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34-127-23436

Well Details

Well ID: 34-127-23436
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Country: United States
State: Ohio
County: Perry
Municipality: Jackson Township
Operator Name: DAVID R HILL INC
Well Pad ID:
Farm/Lease Name: C E FOLK
License Status: Final Restoration
License Date: 2012-09-10
Spud Date: 1974-10-01
Spud Drilling Contractor:
Final Drill Date: 1974-10-24
Well Total Depth: 2890.00 ft
Configuration: Vertical
Latitude: 39.730000
Longitude: -82.320000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1974-07-23 1056 SOUTHERN TRIANGLE OIL CO GeoDate 7/23/74
Original Spud 1974-10-01 RE-ISS. 7-24-74
Completed 1974-10-24 RE-ISS. 7-24-74
Reached Total Depth 1974-10-24 RE-ISS. 7-24-74
Change of Owner 2012-08-29 Operator changed from 1056, SOUTHERN TRIANGLE OIL CO to 490, HILL DAVID R INC
APP 2012-09-10 Proposed Formations:CLINTON, Issued Date:9/10/2012, Expired Date:9/10/2014 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2013-06-26 RE-ISS. 7-24-74
Record Last Modified 2014-07-25 RE-ISS. 7-24-74
Construction Permit Expires 2014-09-10 RE-ISS. 7-24-74

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 8000 Bbl 0
ACID 0 1000 Gal 0

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2003 DAVID R HILL INC 0.00 0.00 0
2004 DAVID R HILL INC 0.00 0.00 0
2005 DAVID R HILL INC 0.00 0.00 0
2006 DAVID R HILL INC 0.00 0.00 0
2007 DAVID R HILL INC 0.00 0.00 0
2008 DAVID R HILL INC 0.00 0.00 0
2009 DAVID R HILL INC 0.00 0.00 0
2010 DAVID R HILL INC 0.00 0.00 0
2011 DAVID R HILL INC 0.00 0.00 0
2012 DAVID R HILL INC 0.00 0.00 0

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2003 DAVID R HILL INC Brine 0 0
2004 DAVID R HILL INC Brine 0 0
2005 DAVID R HILL INC Brine 0 0
2006 DAVID R HILL INC Brine 0 0
2007 DAVID R HILL INC Brine 0 0
2008 DAVID R HILL INC Brine 0 0
2009 DAVID R HILL INC Brine 0 0
2010 DAVID R HILL INC Brine 0 0
2011 DAVID R HILL INC Brine 0 0
2012 DAVID R HILL INC Brine 0 0

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1065482273 2013-6-25 0:00: PB No Violations 6.00
-1921023061 2003-10-2 0:00: FR No Violations
1023200549 2013-06-26 Plug / Plug Back No Violations Appalachian was on location to run the bonalog down hole to see where the 4 is free at. It showed a free spot at 450ft. We then ran down to 1050ft and shot holes in the 4. The rig crew ran tubing in the well to that point and we set a 350ft plug. They pulled the tubing back out then Appalachian ran in and cut the 4 off at 450ft. The rig crew pulled out the 4 then ran tubing back in the well. They set a 450ft surface plug. The cement stayed at the top of the hole.
1065482273 2013-06-25 Plug / Plug Back No Violations The rig crew is back on location. They are bailing the fluid out of the hole this morning to get in more clay. We got the rest of the clay in the hole then we tried to rip the 4. We ripped it at 1203ft and it was still hung. They pulled up to 65,000lbs on it. It only moved 3 inches. I told the rig crew to shut down for the day and set up Appalachian to come tomorrow to run a bonalog to see where the pipe is free at.
1161616266 2013-10-28 Final Restoration No Violations The final restoration meets 1509.072.
1372428937 2013-06-24 Plug / Plug Back No Violations Berry Well Service was on site to plug this well. They ripped the 4 at 2314ft, 2110ft, and at 1991ft. The 4 is hung in the hole. I had the rig crew wash in another 4 ton of clay to cover the lime. The hole filled up with water so they shut down for the day and are going to bring the baylor with them tomorrow.
1582386188 2013-08-27 Plug / Plug Back Violations Noted The final restoration could not be completed because there is still pipe on the location. I contacted Benny and he said he was just waiting on it to get dry enough to get a skid steerer in there. The tanks have already been removed.
1921023061 2003-10-02 Final Restoration No Violations Final Restoration meets 1509.072(B) requirements.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1582386188 US-OH-115481 2014-04-23 Failure to proceed with due diligence until completed

For data sources see[8]

References