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34-127-25218

Well Details

Well ID: 34-127-25218
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Country: United States
State: Ohio
County: Perry
Municipality: Madison Township
Operator Name: R C POLING CO INC
Well Pad ID:
Farm/Lease Name: SANDS WALTER
License Status: Final Restoration
License Date: 2015-03-30
Spud Date: 1981-09-09
Spud Drilling Contractor:
Final Drill Date: 1981-10-10
Well Total Depth: 0.00 ft
Configuration: Vertical
Latitude: 39.850000
Longitude: -82.170000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1981-09-09 PLUG STAUS CHANGED PER PLUG REPORT
Completed 1981-10-10 PLUG STAUS CHANGED PER PLUG REPORT
Reached Total Depth 1981-10-10 PLUG STAUS CHANGED PER PLUG REPORT
CO 1981-12-07 236 POLING R C CO INC GeoDate 12/7/81
Oil and Gas 1981-12-07 Issued Date 12/7/81 Expired Date 12/7/82 Acres 0000000 Tool Type NT Proposed Formation Proposed Depth 00000 Proposed Drill Depth 00000
APP 2013-01-31 Proposed Formations:CLINTON, Issued Date:1/31/2013, Expired Date:1/31/2015 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:
APP 2015-03-30 Proposed Formations:CLINTON, Issued Date:3/30/2015, Expired Date:3/29/2017 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2016-08-20 PLUG STAUS CHANGED PER PLUG REPORT
Construction Permit Expires 2017-03-29 PLUG STAUS CHANGED PER PLUG REPORT
Record Last Modified 2017-08-12 PLUG STAUS CHANGED PER PLUG REPORT

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 2100 Bbl 30000

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 R C POLING CO INC 679.00 208.00 365
1986 R C POLING CO INC 0.00 69.00 365
1987 R C POLING CO INC 0.00 59.00 365
1988 R C POLING CO INC 0.00 0.00 0
1989 R C POLING CO INC 0.00 0.00 365
1991 R C POLING CO INC 0.00 69.00 365
2007 R C POLING CO INC 0.00 0.00 365
2008 R C POLING CO INC 0.00 0.00 365
2009 R C POLING CO INC 0.00 0.00 365
2010 R C POLING CO INC 0.00 83.00 365
2011 R C POLING CO INC 0.00 30.00 365
2012 R C POLING CO INC 0.00 0.00 366
2013 R C POLING CO INC 0.00 0.00 365
2014 R C POLING CO INC 0.00 0.00 365
2015 R C POLING CO INC 0.00 24.00 365
2016 R C POLING CO INC 0.00 0.00 227

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 R C POLING CO INC Brine 0 365
1986 R C POLING CO INC Brine 5 365
1987 R C POLING CO INC Brine 0 365
1988 R C POLING CO INC Brine 0 0
1989 R C POLING CO INC Brine 0 365
1991 R C POLING CO INC Brine 0 365
2007 R C POLING CO INC Brine 0 365
2008 R C POLING CO INC Brine 0 365
2009 R C POLING CO INC Brine 0 365
2010 R C POLING CO INC Brine 120 365
2011 R C POLING CO INC Brine 70 365
2012 R C POLING CO INC Brine 0 366
2013 R C POLING CO INC Brine 40 365
2014 R C POLING CO INC Brine 0 365
2015 R C POLING CO INC Brine 0 365
2016 R C POLING CO INC Brine 40 227

