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Well ID: 34-121-24355 | Loading map...
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Country: United States | |
State: Ohio | |
County: Noble | |
Municipality: Center Township | |
Operator Name: NORTHWOOD ENERGY CORP | |
Well Pad ID: | |
Farm/Lease Name: WATSON S | |
License Status: Producing | |
License Date: 2012-03-02 | |
Spud Date: 2012-03-27 | |
Spud Drilling Contractor: FMS DRILLING | |
Final Drill Date: 2012-04-06 | |
Well Total Depth: 4360.00 ft | |
Configuration: Vertical | |
Latitude: 39.800000 | |
Longitude: -81.480000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2012-03-02 | Proposed Formations:BEREA THRU ORISKANY, Issued Date:3/2/2012, Expired Date:3/2/2014 12:00:00 PM, Drilling unit acres:286.673, Proposed Well Type:OG, Proposed Well Class:POOL |
Reached Total Depth | 2012-04-06 | |
Completion Report Received | 2013-03-01 | |
Construction Permit Expires | 2014-03-02 | |
Record Last Modified | 2015-09-24 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2013-03-04 | 2130 | 3152 | 152 |
2130 | 3152 | 152 | |
2130 | 3152 | 152 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
2012-04-18 | H2O | 7 | 252140 Gal | 60000 | Producers Service Corporation | 1st stage frac-well was perferated from 2668' to 3152' using hollow steel carrier's with a total of 84 shots in this zone , also set 2nd stage wireline frac plug @2610' and perferate 2nd stage on this date ,2nd stage to be fracked tomorrow.Invoice #13895 |
2012-04-19 | H2O | 7 | 252139 Gal | 60000 | Producers Service Corporation | Perfed from 2130' to 2478' 68 shot- hollow steel carrier .Invoice #13869 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2012 | NORTHWOOD ENERGY CORP | 0.00 | 224.00 | 366 |
2013 | NORTHWOOD ENERGY CORP | 13257.00 | 5800.00 | 365 |
2014 | NORTHWOOD ENERGY CORP | 10727.00 | 4290.00 | 365 |
2015 | NORTHWOOD ENERGY CORP | 5398.00 | 1998.00 | 365 |
2016 | NORTHWOOD ENERGY CORP | 4529.00 | 716.00 | 365 |
2017 | NORTHWOOD ENERGY CORP | 4251.00 | 390.00 | 365 |
2018 | NORTHWOOD ENERGY CORP | 3560.00 | 328.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2012 | NORTHWOOD ENERGY CORP | Brine | 521 | 366 |
2013 | NORTHWOOD ENERGY CORP | Brine | 941 | 365 |
2014 | NORTHWOOD ENERGY CORP | Brine | 25 | 365 |
2015 | NORTHWOOD ENERGY CORP | Brine | 22 | 365 |
2016 | NORTHWOOD ENERGY CORP | Brine | 34 | 365 |
2017 | NORTHWOOD ENERGY CORP | Brine | 48 | 365 |
2018 | NORTHWOOD ENERGY CORP | Brine | 119 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-105222550 | 2013-2-14 0:00: | PW | No Violations | 6.00 |
-1936224599 | 2018-11-8 0:00: | PW | No Violations | 1.00 |
-196480471 | 2015-11-9 0:00: | PW | No Violations | |
-362316994 | 2020-3-4 0:00:0 | PW | No Violations | 0.50 |
-533200533 | 2015-11-13 0:00 | PW | No Violations | 1.00 |
-599234449 | 2019-4-12 0:00: | PW | No Violations | 1.50 |
-709431626 | 2020-3-3 0:00:0 | PW | No Violations | 0.50 |
0105222550 | 2013-02-14 | Production Wells | No Violations | My inspection today finds that the pressure relief valve has been opening and has released approximately 2 bbl of oil. I contacted Northwood Energy and Corps Oil Field Services and told them of the spill. Within two hours there were five contractors on site to clean the spill. By 3:00pm. the spill had been cleaned. |
0160763153 | 2019-04-23 | Production Wells | No Violations | The purpose of my inspection is to follow up on a previously issued compliance notice. On the day of my inspection I witnessed production equipment including a 210 barrel steel production fluid storage tank, 100-barrel steel production fluid storage tank, a horizontal separator which appears to be the primary means of separation and a vertical separator that is acting as a fluid drop out for the sales line, there is also a drip and 2-inch diameter meter run with .500 orifice. The well was equipped with 8.625-inch diameter surface casing, 4.5-inch diameter production casing with 2.375-inch diameter tubing, with rods, a lubricator, and a Churchill Pumping Unit with an electric motor. The lubricator on the well head was running into a 50-gallon steel drum. At the time of my inspection it appeared that the contaminated soil had been removed from around the well head, the earthen containment was still in place but appeared to be free of pollution and contamination. At the time of my inspection Mike Corp a contractor for Northwood Energy Corporation stopped by, I informed Mike that the trash and jugs around the pumping unit needed to be cleaned up, but compliance issued for pollution and contamination will be closed. |
0196480471 | 2015-11-09 | Production Wells | Violations Noted | My inspection today finds an area of crude oil contamination 45 from the wellhead. An area approximately 40 square feet is discolored and has a strong odor of crude oil. A small earthen dike around the wellhead has a couple inches of oil contaminated absorbent lying in it. The tank battery has multiple leaking pipe connections with some of them allowing natural gas to escape to atmosphere and oil to reach the ground. Remove all contaminated soil and repair |
0451175211 | 2019-01-23 | Production Wells | No Violations | The purpose of my inspection is to follow up on a previously issued compliance notice. On the day of my inspection I witnessed production equipment including a 210 barrel, and 100-barrel steel production fluid storage tank, a horizontal separator which appears to be the primary means of separation and a vertical separator that is acting as a fluid drop out for the sales line, there is also a drip and 2-inch diameter meter run with .500 orifice. The well was equipped with 8.625-inch diameter surface casing, 4.5-inch diameter production casing with 2.375- |
