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Well ID: 34-121-23528 | Loading map...
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Country: United States | |
State: Ohio | |
County: Noble | |
Municipality: Enoch Township | |
Operator Name: NORTHWOOD ENERGY CORP | |
Well Pad ID: | |
Farm/Lease Name: ARNOLD C | |
License Status: Producing | |
License Date: 2014-02-21 | |
Spud Date: 1986-01-08 | |
Spud Drilling Contractor: CT DRILLING | |
Final Drill Date: 1986-01-18 | |
Well Total Depth: 6220.00 ft | |
Configuration: Vertical | |
Latitude: 39.690000 | |
Longitude: -81.410000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1985-12-16 | 122 TIGER OIL INC GeoDate 12/16/85 |
Oil and Gas | 1985-12-16 | Issued Date 12/16/85 Expired Date 12/16/86 Acres 0057000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 06220 Proposed Drill Depth 06220 |
Original Spud | 1986-01-08 | LOG TYPE=LASER |
Completed | 1986-01-18 | LOG TYPE=LASER |
Reached Total Depth | 1986-01-18 | LOG TYPE=LASER |
Completion Report Received | 1986-06-11 | LOG TYPE=LASER |
CO | 1994-11-28 | 2680 ENERGY CONTRACTORS INC GeoDate 12/16/85 |
CO | 1995-07-10 | 2680 ENERGY CONTRACTORS INC GeoDate 12/16/85 |
Change of Owner | 1998-09-28 | Operator changed from 2680, ENERGY CONTRACTORS INC to 56, BUCKEYE OIL PRODUCING CO |
APP | 2005-11-29 | Proposed Formations:OHIO SHALE, Issued Date:11/29/2005, Expired Date:11/29/2006 6:00:00 AM, Drilling unit acres:57, Proposed Well Type:TAAD, Proposed Well Class:POOL |
Change of Owner | 2006-04-07 | Operator changed from 56, BUCKEYE OIL PRODUCING CO to 2680, ENERGY CONTRACTORS INC |
Change of Owner | 2008-07-14 | Operator changed from 2680, ENERGY CONTRACTORS INC to 1634, NORTHWOOD ENERGY CORP |
Last Compliance Report | 2009-10-10 | LOG TYPE=LASER |
APP | 2014-02-21 | Proposed Formations:DEVONIAN SHALE/ORISKANY SS, Issued Date:2/21/2014, Expired Date:2/21/2016 12:00:00 PM, Drilling unit acres:57, Proposed Well Type:OG, Proposed Well Class:POOL |
Plugged Back | 2014-04-23 | LOG TYPE=LASER |
Construction Permit Expires | 2016-02-21 | LOG TYPE=LASER |
Record Last Modified | 2017-10-23 | LOG TYPE=LASER |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 6064 | 6063 | 2 |
6064 | 6063 | 2 | |
6064 | 6063 | 2 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
N2 | 0 | 150 Mscf | 0 | |||
2014-04-23 | H2O | 8 | 7715 Bbl | 77750 | Producers Service Corporation | |
H2O | 0 | 1500 Bbl | 28000 | |||
ACID | 0 | 500 Gal | 0 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1986 | TIGER OIL INC | 3939.00 | 0.00 | 212 |
1987 | TIGER OIL INC | 3191.00 | 0.00 | 365 |
1989 | TIGER OIL INC | 2291.00 | 0.00 | 365 |
1990 | TIGER OIL INC | 1525.00 | 0.00 | 365 |
1991 | TIGER OIL INC | 2011.00 | 0.00 | 365 |
1992 | TIGER OIL INC | 998.00 | 26.00 | 365 |
1993 | TIGER OIL INC | 777.00 | 0.00 | 330 |
1994 | TIGER OIL INC | 1121.00 | 0.00 | 365 |
1995 | ENERGY CONTRACTORS INC | 1004.00 | 0.00 | 365 |
1996 | ENERGY CONTRACTORS INC | 712.00 | 0.00 | 365 |
1997 | ENERGY CONTRACTORS INC | 961.00 | 0.00 | 365 |
1998 | ENERGY CONTRACTORS INC | 947.00 | 0.00 | 365 |
1999 | BUCKEYE OIL PRODUCING CO | 1014.00 | 0.00 | 0 |
2000 | BUCKEYE OIL PRODUCING CO | 438.00 | 0.00 | 0 |
2001 | BUCKEYE OIL PRODUCING CO | 335.00 | 0.00 | 365 |
2002 | BUCKEYE OIL PRODUCING CO | 391.00 | 0.00 | 365 |
2003 | BUCKEYE OIL PRODUCING CO | 432.00 | 0.00 | 365 |
2004 | BUCKEYE OIL PRODUCING CO | 176.00 | 0.00 | 365 |
2005 | BUCKEYE OIL PRODUCING CO | 13.00 | 0.00 | 365 |
2006 | BUCKEYE OIL PRODUCING CO | 340.00 | 0.00 | 365 |
2008 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2009 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2010 | NORTHWOOD ENERGY CORP | 508.00 | 0.00 | 365 |
2011 | NORTHWOOD ENERGY CORP | 503.00 | 0.00 | 0 |
2012 | NORTHWOOD ENERGY CORP | 408.00 | 0.00 | 366 |
