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Well ID: 34-121-23193 | Loading map...
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Country: United States | |
State: Ohio | |
County: Noble | |
Municipality: Jackson Township | |
Operator Name: GENESIS RESOURCES LLC | |
Well Pad ID: | |
Farm/Lease Name: MARIETTA COAL | |
License Status: Producing | |
License Date: 1984-05-31 | |
Spud Date: 1984-06-09 | |
Spud Drilling Contractor: J & B DRILLING | |
Final Drill Date: 1984-06-17 | |
Well Total Depth: 6217.00 ft | |
Configuration: Vertical | |
Latitude: 39.600000 | |
Longitude: -81.500000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1984-05-31 | 6 BENATTY CORP GeoDate 5/31/84 |
Oil and Gas | 1984-05-31 | Issued Date 5/31/84 Expired Date 11/27/84 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 06217 Proposed Drill Depth 06217 |
Original Spud | 1984-06-09 | |
Completed | 1984-06-17 | |
Reached Total Depth | 1984-06-17 | |
Completion Report Received | 1984-07-24 | |
Construction Permit Expires | 1984-11-27 | |
CO | 1995-01-20 | 182 BELDEN & BLAKE CO GeoDate 5/31/84 |
Change of Owner | 2003-05-07 | Operator changed from 182, BELDEN & BLAKE CORPORATION to 5352, ARTEX OIL COMPANY |
Change of Owner | 2003-05-07 | Operator changed from 5352, ARTEX OIL COMPANY to 952, G-R CONTRACTING INC |
Last Compliance Report | 2014-04-15 | |
Change of Owner | 2019-01-22 | Operator changed from 952, G-R CONTRACTING INC to 9086, GENESIS RESOURCES LLC |
Record Last Modified | 2019-01-22 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 5924 | 6014 | 0 |
5924 | 6014 | 0 | |
2006-09-11 | 5950 | 5958 | 2 |
5950 | 5958 | 2 | |
5924 | 6014 | 0 | |
2006-09-11 | 6062 | 6078 | 2 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
N2 | 0 | 155 Mscf | 0 | CL. | ||
N2 | 0 | 134 Mscf | 0 | MED. | ||
H2O | 0 | 36500 Gal | 40000 | FRAC: H2O,SAND,N2 | ||
H2O | 0 | 45750 Gal | 40000 | CL. |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | BENATTY CORP | 13576.00 | 0.00 | 0 |
1985 | BENATTY CORP | 34348.00 | 0.00 | 0 |
1986 | BENATTY CORP | 15431.00 | 0.00 | 365 |
1987 | BENATTY CORP | 11381.00 | 0.00 | 365 |
1988 | BENATTY CORP | 7915.00 | 0.00 | 365 |
1989 | BENATTY CORP | 6036.00 | 0.00 | 365 |
1990 | BENATTY CORP | 4841.00 | 0.00 | 365 |
1991 | BENATTY CORP | 3153.00 | 0.00 | 365 |
1992 | BENATTY CORP | 3482.00 | 0.00 | 365 |
1993 | BENATTY CORP | 3150.00 | 0.00 | 365 |
1994 | BELDEN & BLAKE CORPORATION | 782.00 | 0.00 | 366 |
1995 | BELDEN & BLAKE CORPORATION | 950.00 | 41.00 | 249 |
1996 | BELDEN & BLAKE CORPORATION | 184.00 | 0.00 | 141 |
1999 | ARTEX OIL COMPANY | 1880.00 | 0.00 | 0 |
2000 | ARTEX OIL COMPANY | 1632.00 | 0.00 | 365 |
2001 | ARTEX OIL COMPANY | 2191.00 | 0.00 | 365 |
2002 | G-R CONTRACTING INC | 0.00 | 0.00 | 365 |
2003 | G-R CONTRACTING INC | 0.00 | 0.00 | 365 |
2004 | G-R CONTRACTING INC | 249.00 | 0.00 | 365 |
2005 | G-R CONTRACTING INC | 0.00 | 0.00 | 365 |
2006 | G-R CONTRACTING INC | 0.00 | 0.00 | 365 |
2007 | G-R CONTRACTING INC | 0.00 | 0.00 | 365 |
2008 | G-R CONTRACTING INC | 0.00 | 0.00 | 365 |
2009 | G-R CONTRACTING INC | 42.00 | 0.00 | 365 |
2010 | G-R CONTRACTING INC | 0.00 | 0.00 | 365 |
2011 | G-R CONTRACTING INC | 0.00 | 0.00 | 365 |