0452842061 | 2013-02-14 | Production Wells | No Violations | Notification was received at 7:35 Am by Eric Byers of Byers Oil & Gas that He observed the well storage tank battery separator dispersing fluid. I made notification to the lead inspector Eric Conrad and proceeded to respond to the site. Upon arrival @ 7:40 Am it was observed that the separator check valve was releasing oil into the tank battery. At 7:45 Am a Northwood representative arrived and shut the well in stopping the dispersant of product. I assisted Inspector Conrad with the spill report and left location at 9:00 Am. Notification was made to the Southeast supervisor Rocky King at 7:38 Am and a copy of the spill report sent Kyle Tharp and Rocky King. |
0533200533 | 2015-11-13 | Production Wells | No Violations | My inspection today finds the previous violation has been resolved. |
0599234449 | 2019-04-12 | Production Wells | No Violations | The purpose of my inspection is to follow up on a previously issued compliance notice. On the day of my inspection I witnessed production equipment including a 210 barrel steel production fluid storage tank, 100-barrel steel production fluid storage tank, a horizontal separator which appears to be the primary means of separation and a vertical separator that is acting as a fluid drop out for the sales line, there is also a drip and 2-inch diameter meter run with .500 orifice. The well was equipped with 8.625-inch diameter surface casing, 4.5-inch diameter production casing with 2.375-inch diameter tubing, with rods, a lubricator, and a Churchill Pumping Unit with an electric motor. There was approximately 80 square feet of pollution and contamination in a dike that was created around the well head. There were multiple areas on the well equipment that appeared to be leaking, and the lubricator valve was open and running to a 50- |
1100097963 | 2012-09-11 | Production Wells | No Violations | My inspection today finds the well is equipped with 4.5 casing, 2.375 tubing, rods, and a pump jack. The tank battery consists of one 210 bbl tank, one 100 bbl tank, a separator, and a meter inside of a dike with proper identification. The location has recently been seeded. Pipe line work is under way. |
1329462201 | 2018-12-03 | Production Wells | Violations Noted | On the day of my inspection I witnessed production equipment including a 210 barrel, and 100 barrel steel production fluid storage tank, a horizontal separator which appears to be the primary means of separation and a vertical separator that is acting as a fluid drop out for the sales line, there is also a drip and 2 inch diameter meter run with .500 orifice. The well was equipped with 8.625-inch diameter surface casing, 4.5-inch diameter production casing with 2.375-inch diameter tubing, with rods, a lubricator, and a Churchill Pumping Unit with an electric motor. There was approximately 80 square feet of pollution and contamination in a dike that was created around the well head. There were multiple areas on the well equipment that appeared to be leaking. All valves were open at the time of my inspection and the well was pumping at the time of my inspection, production was reported for 2017. I contacted Northwood Energy Corporation, Cory McCudden and informed him a compliance notice will be issued for the well. |
1361304879 | 2013-02-19 | Production Wells | No Violations | My inspection today finds the small oil spill has been fully cleaned and there is no oil visible in the effected area. |
1404240197 | 2014-07-01 | Production Wells | No Violations | My inspection finds Corps Well Service is cleaning a small oil spill around the well. A small dike around the wellhead contained the oil in 4 x 4 area. The company has removed all heavy oil from the area and is applying a bio remediating material. |
1558713196 | 2019-5-24 0:00: | WR | No Violations | 1.00 |
160763153 | 2019-4-23 0:00: | PW | No Violations | 1.00 |
1765266350 | 2019-11-1 0:00: | PW | No Violations | 0.80 |
1780753188 | 2012-10-25 | Preliminary Restoration | No Violations | My inspection today finds the well site has been reclaimed. The pits are filled, and vegetation has been established. |
1936224599 | 2018-11-08 | Production Wells | No Violations | On the day of my inspection I witnessed production equipment including a 210 barrel, and 100 barrel steel production fluid storage tank, a horizontal separator which appears to be the primary means of separation and a vertical separator that is acting as a fluid drop out for the sales line, there is also a drip and 2 inch diameter meter run with .500 orifice. The well was equipped with 8.625-inch diameter surface casing, 4.5-inch diameter production casing with 2.375-inch diameter tubing, with rods and a Churchill Pumping Unit with an electric motor. There was approximately 80 square feet of pollution and contamination in a dike that was created around the well. There were multiple areas on the well equipment that appeared to be leaking. I contacted Mike Corp with Northwood energy and informed him of the problem. Identification tags were present, and production was reported for 2017. |
451175211 | 2019-1-23 0:00: | PW | No Violations | 1.00 |
452842061 | 2013-2-14 0:00: | PW | No Violations | |
97722671 | 2019-9-11 0:00: | PW | No Violations | 0.80 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0196480471 | US-OH-119841 | 2015-11-23 | Well operation causing pollution and contamination | |
1329462201 | US-OH-109430 | 2019-05-13 | 9-1-07 | Well operation causing pollution and contamination |
For data sources see[9]