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34-127-23814

Well Details

Well ID: 34-127-23814
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Country: United States
State: Ohio
County: Perry
Municipality: Madison Township
Operator Name: HUFFMAN-BOWERS INC
Well Pad ID:
Farm/Lease Name: JOHNSON THOMAS
License Status: Final Restoration
License Date: 2014-08-26
Spud Date:
Spud Drilling Contractor:
Final Drill Date: 1976-10-03
Well Total Depth: 3221.00 ft
Configuration: Vertical
Latitude: 39.850000
Longitude: -82.200000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1976-08-13 756 MOORE L A & SON INC GeoDate 8/13/76
Oil and Gas 1976-08-13 Issued Date 8/13/76 Expired Date 8/13/77 Acres 0000000 Tool Type Proposed Formation Proposed Depth 00000 Proposed Drill Depth 00000
Completed 1976-10-03
Reached Total Depth 1976-10-03
CO 1993-05-18 756 MOORE L A & SON INC GeoDate 5/18/93
Unknown 1993-05-18 Issued Date 5/18/93 Expired Date 5/18/94 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date
Change of Owner 2001-01-30 Operator changed from 756, MOORE L A & SON INC to 5155, HUFFMAN-BOWERS INC
APP 2014-08-26 Proposed Formations:CLINTON, Issued Date:8/26/2014, Expired Date:8/25/2016 12:00:00 PM, Drilling unit acres:25, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2015-09-17
Construction Permit Expires 2016-08-25
Record Last Modified 2017-02-10

For data sources see[2]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2001 HUFFMAN-BOWERS INC 0.00 0.00 365
2002 HUFFMAN-BOWERS INC 0.00 0.00 365
2003 HUFFMAN-BOWERS INC 0.00 0.00 365
2005 HUFFMAN-BOWERS INC 0.00 0.00 365
2006 HUFFMAN-BOWERS INC 0.00 0.00 365
2007 HUFFMAN-BOWERS INC 0.00 0.00 365
2008 HUFFMAN-BOWERS INC 0.00 0.00 365
2009 HUFFMAN-BOWERS INC 0.00 0.00 365
2010 HUFFMAN-BOWERS INC 0.00 0.00 365
2011 HUFFMAN-BOWERS INC 0.00 0.00 365
2012 HUFFMAN-BOWERS INC 0.00 0.00 366
2013 HUFFMAN-BOWERS INC 0.00 0.00 365
2014 HUFFMAN-BOWERS INC 0.00 0.00 365

For data sources see[3] [4]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2001 HUFFMAN-BOWERS INC Brine 0 365
2002 HUFFMAN-BOWERS INC Brine 0 365
2003 HUFFMAN-BOWERS INC Brine 0 365
2005 HUFFMAN-BOWERS INC Brine 140 365
2006 HUFFMAN-BOWERS INC Brine 0 365
2007 HUFFMAN-BOWERS INC Brine 0 365
2008 HUFFMAN-BOWERS INC Brine 0 365
2009 HUFFMAN-BOWERS INC Brine 0 365
2010 HUFFMAN-BOWERS INC Brine 0 365
2011 HUFFMAN-BOWERS INC Brine 0 365
2012 HUFFMAN-BOWERS INC Brine 0 366
2013 HUFFMAN-BOWERS INC Brine 0 365
2014 HUFFMAN-BOWERS INC Brine 0 365

For data sources see[5] [6]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1320385477 2015-6-30 0:00: PW No Violations 1.00
-1500637249 2014-8-4 0:00:0 PW No Violations 1.00
-1657585688 2015-9-10 0:00: PB No Violations 1.50
-1678722996 2014-4-23 0:00: PW No Violations
-1704201780 2014-6-2 0:00:0 PW No Violations 1.00
-486304082 2008-2-8 0:00:0 PW No Violations
-562985426 2015-9-14 0:00: PB No Violations 6.50
-679861707 2015-9-16 0:00: PB No Violations 3.00
0486304082 2008-02-08 Production Wells Violations Noted An inspection of the well revealed no ID at the well or tank battery, no dike around production tanks.
0562985426 2015-09-14 Plug / Plug Back No Violations I witnessed the bottom hole plug and the big lime plug today for county inspector Justin Smith. Both plus were sat through upset tubing. They could only get to about 2635 feet so they had to sit the bottom hole plug there. They pulled 13 joints of tubing and sat the big Lime plug.
0612236447 2015-10-13 Final Restoration No Violations The final restoration meets 1509.072B.
0679861707 2015-09-16 Plug / Plug Back No Violations I was on location today to finish plugging this well. The tubing was ran back in the well to 200ft. The rig crew was able to recover 65ft of 8. The 8 was ate off at that point. We topped the well off with a 200ft cement plug. The cement stayed at the surface. The well is now plugged.
0831549186 2013-12-13 Production Wells Violations Noted This well has 4.5 casing in it, with a swage on top. There is no wellhead. The well is not hooked up and the valve is shut on the 4. All pipes at the well are disconnected. The well will need to be put back in production within 90days or plugging is required within 180days.
1040312855 2015-09-14 Administrative Inspection No Violations I called inspector Justin Smith and gave him an update on todays events.
1207582158 2008-04-04 Production Wells No Violations Follow-up on NOV, In-Compliance.
1320385477 2015-06-30 Production Wells No Violations The well has not been plugged yet but it is the next well on Barrys list to do. He will be on the well in the next 2 weeks.
1441890019 2015-09-09 Plug / Plug Back No Violations Barry Bowers has moved his service rig on this well to plug it. They are currently drilling out inside the casing with tubing. They are at 1605ft at this point. Once the hole is cleaned up the bottom plug will be set with cement.
1442516633 2015-09-15 Plug / Plug Back No Violations I was on location to witness the plugging of this well. The 4.5 was ripped at 1580ft. The casing was pulled from the well and the tubing was ran back in to set the Berea plug and the Bottom of the Surface plug. The tubing was then pulled back out of the well so they could work on the 8.
1500637249 2014-08-04 Production Wells No Violations Barry Bowers moved his rig in on this well to see if he could get it back into production. When I showed up at the well the rig was already gone. I contacted Barry to see what his game plan was. He said they were unable to swab the fluid off of the well so he plans on plugging the well. He sent in for the plugging permit and will plug the well once we get the permit.
1657585688 2015-09-10 Plug / Plug Back No Violations I stopped by to see how the drilling was coming along. They have made it down to 2050ft. The rig crew plans to keep drilling the rest of the day.
1678722996 2014-04-23 Production Wells No Violations Barry Bowers is applying for a plug permit for this well. He will be plugging the well this summer.
1704201780 2014-06-02 Production Wells No Violations I met with Barry Bowers about the status of this well. Barry said he plans on moving a rig in on this well to service it and put it back in production if it has a show of production. If not he plans on plugging this well. He has a couple of plug jobs to do before he can move in on this well. I told him that would be fine.
612236447 2015-10-13 0:00 FR No Violations 1.00
831549186 2013-12-13 0:00 PW No Violations 1.00

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0486304082 US-OH-125330 2008-02-08 General Safety
0486304082 US-OH-125331 2008-02-08 Failure to legibly identify well
0486304082 US-OH-125332 2008-02-08 No SPCC dike/or failure to keep dike free of water or oil
0831549186 US-OH-129471 2015-09-15 Nonproduction; well shall be plugged or placed in temporary inactive status

For data sources see[7]

References