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Well ID: 34-127-25106 | Loading map...
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Country: United States | |
State: Ohio | |
County: Perry | |
Municipality: Pleasant Township | |
Operator Name: LUOIL INC | |
Well Pad ID: | |
Farm/Lease Name: GEORGE CARR | |
License Status: Final Restoration | |
License Date: 2012-12-13 | |
Spud Date: 1981-05-08 | |
Spud Drilling Contractor: | |
Final Drill Date: 1981-05-11 | |
Well Total Depth: 3811.00 ft | |
Configuration: Vertical | |
Latitude: 39.640000 | |
Longitude: -82.130000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1981-02-11 | 3110 APPALACHIAN WELL SUPPLY GeoDate 2/11/81 |
Original Spud | 1981-05-08 | |
Completed | 1981-05-11 | |
Reached Total Depth | 1981-05-11 | |
CO | 1991-12-09 | 37 HOPCO RESOURCES INC GeoDate 2/11/81 |
CO | 1993-08-26 | 4074 OIL ENTERPRISES GeoDate 2/11/81 |
Change of Owner | 2003-10-24 | Operator changed from 4243, NUTTCO OIL & GAS to 1429, ALTIER BROTHERS INC |
Change of Owner | 2010-06-29 | Operator changed from 1429, ALTIER BROTHERS INC to 8073, LUOIL INC |
APP | 2012-12-13 | Proposed Formations:CLINTON, Issued Date:12/13/2012, Expired Date:12/13/2014 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:HAD, Proposed Well Class: |
Plugged/Abandoned | 2014-05-23 | |
Construction Permit Expires | 2014-12-13 | |
Record Last Modified | 2017-02-17 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 3692 | 3694 | 2 |
2006-09-11 | 3682 | 3688 | 6 |
3682 | 3688 | 6 | |
3682 | 3688 | 6 | |
2006-09-11 | 3720 | 3724 | 4 |
2006-09-11 | 3708 | 3712 | 2 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1200 Bbl | 70000 | VERSI GEL |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | DORAN & ASSOCIATES | 8948.00 | 707.00 | 365 |
1985 | DORAN & ASSOCIATES | 1868.00 | 287.00 | 334 |
1986 | DORAN & ASSOCIATES | 2338.00 | 73.00 | 252 |
1987 | DORAN & ASSOCIATES | 2392.00 | 219.00 | 360 |
1988 | DORAN & ASSOCIATES | 257.00 | 0.00 | 158 |
1993 | OIL ENTERPRISES | 460.00 | 429.00 | 365 |
1994 | OIL ENTERPRISES | 1247.00 | 544.00 | 365 |
1995 | OIL ENTERPRISES | 1627.00 | 633.00 | 365 |
1996 | OIL ENTERPRISES | 428.00 | 592.00 | 365 |
1997 | OIL ENTERPRISES | 27.00 | 64.00 | 120 |
2002 | NUTTCO OIL & GAS | 0.00 | 80.00 | 100 |
2008 | LUOIL INC | 0.00 | 60.00 | 30 |
2009 | LUOIL INC | 0.00 | 0.00 | 120 |
2010 | LUOIL INC | 0.00 | 93.00 | 365 |
2011 | LUOIL INC | 0.00 | 382.00 | 156 |
2012 | LUOIL INC | 0.00 | 72.00 | 82 |
2014 | LUOIL INC | 0.00 | 30.00 | 60 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | DORAN & ASSOCIATES | Brine | 0 | 365 |
1985 | DORAN & ASSOCIATES | Brine | 370 | 334 |
1986 | DORAN & ASSOCIATES | Brine | 295 | 252 |
1987 | DORAN & ASSOCIATES | Brine | 144 | 360 |
1988 | DORAN & ASSOCIATES | Brine | 0 | 158 |
1993 | OIL ENTERPRISES | Brine | 0 | 365 |
1994 | OIL ENTERPRISES | Brine | 0 | 365 |
1995 | OIL ENTERPRISES | Brine | 0 | 365 |
1996 | OIL ENTERPRISES | Brine | 0 | 365 |
1997 | OIL ENTERPRISES | Brine | 40 | 120 |
2002 | NUTTCO OIL & GAS | Brine | 80 | 100 |
2008 | LUOIL INC | Brine | 0 | 30 |
2009 | LUOIL INC | Brine | 0 | 120 |
2010 | LUOIL INC | Brine | 20 | 365 |
2011 | LUOIL INC | Brine | 70 | 156 |
2012 | LUOIL INC | Brine | 0 | 82 |
2014 | LUOIL INC | Brine | 0 | 60 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1036813837 | 2012-5-9 0:00:0 | AD | No Violations | |
-1085352271 | 2008-1-17 0:00: | AD | No Violations | |
-1125606560 | 2003-7-3 0:00:0 | PW | No Violations | |
-115787152 | 2014-5-19 0:00: | PB | No Violations | 2.00 |
-1481731840 | 2014-6-24 0:00: | FR | No Violations | 1.00 |
-1525643703 | 2008-6-18 0:00: | AD | No Violations | |
-1555025372 | 2014-5-20 0:00: | PB | No Violations | 9.00 |
-1620696296 | 2014-4-23 0:00: | PB | No Violations | 1.00 |
-1716628027 | 2014-5-9 0:00:0 | PB | No Violations | 3.00 |
-387705600 | 2014-1-10 0:00: | AM | No Violations | 1.00 |
-422937070 | 2012-10-25 0:00 | PW | No Violations | 3.00 |
-51113566 | 2014-5-8 0:00:0 | PB | No Violations | 1.50 |
-537926223 | 2014-5-20 0:00: | PB | No Violations | 9.00 |
-554018911 | 2013-10-15 0:00 | PW | No Violations | 1.00 |
-904965296 | 2014-3-28 0:00: | PW | No Violations | 1.00 |