2013 | NORTHWOOD ENERGY CORP | 200.00 | 0.00 | 365 |
2014 | NORTHWOOD ENERGY CORP | 636.00 | 0.00 | 365 |
2015 | NORTHWOOD ENERGY CORP | 1281.00 | 0.00 | 365 |
2016 | NORTHWOOD ENERGY CORP | 373.00 | 0.00 | 365 |
2017 | NORTHWOOD ENERGY CORP | 203.00 | 0.00 | 365 |
2018 | NORTHWOOD ENERGY CORP | 105.00 | 0.00 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1610124878 | 2009-1-16 0:00: | AD | No Violations | |
-1829278356 | 2014-4-14 0:00: | PB | No Violations | 4.00 |
-2065959049 | 2014-4-16 0:00: | PB | No Violations | 3.00 |
-847680108 | 2014-4-9 0:00:0 | PB | No Violations | 4.00 |
-880849876 | 2014-4-1 0:00:0 | PB | No Violations | |
0000PL7371 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0000UIC298 | 1987-01-16 | Annular Disposal | No Violations | 1501:9-3-11 (B)(4) |
0000UIC299 | 1987-01-16 | Annular Disposal | No Violations | 1501:9-3-11 (B)(5) |
0000UIC300 | 1987-01-16 | Annular Disposal | No Violations | 1501:9-3-11 (A)(3) |
0082834096 | 2014-04-02 | Plug / Plug Back | No Violations | My inspection today finds the service rig crew is unable to run the wire line tools past 4378. The rig crew has made several runs with a stem and an impression block to determine what the obstruction is. There were no discernable markings on the impression block. The fluid level is staying at 500 from surface. The company is going to try and run another type of impression block. |
0172076201 | 2009-03-03 | Production Wells | No Violations | Well is idle and incapable of producing,tubing has been removed from well since my last inspection,and flow line is not hooked to well suspect hole in casing there is a strong sulphur smell at well head ,also no I.D. could be found ,will consult with supervisor onhow he wants to proceed with outstanding violations at well site. |
0255234099 | 2004-06-30 | Production Wells | No Violations | No violations noted on the day of my inspection. |
0502395405 | 2014-04-03 | Plug / Plug Back | No Violations | My inspection finds the rig crew ran another impression block and there was still no sign of what is preventing the tools from going to bottom. The rig crew then ran a sand pump to 4378. The sand pump did not retrieve any material from the bottom. The company is going to run 2 tubing and a drill bit tomorrow to try and clear the obstruction. |
0847680108 | 2014-04-09 | Plug / Plug Back | No Violations | Upon my arrival I witnessed the service rig crew pulling the tubing out of the hole. The bit was removed from the tubing and a few small pieces of shale were found. The rig crew pulled on the 4.5 casing to see if it was free. The pipe is not free. The rig crew began to run a flat bottom mill on the tubing string to make an attempt to clear the obstruction. |
0880849876 | 2014-04-01 | Plug / Plug Back | No Violations | A dozer has prepared the location and the service rig is setting at the end of the lease road. |
1111933526 | 2014-02-28 | Administrative Inspection | No Violations | At 12:01 PM I called Bill Arnholt. I discussed the violation against the well with Mr. Arnholt. Bill stated that the well will be plugged back this summer. A permit to plug back has been issued. |
1289913614 | 2014-04-15 | Plug / Plug Back | No Violations | My inspection today finds the service rig pulled 800 of 4.5 casing. They then ran 4150 of 2 tubing. Cemenco spotted a 72 sk class A cement plug through the 2 tubing. The rig crew pulled the tubing out of the hole. |
1327138578 | 2012-01-20 | Production Wells | No Violations | Upon inspection the well has appeared to of been repaired and in production ,past records show several violations by previous well owner ,Annular Disposal not hooked up, at well head the following equipment is present 4.5casing -2tubing -production valves open ,being produced by means of a pumping unit, well capable of production. |
