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Well ID: 34-127-22283 | ![]() Sorry, we have no imagery here. Sorry, we have no imagery here. ![]() |
Country: United States | |
State: Ohio | |
County: Perry | |
Municipality: Hopewell Township | |
Operator Name: DIVERSIFIED PRODUCTION LLC | |
Well Pad ID: | |
Farm/Lease Name: SHELLY FRANK V | |
License Status: Producing | |
License Date: 1963-06-21 | |
Spud Date: 1963-06-20 | |
Spud Drilling Contractor: | |
Final Drill Date: 1963-07-17 | |
Well Total Depth: 2735.00 ft | |
Configuration: Vertical | |
Latitude: 39.880000 | |
Longitude: -82.320000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1801-01-02 | 79 OXFORD OIL CO |
Oil and Gas | 1802-01-01 | |
Original Spud | 1963-06-20 | |
Completed | 1963-07-17 | |
Reached Total Depth | 1963-07-17 | |
Change of Owner | 2014-02-06 | Operator changed from 79, OXFORD OIL to 9216, ECLIPSE RESOURCES-OHIO LLC |
Change of Owner | 2016-08-02 | Operator changed from 9216, ECLIPSE RESOURCES-OHIO LLC to 8685, M & R INVESTMENTS OHIO LLC |
Record Last Modified | 2016-08-04 |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 820 Bbl | 12000 |
For data sources see[3]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | OXFORD OIL | 0.00 | 305.00 | 0 |
1985 | OXFORD OIL | 0.00 | 289.00 | 365 |
1986 | OXFORD OIL | 0.00 | 230.00 | 365 |
1987 | OXFORD OIL | 0.00 | 290.00 | 365 |
1988 | OXFORD OIL | 0.00 | 225.00 | 365 |
1989 | OXFORD OIL | 0.00 | 137.00 | 365 |
1990 | OXFORD OIL | 0.00 | 235.00 | 365 |
1991 | OXFORD OIL | 0.00 | 147.00 | 365 |
1992 | OXFORD OIL | 0.00 | 244.00 | 365 |
1993 | OXFORD OIL | 0.00 | 159.00 | 365 |
1994 | OXFORD OIL | 0.00 | 204.00 | 365 |
1995 | OXFORD OIL | 0.00 | 146.00 | 365 |
1996 | OXFORD OIL | 0.00 | 232.00 | 366 |
1997 | OXFORD OIL | 0.00 | 231.00 | 365 |
1998 | OXFORD OIL | 0.00 | 148.00 | 365 |
1999 | OXFORD OIL | 0.00 | 224.00 | 365 |
2000 | OXFORD OIL | 0.00 | 229.00 | 0 |
2001 | OXFORD OIL | 0.00 | 152.00 | 365 |
2002 | OXFORD OIL | 0.00 | 153.00 | 365 |
2003 | OXFORD OIL | 0.00 | 192.00 | 365 |
2004 | OXFORD OIL | 0.00 | 176.00 | 365 |
2005 | OXFORD OIL | 0.00 | 129.00 | 365 |
2006 | OXFORD OIL | 0.00 | 225.00 | 365 |
2007 | OXFORD OIL | 0.00 | 143.00 | 365 |
2008 | OXFORD OIL | 0.00 | 140.00 | 0 |
2009 | OXFORD OIL | 0.00 | 156.00 | 0 |
2010 | OXFORD OIL | 0.00 | 159.00 | 365 |
2011 | OXFORD OIL | 0.00 | 150.00 | 0 |
2012 | OXFORD OIL | 0.00 | 155.00 | 0 |
2013 | ECLIPSE RESOURCES-OHIO LLC | 0.00 | 159.00 | 365 |
2014 | ECLIPSE RESOURCES-OHIO LLC | 0.00 | 223.00 | 365 |
2015 | ECLIPSE RESOURCES-OHIO LLC | 0.00 | 154.00 | 365 |
2016 | M & R INVESTMENTS OHIO LLC | 0.00 | 100.00 | 365 |
2017 | M & R INVESTMENTS OHIO LLC | 0.00 | 230.00 | 365 |
2018 | M & R INVESTMENTS OHIO LLC | 0.00 | 157.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | OXFORD OIL | Brine | 0 | 0 |
1985 | OXFORD OIL | Brine | 30 | 365 |
1986 | OXFORD OIL | Brine | 25 | 365 |
1987 | OXFORD OIL | Brine | 20 | 365 |
1988 | OXFORD OIL | Brine | 100 | 365 |
1989 | OXFORD OIL | Brine | 40 | 365 |
1990 | OXFORD OIL | Brine | 35 | 365 |
1991 | OXFORD OIL | Brine | 40 | 365 |
1992 | OXFORD OIL | Brine | 30 | 365 |
1993 | OXFORD OIL | Brine | 20 | 365 |
1994 | OXFORD OIL | Brine | 40 | 365 |
1995 | OXFORD OIL | Brine | 30 | 365 |
1996 | OXFORD OIL | Brine | 30 | 366 |
1997 | OXFORD OIL | Brine | 30 | 365 |
1998 | OXFORD OIL | Brine | 70 | 365 |
1999 | OXFORD OIL | Brine | 51 | 365 |
2000 | OXFORD OIL | Brine | 36 | |
2001 | OXFORD OIL | Brine | 28 | 365 |
2002 | OXFORD OIL | Brine | 34 | 365 |
2003 | OXFORD OIL | Brine | 28 | 365 |
2004 | OXFORD OIL | Brine | 24 | 365 |
2005 | OXFORD OIL | Brine | 26 | 365 |
2006 | OXFORD OIL | Brine | 47 | 365 |
2007 | OXFORD OIL | Brine | 10 | 365 |
2008 | OXFORD OIL | Brine | 16 | |
2009 | OXFORD OIL | Brine | 15 | |
2010 | OXFORD OIL | Brine | 36 | 365 |
2011 | OXFORD OIL | Brine | 27 | |
2012 | OXFORD OIL | Brine | 20 | |
2013 | ECLIPSE RESOURCES-OHIO LLC | Brine | 25 | 365 |
2014 | ECLIPSE RESOURCES-OHIO LLC | Brine | 25 | 365 |
2015 | ECLIPSE RESOURCES-OHIO LLC | Brine | 0 | 365 |
2016 | ECLIPSE RESOURCES-OHIO LLC | Brine | 0 | 365 |
2017 | M & R INVESTMENTS OHIO LLC | Brine | 30 | 365 |