-954035420 | 2003-11-3 0:00: | PW | No Violations | |
0051113566 | 2014-05-08 | Plug / Plug Back | No Violations | I stopped by the well site to check on the rig crew. They rigged up today and are working on getting the rods out of the well. They are not pulling the tubing out today. |
0115787152 | 2014-05-19 | Plug / Plug Back | No Violations | I stopped by this well today to check on the rig crew. They are setting up to plug the well tomorrow. The cement company will be there at 7:30am. I will be onsite to witness the plugging of this well. |
0243713989 | 2014-03-04 | Production Wells | No Violations | I talked with Benny Altier to remind him that this well will need plugged. He told me he still plans on plugging the well. We are going to meet there at the beginning of next week to see if we can talk with the land owner. He has had the gates locked into the well. |
0316991206 | 2014-05-23 | Plug / Plug Back | No Violations | I returned to the well to finish plugging it. The rig crew made up their tools to run in the well. They went in to tag the cement plug with them. The tools set down at 220ft. We had the cement company come out and fill the hole with cement to surface. The plug stayed at the surface. |
0387705600 | 2014-01-10 | Administrative Inspection | No Violations | I stopped at the Altier Brothers to talk with Benny Altier about his well. I asked him when is he planning on plugging this well. He said he is going to try and get it back into production. If he can not, he will apply for a plugging permit for the well. |
0422937070 | 2012-10-25 | Production Wells | Violations Noted | FOLLOW UP TO NOV # 1351191586 I received a call from Attorney Nicolas Grilli, he has informed me the lease for this well has been forfeited back to Dan Brown. This well shall be plugged, the lease has been forfeited, back to Danny B Brown 11. Affidavit of forfeiture ORC 5301.332 Recorded 04/20/2012 at 8:06 AM at the Perry county recorders office. The well consists of pumping unit,100 barrel tank, this well shall meet the restoration requirements of 1509.072. Failure to comply may result in a forfeiture of Bond. |
0451714587 | 2014-04-09 | Administrative Inspection | No Violations | I talked with Benny Altier about moving the rig in on location. Tomorrow we are going to bring in a sullivant truck to put down the well. Then the rig will be moved in on the location at the beginning of next week to service plug the well. |
0537926223 | 2014-05-20 | Plug / Plug Back | No Violations | I am onsite today to witness the plugging of this well. We set the bottom plug then had Appalachian come out to shoot the 4. When Appalachian shot the 4, the pipe jumped and broke the rig slips and elevators. The 4 fell down the hole 5ft. After Appalachian got there wire line back out of the hole, Altiers tried to get screwed onto the 4 with a pull sub. They were not able to screw onto the pipe because the 4 was bent and the top. The 8 was preventing them from being able to get ahold of the 4. We shut down for the day. Altiers is going to bring in there trackhoe out to dig down around the well. We are going to cut the 8 off at 5 so we can hook onto the 4. |
0554018911 | 2013-10-15 | Production Wells | No Violations | I did a follow-up inspection on this well for a previous inspection by Kip Thompson. The well is supposed to be plugged, LUOIL lost the lease for this ground. I contacted Benny Altier to see what is the situation on this well. He is in Italy right now but he told me they are planning on plugging the well. The land owner locked the gates up to the well and they can not get to the well. When he gets back we are going to meet and go out to the well. I told him this well needs plugged right away because they lost the lease to the ground. |
0565716967 | 2016-12-29 | Final Restoration | No Violations | Final restoration meets 1509.072 (B) requirements. |
0904965296 | 2014-03-28 | Production Wells | No Violations | I met with Benny Altier to discuss the plugging of this well. I told him as soon as it is dry we need to move in there. The land owner does not want us in there when it is wet. Benny agreed with me and said when I tell him it is dry enough to move a rig in on the well he would. |
