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34-127-22932

Well Details

Well ID: 34-127-22932
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Country: United States
State: Ohio
County: Perry
Municipality: Jackson Township
Operator Name: MH OILFIELD SERVICE LLC
Well Pad ID:
Farm/Lease Name: MCCANDLISH HAROLD N
License Status: Producing
License Date: 1981-06-18
Spud Date: 1969-10-24
Spud Drilling Contractor:
Final Drill Date: 1970-01-13
Well Total Depth: 2985.00 ft
Configuration: Vertical
Latitude: 39.670000
Longitude: -82.350000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1969-10-24
Completed 1970-01-13
Reached Total Depth 1970-01-13
CO 1981-06-18 75 BARCLAY PETROLEUM INC GeoDate 6/18/81
Change of Owner 2017-11-27 Operator changed from 75, BARCLAY PETROLEUM INC to 8277, MH OILFIELD SERVICE LLC
Record Last Modified 2017-11-27

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1785 Bbl 15000

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1985 MARJAC ENERGY CO 0.00 322.00 0
1986 MARJAC ENERGY CO 0.00 243.00 365
1988 BARCLAY PETROLEUM INC 0.00 201.00 365
1989 BARCLAY PETROLEUM INC 0.00 217.00 365
1990 BARCLAY PETROLEUM INC 0.00 228.00 365
1991 BARCLAY PETROLEUM INC 0.00 176.00 340
1992 BASS ENERGY CO INC 0.00 196.00 260
1993 BARCLAY PETROLEUM INC 0.00 119.00 260
1994 BARCLAY PETROLEUM INC 0.00 142.00 365
1995 BARCLAY PETROLEUM INC 0.00 75.00 365
1996 BARCLAY PETROLEUM INC 0.00 0.00 100
1997 BARCLAY PETROLEUM INC 0.00 0.00 120
1998 BARCLAY PETROLEUM INC 0.00 0.00 120
1999 BARCLAY PETROLEUM INC 0.00 0.00 90
2000 BARCLAY PETROLEUM INC 0.00 0.00 120
2001 BARCLAY PETROLEUM INC 0.00 0.00 20
2002 BARCLAY PETROLEUM INC 0.00 0.00 20
2003 BARCLAY PETROLEUM INC 0.00 0.00 14
2004 BARCLAY PETROLEUM INC 0.00 0.00 30
2005 BARCLAY PETROLEUM INC 0.00 0.00 15
2006 BARCLAY PETROLEUM INC 0.00 0.00 30
2007 BARCLAY PETROLEUM INC 0.00 0.00 180
2008 BARCLAY PETROLEUM INC 0.00 0.00 60
2009 KENOIL LLC 0.00 0.00 365
2010 BARCLAY PETROLEUM INC 0.00 0.00 0
2011 BARCLAY PETROLEUM INC 0.00 0.00 60
2012 BARCLAY PETROLEUM INC 0.00 0.00 0
2013 BARCLAY PETROLEUM INC 0.00 0.00 60
2014 BARCLAY PETROLEUM INC 0.00 0.00 0
2015 BARCLAY PETROLEUM INC 0.00 0.00 0
2016 BARCLAY PETROLEUM INC 0.00 0.00 0
2017 BARCLAY PETROLEUM INC 0.00 0.00 0

