CONTRACTING INC | 1236.00 | 0.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | BENATTY CORP | Brine | 0 | 0 |
1985 | BENATTY CORP | Brine | 195 | 0 |
1986 | BENATTY CORP | Brine | 0 | 365 |
1987 | BENATTY CORP | Brine | 150 | 365 |
1988 | BENATTY CORP | Brine | 0 | 365 |
1989 | BENATTY CORP | Brine | 150 | 365 |
1990 | BENATTY CORP | Brine | 150 | 365 |
1991 | BENATTY CORP | Brine | 0 | 365 |
1992 | BENATTY CORP | Brine | 120 | 365 |
1993 | BENATTY CORP | Brine | 0 | 365 |
1994 | BELDEN & BLAKE CORPORATION | Brine | 60 | 31 |
1995 | BELDEN & BLAKE CORPORATION | Brine | 0 | 49 |
1999 | ARTEX OIL COMPANY | Brine | ||
2000 | ARTEX OIL COMPANY | Brine | 0 | 365 |
2001 | ARTEX OIL COMPANY | Brine | 0 | 365 |
2002 | G-R CONTRACTING INC | Brine | 0 | 365 |
2003 | G-R CONTRACTING INC | Brine | 0 | 365 |
2004 | G-R CONTRACTING INC | Brine | 0 | 365 |
2005 | G-R CONTRACTING INC | Brine | 0 | 365 |
2006 | G-R CONTRACTING INC | Brine | 0 | 365 |
2012 | G-R CONTRACTING INC | Brine | 0 | 366 |
2013 | G-R CONTRACTING INC | Brine | 0 | 365 |
2014 | G-R CONTRACTING INC | Brine | 0 | 365 |
2015 | G-R CONTRACTING INC | Brine | 0 | 365 |
2016 | G-R CONTRACTING INC | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1420408808 | 2016-10-11 0:00 | PB | No Violations | 8.00 |
-641963773 | 2016-9-29 0:00: | PB | No Violations | 4.00 |
-842877345 | 2016-8-8 0:00:0 | PW | No Violations | 1.00 |
0000PL7660 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0003476989 | 2002-08-05 | Production Wells | No Violations | |
0641963773 | 2016-09-29 | Plug / Plug Back | No Violations | G-R Contracting used their service rig to attempt to get a hold of the 1.5 tubing setting 4 from the top of the 4.5 casing wellhead. The overshot tool was unable to retrieve the pipe. Appalachian Wireline Surveys attempted to run a collar locator tool down the tubing, but only made it to a depth of 3036. |
0648290986 | 2016-10-13 | Plug / Plug Back | No Violations | During my inspection today Formations Cementing set a 200 foot isolation plug with Class A cement in the 7.875 inch diameter open hole from 3940 feet to 3740 feet. G-R contracting pulled 51 joints of the 4.5 inch diameter casing to 1967 feet. Formations set a 200 foot bottom of surface plug with Class A cement from 1967 feet to 1776 feet. G-R pulled the 4.5 inch diameter casing to 200 foot. Formations cementing set a 200 foot surface plug with Class A cement with 2% calcium. G-R pulled the remaining 4.5 inch casing from the hole. The surface plug dropped and Formations set an additional 125 foot surface plug with Class A cement with 2% calcium. Cement stayed at surface. |
0726455424 | 2016-07-19 | Temporary Abandoned Annular Disposal | No Violations | My inspection today finds the annular disposal is not in use. The well is equipped with 4.5 casing and 1.5 tubing. Both valves on the 4.5 by 1.5 tubing head have rotted off and are laying at the base of the well. Also, the wellhead is very badly corroded, which is consistent with being affected by H2S. The 1.5 tubing and plunger lift lubricator have broken off at the top of the wellhead. There are no means of well control on the 1.5 tubing or the 4.5 casing. A sulfur smell can be detected in the vicinity of the well, but no H2S was noted on the gas detector. A ten foot diameter area, around the well, has been affected to the point that no vegetation is growing. The tank battery is comprised of one 210 barrel tank, a rusted out and collapsed 50 barrel steel tank and a production unit. No identification could be found at the wellhead or the tank battery. G-R Contracting Inc. shall submit a written plugging schedule to Eric Conrad at 5880 Memory Road Zanesville, Ohio 43701 within 15 days, per OAC 1501:9-11-05(B), and plug the well within 90 days. G-R Contracting Inc. will be notified if the plugging schedule is approved or denied. |