0954035420 | 2003-11-03 | Production Wells | No Violations | All work completed as ordered. ( RESOLVED. ) |
1036813837 | 2012-05-09 | Annular Disposal | No Violations | Follow-up on Compliance Notice, In-Compliance. |
1057610260 | 2003-07-03 | Production Wells | Violations Noted | Immediately repair slice in plastic gas line. Remove brine from tank dike, repair damaged area and identify well by 7/29/03. |
1085352271 | 2008-01-17 | Annular Disposal | Violations Noted | A complaint was received on Monday, January 14, 2008 from Mr. Dan Brown( landowner). An inspection of the well revealed lease road will need graded and water break put in on hill, old kill area on well site needs cleaned up, oily material around well head and dike around tank battery needs rebuilt and drain installed. Stop venting gas into the air. |
1125606560 | 2003-07-03 | Production Wells | Violations Noted | FOLLOW UP TO NOV # 1057610260 Immediately repair slice in plastic gas line. Remove brine from tank dike, repair damaged area and identify well by 7/29/03. |
1299924583 | 2008-05-06 | Annular Disposal | No Violations | Follow-up on NOV, Non-Compliance, no action to comply with NOV. |
1329830646 | 2012-02-13 | Annular Disposal | Violations Noted | The inspection revealed ID on tank battery has wrong owner name and ER name. Venting gas at well head. Need full and complete ID at well head or tank battery, stop venting gas into air, company may flare. Spoke to Benny Altier about violations and he stated he will correct violations. |
1351191586 | 2012-10-25 | Production Wells | Violations Noted | I received a call from Attorney Nicolas Grilli, he has informed me the lease for this well has been forfeited back to Dan Brown. This well shall be plugged, the lease has been forfeited, back to Danny B Brown 11. Affidavit of forfeiture ORC 5301.332 Recorded 04/20/2012 at 8:06 AM at the Perry county recorders office. The well consists of pumping unit,100 barrel tank, this well shall meet the restoration requirements of 1509.072. Failure to comply may result in a forfeiture of Bond. |
1393527671 | 2013-03-21 | Production Wells | Violations Noted | FOLLOW UP TO NOV # 1903912468 I received a call from Dan Brown concerning when Luoil would plug this well. I have called Lewis altier to inform him he has 30 days to plug this well. The well shall be plugged within 30 days, failure to do so may result in forfeiture of bond. |
1397559505 | 2014-04-14 | Production Wells | No Violations | I met Benny Altier at this well to let him on the property so they could put sullivant down the well. The land owner does not want the company on the property without someone there. They will be moving the service rig onto the well this week to start plugging it. |
1401187993 | 2014-05-22 | Plug / Plug Back | No Violations | I returned to this well to finish plugging this well. Altiers had Formation Cementing onsite to set the plugs while they pulled out the 4. The surface plug did not stay at the surface. We shut down for the day to let the cement set up. We will tag the plug tomorrow to see where the plug is at then fill to surface with cement |
1401394246 | 2014-05-29 | Plug / Plug Back | No Violations | I stopped by this well today to check on the reclamation of the well pad. Benny Altier wanted me to stop and look at it so the landowner didnt complain. I told him it looked good and I would stop back in a few weeks to make sure the seed grows. |
1481731840 | 2014-06-24 | Final Restoration | No Violations | Final restoration meets 1509.072. |
1525643703 | 2008-06-18 | Annular Disposal | No Violations | Follow-up on NOV, In-Compliance. |
1534904664 | 2014-03-18 | Production Wells | No Violations | I was able to get ahold of the land owner for this well. I told him I am working on getting Benny Altier to plug the well. I told him I needed the new code for the lock so we could get in there when it is time to plug it. He gave me the code and told me he wanted them to plug it when it is dry so they dont ruin his field. |
