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Well ID: 34-127-22120 | Loading map...
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Country: United States | |
State: Ohio | |
County: Perry | |
Municipality: Jackson Township | |
Operator Name: BELL OIL | |
Well Pad ID: | |
Farm/Lease Name: HARMON NEAL | |
License Status: Final Restoration | |
License Date: 2018-01-26 | |
Spud Date: 1961-02-04 | |
Spud Drilling Contractor: | |
Final Drill Date: 1961-03-05 | |
Well Total Depth: 2759.00 ft | |
Configuration: Vertical | |
Latitude: 39.690000 | |
Longitude: -82.360000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1961-02-04 | UPDATE LOCATION PER DOGRM SURVEYOR ALE 4/16/18. GMM UPDATED PLUG STAUS PER PLUG REPORT |
Completed | 1961-03-05 | UPDATE LOCATION PER DOGRM SURVEYOR ALE 4/16/18. GMM UPDATED PLUG STAUS PER PLUG REPORT |
Reached Total Depth | 1961-03-05 | UPDATE LOCATION PER DOGRM SURVEYOR ALE 4/16/18. GMM UPDATED PLUG STAUS PER PLUG REPORT |
CO | 1995-04-25 | 315 BELL OIL GeoDate 4/25/95 |
APP | 2018-01-26 | Proposed Formations:CLINTON SAND, Issued Date:1/26/2018, Expired Date:1/26/2020 12:00:00 PM, Drilling unit acres:60, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2018-05-29 | UPDATE LOCATION PER DOGRM SURVEYOR ALE 4/16/18. GMM UPDATED PLUG STAUS PER PLUG REPORT |
Record Last Modified | 2018-12-19 | UPDATE LOCATION PER DOGRM SURVEYOR ALE 4/16/18. GMM UPDATED PLUG STAUS PER PLUG REPORT |
Construction Permit Expires | 2020-01-26 | UPDATE LOCATION PER DOGRM SURVEYOR ALE 4/16/18. GMM UPDATED PLUG STAUS PER PLUG REPORT |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 700 Bbl | 20000 |
For data sources see[3]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1988 | M & S OIL CO | 0.00 | 233.00 | 365 |
1990 | M & S OIL CO | 0.00 | 203.00 | 365 |
1991 | M & S OIL CO | 0.00 | 182.00 | 365 |
1992 | M & S OIL CO | 0.00 | 199.00 | 365 |
1993 | M & S OIL CO | 0.00 | 145.00 | 365 |
1994 | M & S OIL CO | 0.00 | 132.00 | 365 |
1995 | BELL OIL | 0.00 | 219.00 | 365 |
1996 | BELL OIL | 0.00 | 251.00 | 365 |
1997 | BELL OIL | 0.00 | 204.00 | 365 |
1998 | BELL OIL | 0.00 | 101.00 | 365 |
1999 | BELL OIL | 0.00 | 206.00 | 365 |
2000 | BELL OIL | 0.00 | 207.00 | 365 |
2001 | BELL OIL | 0.00 | 313.00 | 365 |
2002 | BELL OIL | 0.00 | 338.00 | 365 |
2003 | BELL OIL | 0.00 | 195.00 | 365 |
2004 | BELL OIL | 0.00 | 228.00 | 365 |
2005 | BELL OIL | 0.00 | 241.00 | 365 |
2006 | BELL OIL | 0.00 | 142.00 | 365 |
2007 | BELL OIL | 0.00 | 144.00 | 365 |
2008 | BELL OIL | 0.00 | 183.00 | 365 |
2009 | BELL OIL | 0.00 | 274.00 | 365 |
2010 | BELL OIL | 0.00 | 255.00 | 365 |
2011 | BELL OIL | 0.00 | 257.00 | 365 |
2012 | BELL OIL | 0.00 | 224.00 | 366 |
2013 | BELL OIL | 0.00 | 230.00 | 365 |
2014 | BELL OIL | 0.00 | 235.00 | 365 |
2015 | BELL OIL | 0.00 | 111.00 | 365 |
2016 | BELL OIL | 0.00 | 113.00 | 365 |
2017 | BELL OIL | 0.00 | 121.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1988 | M & S OIL CO | Brine | 0 | 365 |
1990 | M & S OIL CO | Brine | 0 | 365 |
1991 | M & S OIL CO | Brine | 0 | 365 |
1992 | M & S OIL CO | Brine | 0 | 365 |
1993 | M & S OIL CO | Brine | 0 | 365 |
1994 | M & S OIL CO | Brine | 0 | 365 |
1995 | BELL OIL | Brine | 0 | 365 |
1996 | BELL OIL | Brine | 0 | 365 |
1997 | BELL OIL | Brine | 0 | 365 |
1998 | BELL OIL | Brine | 0 | 365 |
1999 | BELL OIL | Brine | 0 | 365 |
2000 | BELL OIL | Brine | 0 | 365 |
2001 | BELL OIL | Brine | 0 | 365 |
2002 | BELL OIL | Brine | 0 | 365 |
2003 | BELL OIL | Brine | 0 | 365 |
2004 | BELL OIL | Brine | 0 | 365 |
2005 | BELL OIL | Brine | 0 | 365 |
2006 | BELL OIL | Brine | 0 | 365 |
2007 | BELL OIL | Brine | 33 | 365 |
2008 | BELL OIL | Brine | 0 | 365 |
2009 | BELL OIL | Brine | 0 | 365 |
2010 | BELL OIL | Brine | 0 | 365 |
2011 | BELL OIL | Brine | 0 | 365 |
2012 | BELL OIL | Brine | 0 | 366 |
2013 | BELL OIL | Brine | 0 | 365 |