1380551649 | 2014-04-11 | Plug / Plug Back | No Violations | My inspection finds the tubing and mill are stuck at 4150. Cemenco is onsite to attempt to regain circulation. The rig pulled 75,000 pounds on the tubing. The tubing will not rotate and circulation could not be established. |
1383382573 | 2009-01-16 | Annular Disposal | No Violations | FOLLOW UP TO NOV # -1610124878 Inspection revealed that well is idle a slight odor of H2S is present at wellhead suspect casing possibly has a hole in it,last production reported on well was back in 2006,no ID could be found on tank or at wellhead. |
1395150362 | 2014-03-17 | Annular Disposal | No Violations | My inspection today finds the annular disposal is not hooked up and not in use. The well is equipped with 4.5 casing, 2 tubing, rods, and a pump jack. All production valves are open. The tank battery is comprised of a 100 bbl tank, a separator, and a meter with a current chart. |
1397229408 | 2014-04-10 | Plug / Plug Back | No Violations | My inspection finds the drilling rig is running a flat bottom mill on 2.375 EUE tubing with a string float and a bit sub. The tubing sat down at 4120. The company will attempt to mill down to and through the obstruction at 4380 |
1610124878 | 2009-01-16 | Annular Disposal | Violations Noted | Inspection revealed that well is idle a slight odor of H2S is present at wellhead suspect casing possibly has a hole in it,last production reported on well was back in 2006,no ID could be found on tank or at wellhead. |
172076201 | 2009-3-3 0:00:0 | PW | No Violations | |
1821922609 | 2009-07-30 | Annular Disposal | Violations Noted | Inspection revealed that well is still idle,no change in status of well since my last inspection. |
1829278356 | 2014-04-14 | Plug / Plug Back | No Violations | My inspection finds Appalachian Wireline Services cut the 2 tubing of at 4200. The service rig pulled the tubing. Appalachian then cut the 4.5 casing at 4170. The rig pulled 800 of 4.5 casing. |
2065959049 | 2014-04-16 | Plug / Plug Back | No Violations | My inspection finds the service rig crew ran in the well with the sand line and tagged the plug at 3921. Further operations will resume on Monday 4-20. |
2136926058 | 2012-01-20 | Production Wells | No Violations | Upon inspection the well has appeared to of been repaired and in production, past records show several violations by previous well owner, Annular Disposal not hooked up, at well head the following equipment is present 4.5casing -2tubing -production valves open, being produced by means of a pumping unit, well capable of production. |
2142071247 | 2014-04-23 | Plug / Plug Back | No Violations | My inspection today finds Davis Well Service ran 3497 of 9.5 pound 4.5 casing. Cemenco cemented the pipe in place with 170 sks of class A with 2% gel and 140 sks of strait class A cement. |
255234099 | 2004-6-30 0:00: | PW | No Violations | |
502395405 | 2014-4-3 0:00:0 | PB | No Violations | 5.00 |
82834096 | 2014-4-2 0:00:0 | PB | No Violations | |
PL7371 | PL | No Violations | ||
UIC298 | 1987-1-16 0:00: | AD | No Violations | |
UIC299 | 1987-1-16 0:00: | AD | No Violations | |
UIC300 | 1987-1-16 0:00: | AD | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1610124878 | US-OH-115810 | 2009-01-16 | Well operation causing pollution and contamination | |
1610124878 | US-OH-115811 | 2009-01-16 | Failure to legibly identify well | |
1610124878 | US-OH-115812 | 2009-01-16 | Well shall be plugged | |
1821922609 | US-OH-118201 | 2009-01-16 | Well operation causing pollution and contamination | |
1821922609 | US-OH-118202 | 2009-01-16 | Failure to legibly identify well | |
1821922609 | US-OH-118203 | 2009-01-16 | Well shall be plugged |
For data sources see[9]