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1299785193 2012-4-19 0:00: PW No Violations
-1525068722 2016-8-22 0:00: PB No Violations 5.00
-2132124326 2016-8-24 0:00: PW No Violations 2.00
-262703374 2017-8-10 0:00: FR No Violations 0.50
-44568688 2016-6-23 0:00: PW No Violations 1.00
0000016676 Preliminary Restoration No Violations PASSED Y WITNESSED 10/5/92 INSPECTOR MIKE HOUSEHOLDER DATE 10/0519/92 DATA FROM OLD VAX INFO
0044568688 2016-06-23 Production Wells No Violations I was on location to do a field inspection on this well. Mr. Poling is planning on plugging this well this summer.
0072358749 2016-08-23 Plug / Plug Back No Violations I returned to this well today to witness the plugging of this well. The rig crew has bailed the hole down to 450 feet. We set a bride plug at this point and filled the well the rest of the way with concrete. The clay was up to 600 feet before it started bridging off. The cement is now up to the surface. I will return in the morning to make sure the plug did not settle.
0262703374 2017-08-10 Final Restoration No Violations The final restoration meets 1509.072(B).
0698251644 2013-01-08 Production Wells No Violations I did a general inspection on this well to check the status on it. The valves are open on the well to the tank pad. The well is capable of production. I looked up the production report on this well and zero production was reported in 2012. Mr. Poling has already applied for the plugging permit for this well as of 01/31/2013. I will contact Mr. Poling to see when he plans on plugging the well.
0724088275 2016-11-01 Plug / Plug Back No Violations I returned to this well today to see if I could do the final restoration on it. When I arrived on location Zack Poling was on location removing all of the production line and production equipment. I will return to this well in a month to check on the progress of it.
1161774118 2016-08-12 Plug / Plug Back No Violations I returned to this well today to witness the plugging of this well. Today Mark Hines had his rig crew on location to wash in the bottom plug using plugging clay from Logan Clay. After the bottom plug was set the rig crew loaded the hole with fresh water before they ran there 4.5 inch ripping tools to rip the 4.5 inch diameter casing.
1299785193 2012-04-19 Production Wells No Violations On the day of my inspection I found a pumping unit at the well site, the well could be capable of production, there is no permit number posted at the well site, there is (1) one hundred barrel production tank setting inside a containment dike, there is no permit number posted at the tank.
1471006937 2016-08-10 Plug / Plug Back No Violations I stopped by the well today to see how the operations were going on getting this well plugged. Today Mark Hines has his rig crew on location pulling out the rods and tubing from the well. They are planning on putting in plugging clay in the next couple of days.
1471349161 2016-08-16 Plug / Plug Back No Violations I was back on location today to witness the plugging of this well. The rig crew were able to rip the 4.5 inch diameter casing at 2980 feet. After pulling the pipe up to make sure it was free the rig crew setup to set the Lime plug using plugging clay from Logan Clay.
1471445054 2016-08-17 Plug / Plug Back No Violations I returned to this well today to witness the plugging activities for this well. Today the rig crew set a brush and stone bridge plug at 1035 feet. That is 50 feet below the bottom of the Berea Formation. From this point they washed in a couple more tons of plugging clay before they worked on retrieving the 7 inch diameter casing that is in the hole. According to the plugging permit the 7 inch casing had been pulled but it is still in the well. The rig crew worked on retrieving the 7 inch casing from the well. They were able to find free pipe at 610 feet.
1471869601 2016-08-19 Plug / Plug Back No Violations I was back on location today to witness the plugging activities of this well. The plugging clay has bridged off around 60 feet down hole. The bridge is around 50 feet long from running the tools through it. The rig crew is working on getting the hole cleaned back up and washing the bridge out before putting anymore clay down hole.
1525068722 2016-08-22 Plug / Plug Back No Violations I returned to this well today to witness more plugging of this well. We ran the tools down hole first thing this morning to make sure the hole was still cleaned up. Today we will be putting more plugging clay in the well and checking to make sure it does not bridge up hole again. After trying to get the clay down the hole and it bridging off we have decided to bail the hole out and set a brush and stone plug then fill the hole with concrete.
16676 PL No Violations
2132124326 2016-08-24 Production Wells No Violations I returned to this well today to check to see if the plug had stayed at the surface. The plug had dropped 20 feet down hole so the rig crew topped it off with clay. The well is now plugged.
698251644 2013-1-8 0:00:0 PW No Violations 1.00
72358749 2016-8-23 0:00: PB No Violations 4.00
724088275 2016-11-1 0:00: PB No Violations

For data sources see[8]

References