2012 | G-R CONTRACTING INC | 0.00 | 0.00 | 366 |
2013 | G-R CONTRACTING INC | 0.00 | 0.00 | 365 |
2014 | G-R CONTRACTING INC | 0.00 | 0.00 | 365 |
2015 | G-R CONTRACTING INC | 0.00 | 0.00 | 365 |
2016 | G-R CONTRACTING INC | 0.00 | 0.00 | 365 |
2017 | G-R CONTRACTING INC | 0.00 | 0.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | BENATTY CORP | Brine | 0 | 0 |
1985 | BENATTY CORP | Brine | 420 | 0 |
1986 | BENATTY CORP | Brine | 320 | 365 |
1987 | BENATTY CORP | Brine | 325 | 365 |
1988 | BENATTY CORP | Brine | 140 | 365 |
1989 | BENATTY CORP | Brine | 101 | 365 |
1990 | BENATTY CORP | Brine | 135 | 365 |
1991 | BENATTY CORP | Brine | 100 | 365 |
1992 | BENATTY CORP | Brine | 0 | 365 |
1993 | BENATTY CORP | Brine | 60 | 365 |
1994 | BELDEN & BLAKE CORPORATION | Brine | 0 | 366 |
1995 | BELDEN & BLAKE CORPORATION | Brine | 0 | 249 |
1996 | BELDEN & BLAKE CORPORATION | Brine | 0 | 141 |
1999 | ARTEX OIL COMPANY | Brine | ||
2000 | ARTEX OIL COMPANY | Brine | 0 | 365 |
2001 | ARTEX OIL COMPANY | Brine | 0 | 365 |
2002 | G-R CONTRACTING INC | Brine | 0 | 365 |
2003 | G-R CONTRACTING INC | Brine | 0 | 365 |
2004 | G-R CONTRACTING INC | Brine | 0 | 365 |
2005 | G-R CONTRACTING INC | Brine | 0 | 365 |
2006 | G-R CONTRACTING INC | Brine | 0 | 365 |
2007 | G-R CONTRACTING INC | Brine | 0 | 365 |
2008 | G-R CONTRACTING INC | Brine | 0 | 365 |
2009 | G-R CONTRACTING INC | Brine | 0 | 365 |
2010 | G-R CONTRACTING INC | Brine | 0 | 365 |
2011 | G-R CONTRACTING INC | Brine | 0 | 365 |
2012 | G-R CONTRACTING INC | Brine | 0 | 366 |
2013 | G-R CONTRACTING INC | Brine | 0 | 365 |
2014 | G-R CONTRACTING INC | Brine | 0 | 365 |
2015 | G-R CONTRACTING INC | Brine | 0 | 365 |
2016 | G-R CONTRACTING INC | Brine | 0 | 365 |
2017 | G-R CONTRACTING INC | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-2121904182 | 2014-3-27 0:00: | PW | No Violations | 1.50 |
-81323815 | 2014-2-25 0:00: | PW | No Violations | 4.50 |
0000PL7568 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0081323815 | 2014-02-25 | Production Wells | No Violations | The company sent a dozer to repair the lease road. Once accessing the location we determined that the 4.5 casing has no pressure and the tubing has over 600 psi. The pressures indicate the tubing may be set on a packer. The 8.625 casing has over 150 psi and the gas has traces of H2S. I instructed the company representative to flare the gas off of the 8.625 casing and load the hole with fluid to stop the flow of gas. |
0152812929 | 2008-09-02 | Annular Disposal | No Violations | A.D.not hooked up well is shut in at present time, it is equipped with tubing&production casing&8 surface casing and 1-100 bbl tank in need of dike work preformed will call company and discuss future plans on placing well into production or file for plugging permit/ |
0169267478 | 2014-01-31 | Annular Disposal | No Violations | The annular disposal is not in use. The well is equipped with 4.5 casing and 1.5 tubing. All the valves are shut. The well has a significant lean. It appears the casing has failed at the surface. There is a strong odor of sulfur at the well. I will return on Monday to test the area for H2S. The lease road is impassible. |
