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Well ID: 34-121-24595 | Loading map...
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Country: United States | |
State: Ohio | |
County: Noble | |
Municipality: Beaver Township | |
Operator Name: ANTERO RESOURCES CORPORATION | |
Well Pad ID: US-OH-001330 | |
Farm/Lease Name: POTTER UNIT | |
License Status: Drilling | |
License Date: 2015-10-20 | |
Spud Date: 2015-11-11 | |
Spud Drilling Contractor: | |
Final Drill Date: | |
Well Total Depth: 100.00 ft | |
Configuration: Horizontal | |
Latitude: 39.880000 | |
Longitude: -81.270000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2015-10-20 | Proposed Formations:POINT PLEASANT, Issued Date:10/20/2015, Expired Date:10/19/2017 12:00:00 PM, Drilling unit acres:526.871, Proposed Well Type:OG, Proposed Well Class:POOL |
Record Last Modified | 2017-02-10 | |
Construction Permit Expires | 2017-10-19 |
For data sources see[2]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0170436507 | 2015-11-12 | Casing String Witnessed | No Violations | On site inspection to witness the conductor cement job found Express Energys top hole rig spudded the said well on 11/11/2015 and drilled a 100 x 32 borehole. Express Energys cement service cemented the casing using 33o sacks of class A-2% calcium .125 and displaced to 90 using 56 barrels of fresh water with good cement returns witnessed to surface. |
1013591312 | 2018-09-18 | Drill / Deepen / Reopen | No Violations | The Quintel Pad consists of 10 wells and 1 conductor. RBDMS records show a conductor was drilled with no other strings spudded. The mouse hole was visible at surface but the conductor was not. |
1456318680 | 2016-02-23 | Preliminary Restoration | No Violations | My inspection today finds the well site meets the preliminary restoration requirements of 1509.72(A). |
170436507 | 2015-11-12 0:00 | CS | No Violations | 2.00 |
For data sources see[3]