2014 | BELL OIL | Brine | 0 | 365 |
2015 | BELL OIL | Brine | 0 | 365 |
2016 | BELL OIL | Brine | 0 | 365 |
2017 | BELL OIL | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1081484709 | 2018-5-18 0:00: | PB | No Violations | |
-1175149276 | 2008-1-17 0:00: | PW | No Violations | |
-1214642905 | 2018-12-11 0:00 | FR | No Violations | 0.50 |
-1301541548 | 2018-5-29 0:00: | PB | No Violations | 1.00 |
-376465098 | 2018-9-7 0:00:0 | PB | No Violations | 0.50 |
-673604061 | 2018-5-16 0:00: | PB | No Violations | 3.00 |
0022448124 | 2017-12-28 | Production Wells | No Violations | I was on location today to do a field inspection on this well. Linn Bell has moved his service rig in on this well to plug it. At this point they are waiting on the plugging permit for it. They have pulled the rods and tubing from the well and will plug the well with clay once they get the permit. The rig crew was not on location at the time of my inspection. |
0083296456 | 2018-05-24 | Plug / Plug Back | No Violations | I was back on location today to witness the plugging of this well. Today the rig crew is washing in the surface plug with plugging clay. Once the clay reaches the surface the well will be left open for a couple days to make sure the clay does not settle. |
0376465098 | 2018-09-07 | Plug / Plug Back | No Violations | I was on location today to do the final restoration on this well. The final restoration meets 1509.072(B) requirements. |
0429195468 | 2008-03-18 | Production Wells | No Violations | Follow-up on NOV, In-Compliance. |
0673604061 | 2018-05-16 | Plug / Plug Back | No Violations | I was on location today to witness the plugging activities on this well. The rig crew washed in the bottom plug using plugging clay then they ripped the 4.5 inch diameter casing at 2340 feet. The Lime plug was then washed in before the rig crew worked on pulling out the 4.5 inch casing. The rig crew will pull out the rest of the casing today then we will run in the 7 inch pre-cast plug tomorrow. |
1081484709 | 2018-05-18 | Plug / Plug Back | No Violations | I was back on location this morning to witness the plugging activities on the well. Today Mr. Bell washed in more plugging clay on top of the 7 inch seat. The well is taking the clay slow because of the water level in the well. When I was leaving the location he was working on welding an 8 inch nipple onto the casing so he could retrieve the 8 inch from the well. |
1175149276 | 2008-01-17 | Production Wells | Violations Noted | An inspection of the well and tank battery revealed no ID at the well or tank battery, and dike around tanks do not meet SPCC requirements. |
1214642905 | 2018-12-11 | Final Restoration | No Violations | I was on location today to do the final restoration on this well. The final restoration meets 1509.072(B) requirements. |
1301541548 | 2018-05-29 | Plug / Plug Back | No Violations | I returned to this well today to make sure the clay had stayed at the surface before the company started to reclaim it. The clay was still at the surface so I let Mr. Bell know he could reclaim this location. |
1329805221 | 2018-05-17 | Plug / Plug Back | No Violations | Today I was back on location to witness the plugging of the well. The rig crew is running the 7 inch pre-cast plug down to the 7 inch seat today. They were able to get the plug down to 900 feet. The rig crew will now wash in a few ton of clay on top of the pre-cast plug before trying to remove the 8 inch surface casing. |
22448124 | 2017-12-28 0:00 | PW | No Violations | 0.50 |
429195468 | 2008-3-18 0:00: | PW | No Violations | |
83296456 | 2018-5-24 0:00: | PB | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1175149276 | US-OH-104639 | 2008-01-17 | Failure to legibly identify well | |
1175149276 | US-OH-104640 | 2008-01-17 | No SPCC dike/or failure to keep dike free of water or oil |
For data sources see[8]