0523912195 | 2014-02-06 | Production Wells | Violations Noted | My inspection finds the well is equipped to be produced by a plunger lift system. All valves are shut in at the well. A test of the area around the 8.625 casing, with a Honeywell PhD6 gas meter, indicated that H2S gas was present in amounts of 80 ppm. I contacted Mr. Shulzberger with G-R Contracting and made him aware of the issue. Mr. Shulzberger was directed to immediately cordon off the area around the well and post signage notifying people of the danger. I also directed Mr. Shulzberger to submit a plan in writing that outlines the company plan to kill the well to prevent the flow of H2S. Additionally I asked for a plan to remedy the well long term with a specific time frame. IMMEDIATELY STOP THE FLOW OF H2S. IMMEDIATELY REPAIR THE CASING, CORRECT THE CONSTRUCTION INADEQUACIES, OR PLUG AND ABANDON THE WELL. SUBMIT, IN WRITING, A PLAN WITH TIME LINES TO ACHIEVE THESE REQUIREMENTS WITHIN 72 HOURS. |
0942950055 | 2014-02-05 | Administrative Inspection | No Violations | I called Jordan with G-R Contracting at 1:06 pm. I spoke to him about the condition of the well. He stated that a truck had struck the well sometime ago and caused the well to lean. I informed him that I detected a strong odor, that may be H2S, on my 1/31/14 inspection and that I would return to test the well as soon as the weather permitted. I also told him that if the well was leaking H2S the company would be required to take immediate action. |
1224540657 | 2008-10-20 | Annular Disposal | No Violations | Upon inspecting site again found well is still shut in contacted owner and he stated they would apply for plugging permit over the winter months and plug said well in the spring of 09. |
1393017683 | 2014-02-21 | Administrative Inspection | No Violations | I called Jordan Jones of G-R Contracting at 11:15 am. I asked him when he was going to move a dozer and water truck to the site to kill the flow of sour gas. He stated that the county roads were too soft and he did not want to tear them up with the heavy trucks. I agreed to allow them to wait until next Tuesday for the road conditions to improve. |
152812929 | 2008-9-2 0:00:0 | AD | No Violations | |
1586784220 | 2020-4-2 0:00:0 | TD | No Violations | 0.10 |
1638373737 | 2020-4-6 0:00:0 | AM | No Violations | 0.30 |
169267478 | 2014-1-31 0:00: | AD | No Violations | 1.00 |
2121904182 | 2014-03-27 | Production Wells | No Violations | My inspection finds the well has been returned to production. The previous violations have been corrected. The flow of H2S has been stopped. The well is equipped with 1.5 tubing on a packer and is being produced through an intermittent timer. A meter is set on location and it has a current chart. |
266917430 | 2020-4-22 0:00: | PW | No Violations | 1.00 |
50833373 | 2020-4-2 0:00:0 | PW | No Violations | 1.50 |
523912195 | 2014-2-6 0:00:0 | PW | No Violations | |
942950055 | 2014-2-5 0:00:0 | AM | No Violations | 0.20 |
PL7568 | PL | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0523912195 | US-OH-125726 | 2014-04-10 | General Safety | |
0523912195 | US-OH-125727 | 2014-04-10 | Well shall be plugged |
For data sources see[9]