1555025372 | 2014-05-20 | Plug / Plug Back | No Violations | Accompanied Inspector Justin Smith to witness plugging activities at this well location. Witnessed Formation Cementing bullhead down a 400 bottom plug using 35 sks of 2% gel cement. Appalachian Well Surveys then ran a bond log to find free pipe. Free pipe was found at approximately 2650 and the 4.5 casing was shot off at 2648. When the 4.5 was shot off, it jumped in the hole due to significant stretch being pulled on it by the rig. This jump caused damage to the slips and the elevators, which resulted in the 4.5 casing being dropped approximately 6 down-hole. Altier Brothers attempted to thread back onto the 4.5 casing with a sub, but were unable to do so due to the casing being bent from the fall. Altier Brothers will dig down and cut off the 8.625 approximately 6 down to get to the bent 4.5 casing to retrieve it and continue the plug job. |
1620696296 | 2014-04-23 | Plug / Plug Back | No Violations | Benny Altier has moved his rig in on this well. The rig is parked on location at this time. It is not rigged up right now and there is no one at the jobsite. Benny wanted to get the rig in while the ground was dry. They plan on plugging the well this week. |
1716628027 | 2014-05-09 | Plug / Plug Back | No Violations | I was out at the well today while the rig crew pulled tubing. They are going to set the bottom plug next week. They do not have a time as of right now. |
1903912468 | 2013-03-21 | Production Wells | Violations Noted | I received a call from Dan Brown concerning when Luoil would plug this well. I have called Lewis altier to inform him he has 30 days to plug this well. The well shall be plugged within 30 days, failure to do so may result in forfeiture of bond. |
1908015965 | 2014-03-11 | Production Wells | No Violations | I went out to this well with Benny Altier. The well is supposed to get plugged because they lost there lease. We were unable to get the gates open that go to the well. The codes have been changed on the locks. We climbed over the gates so we could get back to the well and inspect it. I told Benny to see if he could find the land owners phone number so we could contact him and let him know that we need to get on the property to plug the well. He is supposed to look find the number and get back with me. |
243713989 | 2014-3-4 0:00:0 | PW | No Violations | 1.00 |
316991206 | 2014-5-23 0:00: | PB | No Violations | 7.50 |
451714587 | 2014-4-9 0:00:0 | AM | No Violations | 1.00 |
565716967 | 2016-12-29 0:00 | FR | No Violations | 1.00 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0422937070 | US-OH-124503 | 2014-05-21 | Failure to legibly identify well | |
0422937070 | US-OH-124504 | 2014-05-21 | Nonproduction; well shall be plugged or placed in temporary inactive status | |
1057610260 | US-OH-101078 | 2003-07-08 | Well insufficiently equipped to prevent escape of oil and gas | |
1057610260 | US-OH-101079 | 2003-07-07 | Failure to legibly identify well | |
1085352271 | US-OH-101948 | 2008-01-17 | Well operation causing pollution and contamination | |
1085352271 | US-OH-101949 | 2008-01-17 | Well not equipped to prevent escape of oil and/or gas | |
1085352271 | US-OH-101950 | 2008-01-17 | Equipment pressure rated below operating pressure | |
1085352271 | US-OH-101951 | 2008-01-17 | No SPCC dike/or failure to keep dike free of water or oil | |
1085352271 | US-OH-101952 | 2008-01-17 | Unlawful venting or flaring of gas | |
1125606560 | US-OH-103174 | 2003-07-08 | Well insufficiently equipped to prevent escape of oil and gas | |
1125606560 | US-OH-103175 | 2003-07-07 | Failure to legibly identify well | |
1329830646 | US-OH-109435 | 2012-02-21 | Failure to legibly identify well | |
1329830646 | US-OH-109436 | 2012-02-21 | Unlawful venting or flaring of gas | |
1351191586 | US-OH-110170 | 2018-03-05 | 9-1-03C | Forfeiture of bond |
1351191586 | US-OH-110171 | 2018-03-05 | NONE | Well shall be plugged |
1393527671 | US-OH-111636 | 2014-05-21 | Well shall be plugged | |
1903912468 | US-OH-119136 | 2013-03-21 | Forfeiture of bond | |
1903912468 | US-OH-119137 | 2013-03-21 | Well shall be plugged | |
1903912468 | US-OH-119138 | 2013-03-21 | Nonproduction; well shall be plugged or placed in temporary inactive status |
For data sources see[9]