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Well ID: 34-127-22932 | Loading map...
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Country: United States | |
State: Ohio | |
County: Perry | |
Municipality: Jackson Township | |
Operator Name: MH OILFIELD SERVICE LLC | |
Well Pad ID: | |
Farm/Lease Name: MCCANDLISH HAROLD N | |
License Status: Producing | |
License Date: 1981-06-18 | |
Spud Date: 1969-10-24 | |
Spud Drilling Contractor: | |
Final Drill Date: 1970-01-13 | |
Well Total Depth: 2985.00 ft | |
Configuration: Vertical | |
Latitude: 39.670000 | |
Longitude: -82.350000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1969-10-24 | |
Completed | 1970-01-13 | |
Reached Total Depth | 1970-01-13 | |
CO | 1981-06-18 | 75 BARCLAY PETROLEUM INC GeoDate 6/18/81 |
Change of Owner | 2017-11-27 | Operator changed from 75, BARCLAY PETROLEUM INC to 8277, MH OILFIELD SERVICE LLC |
Record Last Modified | 2017-11-27 |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1785 Bbl | 15000 |
For data sources see[3]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1985 | MARJAC ENERGY CO | 0.00 | 322.00 | 0 |
1986 | MARJAC ENERGY CO | 0.00 | 243.00 | 365 |
1988 | BARCLAY PETROLEUM INC | 0.00 | 201.00 | 365 |
1989 | BARCLAY PETROLEUM INC | 0.00 | 217.00 | 365 |
1990 | BARCLAY PETROLEUM INC | 0.00 | 228.00 | 365 |
1991 | BARCLAY PETROLEUM INC | 0.00 | 176.00 | 340 |
1992 | BASS ENERGY CO INC | 0.00 | 196.00 | 260 |
1993 | BARCLAY PETROLEUM INC | 0.00 | 119.00 | 260 |
1994 | BARCLAY PETROLEUM INC | 0.00 | 142.00 | 365 |
1995 | BARCLAY PETROLEUM INC | 0.00 | 75.00 | 365 |
1996 | BARCLAY PETROLEUM INC | 0.00 | 0.00 | 100 |
1997 | BARCLAY PETROLEUM INC | 0.00 | 0.00 | 120 |
1998 | BARCLAY PETROLEUM INC | 0.00 | 0.00 | 120 |
1999 | BARCLAY PETROLEUM INC | 0.00 | 0.00 | 90 |
2000 | BARCLAY PETROLEUM INC | 0.00 | 0.00 | 120 |
2001 | BARCLAY PETROLEUM INC | 0.00 | 0.00 | 20 |
2002 | BARCLAY PETROLEUM INC | 0.00 | 0.00 | 20 |
2003 | BARCLAY PETROLEUM INC | 0.00 | 0.00 | 14 |
2004 | BARCLAY PETROLEUM INC | 0.00 | 0.00 | 30 |
2005 | BARCLAY PETROLEUM INC | 0.00 | 0.00 | 15 |
2006 | BARCLAY PETROLEUM INC | 0.00 | 0.00 | 30 |
2007 | BARCLAY PETROLEUM INC | 0.00 | 0.00 | 180 |
2008 | BARCLAY PETROLEUM INC | 0.00 | 0.00 | 60 |
2009 | KENOIL LLC | 0.00 | 0.00 | 365 |
2010 | BARCLAY PETROLEUM INC | 0.00 | 0.00 | 0 |
2011 | BARCLAY PETROLEUM INC | 0.00 | 0.00 | 60 |
2012 | BARCLAY PETROLEUM INC | 0.00 | 0.00 | 0 |
2013 | BARCLAY PETROLEUM INC | 0.00 | 0.00 | 60 |
2014 | BARCLAY PETROLEUM INC | 0.00 | 0.00 | 0 |
2015 | BARCLAY PETROLEUM INC | 0.00 | 0.00 | 0 |
2016 | BARCLAY PETROLEUM INC | 0.00 | 0.00 | 0 |
2017 | BARCLAY PETROLEUM INC | 0.00 | 0.00 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1276987625 | 2007-8-15 0:00: | AD | No Violations | |
-1340453482 | 2007-8-13 0:00: | AD | No Violations | |
-1915459745 | 2007-8-14 0:00: | AD | No Violations | |
0767002492 | 2007-12-03 | Annular Disposal | No Violations | Follow-up inspection of water complaint, tested water from inside Mrs. Gillogys holding tank for water, field test reading was a little over 600ppm, Mrs. Gillogy said they have not been pumping the water, explained that the water would be ok for household use but not drinking. Felt that with the rainy season it would clear up. Told Mrs. Gillogy that I would notify Mr. Kellie and explain that he would not have to have water hauled out but would still need to bring out drinking water until I felt the water would meet EPA standards of 250 ppm. Mr Kellie will remove plastic holding tank from yard and Mr. Gillogy will hook up to his water supply. |
1189778435 | 2007-09-10 | Annular Disposal | No Violations | Follow-up on NOV, and met with Bruce Kellie ( owner ) and Tom Tomastik from Columbus, reviewed well site, tank battery and spring, Tom feels spring should clear up if spring is flushed and clean out more in dike area. Bruce said he will continue to haul fresh water in for Connie Gillogy the landowner. Explained to Mrs. Gillogy that holding tank should be cleaned out and spring should be pumped to allow water to flush through the rock formation. |
1276987625 | 2007-08-15 | Annular Disposal | No Violations | Follow-up on NOV, tanks are emptied and ready to be moved. |
1340453482 | 2007-08-13 | Annular Disposal | Violations Noted | An inspection of the well and tank battery revealed both production tanks leaking brine, it appears the bottoms or the tanks may have holes. There is a water well complaint of brine in drinking water, approx 200ft from there tank battery, this maybe where the brine is coming from. No ID at the well or tank battery. Called company office and left a message about leaking tanks and contaminated water system. |
1592392132 | 2020-6-16 0:00: | PW | No Violations | 1.00 |
1726879047 | 2007-12-03 | Annular Disposal | No Violations | Follow-up on NOV, In-Compliance. Done a field test on water with Quantab, the reading was around 250 to 260 ppm. Explained to Mrs. Gillogly that it meets EPA safe drinking standards and the company had complied with NOV. Took water sample from kitchen sink, allowed water to run approx. 45 seconds. Mrs. Gillogy said she was not happy with the companys offer and would be seeking further legal actions and I may be called in as a witness. |
1843561595 | 2020-8-27 0:00: | PW | No Violations | 0.50 |
1915459745 | 2007-08-14 | Annular Disposal | No Violations | Spoke with Bruce Kellie about violations and contaminated water system. Bruce said he has emptied tanks and will be removing them from dike to start dirt removal. |
767002492 | 2007-12-3 0:00: | AD | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1340453482 | US-OH-109803 | 2007-08-20 | Well operation causing pollution and contamination | |
1340453482 | US-OH-109804 | 2007-08-20 | Well not equipped to prevent escape of oil and/or gas | |
1340453482 | US-OH-109805 | 2007-08-20 | Failure to legibly identify well | |
1340453482 | US-OH-109806 | 2007-08-20 | Failure to keep SPCC dike/pit free of brine and other wastes |
For data sources see[8]