2018 | M & R INVESTMENTS OHIO LLC | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1283373749 | 2007-2-21 0:00: | PW | No Violations | |
-1570471757 | 2017-7-17 0:00: | PW | No Violations | 3.00 |
-1755116777 | 2017-8-18 0:00: | PW | No Violations | |
-248084712 | 2017-7-17 0:00: | PW | No Violations | 1.00 |
-469598085 | 2008-11-19 0:00 | PW | No Violations | |
-807849128 | 2020-7-14 0:00: | PW | No Violations | 0.50 |
-8475176 | 2013-8-7 0:00:0 | PW | No Violations | 1.00 |
0008475176 | 2013-08-07 | Production Wells | No Violations | This well is capable of production. It has a pumping unit on it with rods and 2 tubing. The identification for the well is on the tank. The valve coming off the well to the production tank is open. No violations at this time. |
0095448660 | 2017-08-07 | Production Wells | No Violations | I returned to this well today to do a follow-up inspection on it. While I was on location today Rusty and Kevin from M&R Investments were on site working on building the fence around the tank pad. The production tank has been reset, the dike has been rebuilt and they are working on finishing the rest. I will stop back in a couple of days to see if everything is finished. |
0248084712 | 2017-07-17 | Production Wells | No Violations | I returned to this well today to do a follow-up inspection on it. The company has put down an absorbent material to soak up any oil inside the contained area. They will continue to clean up and remove any contamination until it is clean. |
0309632011 | 2015-04-02 | Production Wells | No Violations | Inspection on 4/2/2015 the well and tank were identified properly. Well is capable of producing. Tank battery consisted of two 100 barrel tanks with knockout. Upon inspection of the well there was found to be a small leak with escaping gas around the 4 1/2 well head.. A call was placed to Mike Hartshorn to have Jerry Love the pumper correct the situation. |
0340457603 | 2018-12-19 | Production Wells | No Violations | I was on location today to do a field inspection on this well. The well appears to be capable of production at this time. The well has a pumping unit on it with rods and 2 inch diameter tubing in it. The valves are open from the well to the tank pad. The identification is located on the production tank. There are no violations at this time. |
0469598085 | 2008-11-19 | Production Wells | No Violations | No violations. |
0484732709 | 2017-07-20 | Production Wells | No Violations | I returned back to this location today to check on the clean-up around the tank pad. It looks like the company has been back here and put down more absorbent on the contaminated areas. I tried to contact Jody Jasper from M&R Investments during the time of my inspection to see when they would be setting the production tank back up but I did not reach him. His phone did not go to voicemail so I will try to call him again later in the day. Jody Jasper returned my phone call while I was still on location. He stated at this time he is trying to reach the township and has left them a message to see if they could relocate the production tank on there property so it does not flood again. He stated that they have not got back with him yet so he would try again and let me know what they said. |
0628991585 | 2016-06-30 | Production Wells | No Violations | I was on location today to do a field inspection on this well. The well appears to be capable of production. It has a pumping unit on it with rods and 2 tubing in it. The valves are open from the well to the tank pad. The identification is located on the production tank. There are no violations at this time. |
1062453921 | 2018-01-22 | Production Wells | No Violations | I was on location today to do a field inspection on this well. The well appears to be capable of production at this time. It has a pumping unit on it with rods and 2 inch diameter tubing in it. The valves are open from the wellhead to the tank pad. The identification is located on the production tank. There are no violations at this time. |