0821050425 | 2016-10-12 | Plug / Plug Back | No Violations | The purpose of my inspection today is to witness Appalachian Well Surveys run a bond log and shoot the 4.5 inch diameter casing off. During my inspection Appalachian logged the well and discovered we had free 4.5 inch casing to 4000 feet and the casing appears to be in good condition. Appalachian ran a casing cutter down to 4000 feet and shot the casing off. G-R contracting pulled two joints of the 4.5 inch casing. |
0842877345 | 2016-08-08 | Production Wells | No Violations | My inspection today finds the status of the well has not changed. The wellhead is badly deteriorated. The tubing has broken off. Valves on the 4.5 casing head have rusted off and the well is open to atmosphere. No repairs have been made to the well. I called and spoke to Jordan Jones with G-R Contracting and reminded him that a written plan of action is required for the well. Mr. Jones asked to be allowed to send the plan via email and I agreed. |
1123035080 | 2016-09-14 | Production Wells | No Violations | My inspection today finds the well owner has moved a dozer on location in preparation for plugging. Jordan Jones stated in a telephone conversation that the company intends to place one to two loads of brine in the well to quell any gas flow. |
1420408808 | 2016-10-11 | Plug / Plug Back | No Violations | The purpose of my inspection today is to witness Formations cementing set a plug within the Big Lime formation. During my inspection Appalachian Well Surveys shot the 1.5 inch diameter tubing off at 4525 feet. G-R Contracting pulled two joints of the 1.5 inch tubing and formations set a 300 foot Class A cement plug from 4525 to 4225 feet. G-R Contracting removed all of the 1.5 inch diameter tubing from the hole. |
1475700745 | 2016-10-05 | Plug / Plug Back | No Violations | The purpose of my inspection today is to witness Appalachian Well Surveys shoot the 1.5 inch diameter tubing at 5200 feet in order to get a proper bottom plug. During my inspection Appalachian ran in hole with their tools and they could only make it to 2800 feet. Appalachian pulled their tools back out of the hole and G-R Contraction ran a broach down hole to try and clear a column within the tubing 1.5 inch for Appalachians tools. Once G-R tripped back out of the hole Appalachian ran back in with their tools but could only get down to 3064 feet with this attempt. The depth we need to reach still has not been achieved. Appalachian tripped their tools back out of the hole. When the tools came to surface they attached a heavier sinker bar to the bottom of the casing cutter. Appalachian tripped back into the hole, got down 5194 feet, and successfully cut the 1.5 inch tubing. Appalachian tripped their tools back out of the hole. G-R rigged back up to the 1.5 inch diameter tubing to pull 2 joints up and the rig was not able to pull the tubing. Operations will resume tomorrow. |
1680590625 | 2016-09-20 | Production Wells | No Violations | My inspection today finds the well operator has dug around the wellhead to expose the 8.625 by 4.5 casing head with a back hoe. While digging the 4.5 by 1.5 tubing head fell off. Also, a G-R Contracting employee stated that his personal protection H2S monitor alarmed at 18 parts per million. |
1855330907 | 2016-11-22 | Final Restoration | No Violations | The purpose of my inspection today is a status check on a final restoration. During my inspection the location has been graded and seeded. Vegetation is growing on location and there is not any erosion issues. There is no evidence of an oil and gas well left behind. Location has met 1509.072 B requirements. |
3476989 | 2002-8-5 0:00:0 | PW | No Violations | |
648290986 | 2016-10-13 0:00 | PB | No Violations | 10.50 |
726455424 | 2016-7-19 0:00: | TD | No Violations | 2.00 |
821050425 | 2016-10-12 0:00 | PB | No Violations | 6.00 |
PL7660 | PL | No Violations |
For data sources see[9]