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1985 MARJAC ENERGY CO Brine 150 0
1986 MARJAC ENERGY CO Brine 125 365
1988 BARCLAY PETROLEUM INC Brine 0 365
1989 BARCLAY PETROLEUM INC Brine 0 365
1990 BARCLAY PETROLEUM INC Brine 80 365
1991 BARCLAY PETROLEUM INC Brine 135 340
1992 BASS ENERGY CO INC Brine 140 260
1993 BARCLAY PETROLEUM INC Brine 140 260
1994 BARCLAY PETROLEUM INC Brine 140 365
1995 BARCLAY PETROLEUM INC Brine 70 365
1996 BARCLAY PETROLEUM INC Brine 15 100
1997 BARCLAY PETROLEUM INC Brine 0 120
1998 BARCLAY PETROLEUM INC Brine 0 120
1999 BARCLAY PETROLEUM INC Brine 0 90
2000 BARCLAY PETROLEUM INC Brine 0 120
2001 BARCLAY PETROLEUM INC Brine 0 20
2002 BARCLAY PETROLEUM INC Brine 0 20
2003 BARCLAY PETROLEUM INC Brine 0 14
2004 BARCLAY PETROLEUM INC Brine 0 30
2005 BARCLAY PETROLEUM INC Brine 0 15
2006 BARCLAY PETROLEUM INC Brine 0 30
2007 BARCLAY PETROLEUM INC Brine 0 180
2008 BARCLAY PETROLEUM INC Brine 0 60
2009 KENOIL LLC Brine 145 365
2010 BARCLAY PETROLEUM INC Brine 0 0
2011 BARCLAY PETROLEUM INC Brine 0 60
2012 BARCLAY PETROLEUM INC Brine 0 0
2013 BARCLAY PETROLEUM INC Brine 0 60
2014 BARCLAY PETROLEUM INC Brine 0 0
2015 BARCLAY PETROLEUM INC Brine 0 0
2016 BARCLAY PETROLEUM INC Brine 0 0
2017 BARCLAY PETROLEUM INC Brine 0 0

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1276987625 2007-8-15 0:00: AD No Violations
-1340453482 2007-8-13 0:00: AD No Violations
-1915459745 2007-8-14 0:00: AD No Violations
0767002492 2007-12-03 Annular Disposal No Violations Follow-up inspection of water complaint, tested water from inside Mrs. Gillogys holding tank for water, field test reading was a little over 600ppm, Mrs. Gillogy said they have not been pumping the water, explained that the water would be ok for household use but not drinking. Felt that with the rainy season it would clear up. Told Mrs. Gillogy that I would notify Mr. Kellie and explain that he would not have to have water hauled out but would still need to bring out drinking water until I felt the water would meet EPA standards of 250 ppm. Mr Kellie will remove plastic holding tank from yard and Mr. Gillogy will hook up to his water supply.
1189778435 2007-09-10 Annular Disposal No Violations Follow-up on NOV, and met with Bruce Kellie ( owner ) and Tom Tomastik from Columbus, reviewed well site, tank battery and spring, Tom feels spring should clear up if spring is flushed and clean out more in dike area. Bruce said he will continue to haul fresh water in for Connie Gillogy the landowner. Explained to Mrs. Gillogy that holding tank should be cleaned out and spring should be pumped to allow water to flush through the rock formation.
1276987625 2007-08-15 Annular Disposal No Violations Follow-up on NOV, tanks are emptied and ready to be moved.
1340453482 2007-08-13 Annular Disposal Violations Noted An inspection of the well and tank battery revealed both production tanks leaking brine, it appears the bottoms or the tanks may have holes. There is a water well complaint of brine in drinking water, approx 200ft from there tank battery, this maybe where the brine is coming from. No ID at the well or tank battery. Called company office and left a message about leaking tanks and contaminated water system.
1592392132 2020-6-16 0:00: PW No Violations 1.00
1726879047 2007-12-03 Annular Disposal No Violations Follow-up on NOV, In-Compliance. Done a field test on water with Quantab, the reading was around 250 to 260 ppm. Explained to Mrs. Gillogly that it meets EPA safe drinking standards and the company had complied with NOV. Took water sample from kitchen sink, allowed water to run approx. 45 seconds. Mrs. Gillogy said she was not happy with the companys offer and would be seeking further legal actions and I may be called in as a witness.
1843561595 2020-8-27 0:00: PW No Violations 0.50
1915459745 2007-08-14 Annular Disposal No Violations Spoke with Bruce Kellie about violations and contaminated water system. Bruce said he has emptied tanks and will be removing them from dike to start dirt removal.
767002492 2007-12-3 0:00: AD No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1340453482 US-OH-109803 2007-08-20 Well operation causing pollution and contamination
1340453482 US-OH-109804 2007-08-20 Well not equipped to prevent escape of oil and/or gas
1340453482 US-OH-109805 2007-08-20 Failure to legibly identify well
1340453482 US-OH-109806 2007-08-20 Failure to keep SPCC dike/pit free of brine and other wastes

For data sources see[8]

References