1250281015 | 2018-09-07 | Production Wells | No Violations | I stopped by this well to check on the production tank. We are suppose to get a bunch of rain over the next couple of days so I contacted Matt the supervisor for M&R Investments to see if he can find out how much fluid is in the tank and make sure it is secured so it does not float away again from the heavy rain. He is currently working on it now. |
1283373749 | 2007-02-21 | Production Wells | No Violations | No violations. |
1500315053 | 2017-07-13 | Production Wells | Violations Noted | This inspection was conducted as a status check. I received a phone call regarding a 100 barrel tank flipping on its side due to a flood where high water reached the tank battery. I arrived to the location at 7:30 PM and was accompanied by Southwest Region Supervisor Dan Goins. Ohio EPA OSC Trevor Irwin was on location during inspection. The inspection revealed that water depth at the tank battery location was approximately 6 feet and was responsible for floating the tank and tipping it on its side. The tank stayed within the dike area. Oil was observed on top of the water. A Diversified Resources vac truck arrived at approximately 8:30 PM to cacuum up oil from around the tank. The company was advised to clean up contamination. This was regarded as a verbal compliance notice. |
1500551734 | 2017-07-20 | Production Wells | No Violations | This inspection was conducted as a compliance notice follow-up. No personnel were present during inspection. The oil contamination has been cleaned up. The company has indicated that they are planning on setting the tank battery on higher ground. Time of inspection: 7:55 AM. Weather: 70*F, Partly cloudy |
1559775174 | 2019-05-30 | Production Wells | No Violations | I was on location today to do a field inspection on this well. The well appears to be capable of production at this time. The well has a pumping unit on it with rods and 2 inch diameter tubing in it. The valves are open from the well to the tank pad. The identification is located on the production tank. There are no violations at this time. |
1570471757 | 2017-07-17 | Production Wells | No Violations | I was on location today to check on the clean-up of this location. All the rain we got caused a 100 barrel production tank to lift up and break off from the water knockout. This caused some contamination around the tank pad. The company responded fast and got the production tank emptied and pulled up out of the flooded area. After discussing it with Jody Jasper from M&R Investments and Aaron Wolfe from the EPA they believe they lost less then 20 gallons from what they had in the production tank and what they recovered. The company stated that they had around 2 feet in the tank and they recovered right at 2 feet. The company is working on setting the production tank in a different spot so this does not happen again. |
1755116777 | 2017-08-18 | Production Wells | No Violations | I returned to this well today to check the status of the clean-up. At this point the well is no longer in violation. All of the contamination has been removed, the production tank has been reset, the contamination dike has been rebuilt and a new fence has been put around the production tank. There are no violations at this time. |
1850869098 | 2017-07-14 | Production Wells | No Violations | This inspection was conducted as a follow-up. Inspector Justin Smith was on location when I arrived. Ohio EPA OSC Aaron Wolfe was on location during inspection as well as Perry County Wildlife Officer Eric Lane. Cleanup was in progress during the inspection. The water had receded approximately 8 feet since the previous night. The 100 barrel tank was pulled up onto higher ground. Photos were taken of the cleanup. Time of inspection: 8:40 AM. |
309632011 | 2015-4-2 0:00:0 | PW | No Violations | 1.00 |
340457603 | 2018-12-19 0:00 | PW | No Violations | 0.50 |
484732709 | 2017-7-20 0:00: | PW | No Violations | 1.00 |
628991585 | 2016-6-30 0:00: | PW | No Violations | 1.00 |
95448660 | 2017-8-7 0:00:0 | PW | No Violations | 1.00 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1500315053 | US-OH-114113 | 2017-12-27 | 9-1-07 | Well operation causing pollution and contamination |
For data sources see[8]