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34-127-25784

Well Details

Well ID: 34-127-25784
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Country: United States
State: Ohio
County: Perry
Municipality: Pleasant Township
Operator Name: STONEBRIDGE OPERATING CO LLC
Well Pad ID:
Farm/Lease Name: CAVINEE & FURNEY
License Status: Producing
License Date: 1998-09-01
Spud Date: 1982-12-20
Spud Drilling Contractor: BEVERLY DRLG
Final Drill Date: 1982-12-28
Well Total Depth: 3891.00 ft
Configuration: Vertical
Latitude: 39.650000
Longitude: -82.110000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1982-11-24 631 BT ENERGY CORP GeoDate 11/24/82
Oil and Gas 1982-11-24 Issued Date 11/24/82 Expired Date 5/23/83 Acres 0020000 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 03891 Proposed Drill Depth 03891
Original Spud 1982-12-20
Completed 1982-12-28
Reached Total Depth 1982-12-28
Completion Report Received 1983-02-17
APP 1998-09-01 Proposed Formations:CLINTON, Issued Date:9/1/98, Expired Date:9/1/99 6:00:00 AM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:
Construction Permit Expires 1999-09-01
Change of Owner 2007-10-12 Operator changed from 631, BT ENERGY CORP to 2070, STONEBRIDGE OPERATING CO
Last Compliance Report 2017-03-17
Record Last Modified 2017-03-17

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 3723 3766 0
3723 3766 0
2006-09-11 3724 3757 2
3724 3757 2
3723 3766 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 800 Bbl 60000 FRAC: 800 BBL H2O, 60M SAND

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 BT ENERGY CORP 11171.00 0.00 365
1985 BT ENERGY CORP 3871.00 0.00 365
1986 PARTNERS OIL CO 1913.00 0.00 0
1987 BT ENERGY CORP 4732.00 0.00 365
1988 BT ENERGY CORP 4662.00 0.00 365
1990 BT ENERGY CORP 638.00 0.00 365
1991 BT ENERGY CORP 505.00 0.00 365
1998 STONEBRIDGE OPERATING CO LLC 0.00 0.00 0
2000 STONEBRIDGE OPERATING CO LLC 0.00 0.00 0
2012 STONEBRIDGE OPERATING CO LLC 0.00 0.00 0
2014 STONEBRIDGE OPERATING CO LLC 0.00 0.00 0
2015 STONEBRIDGE OPERATING CO LLC 0.00 0.00 0
2016 STONEBRIDGE OPERATING CO LLC 0.00 0.00 0
2017 STONEBRIDGE OPERATING CO LLC 0.00 0.00 0
2018 STONEBRIDGE OPERATING CO LLC 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 BT ENERGY CORP Brine 0 365
1985 BT ENERGY CORP Brine 60 365
1986 PARTNERS OIL CO Brine 0 0
1987 BT ENERGY CORP Brine 533 365
1988 BT ENERGY CORP Brine 0 365
1990 BT ENERGY CORP Brine 120 365
1991 BT ENERGY CORP Brine 0 365
1998 STONEBRIDGE OPERATING CO LLC Brine 0 0
2000 STONEBRIDGE OPERATING CO LLC Brine 0 0
2012 STONEBRIDGE OPERATING CO LLC Brine 0 0
2014 STONEBRIDGE OPERATING CO LLC Brine 0 0
2015 STONEBRIDGE OPERATING CO LLC Brine 0 0
2016 STONEBRIDGE OPERATING CO LLC Brine 0 0
2017 STONEBRIDGE OPERATING CO LLC Brine 0 0
2018 STONEBRIDGE OPERATING CO LLC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1550361049 2018-8-6 0:00:0 PW No Violations 0.50
-1805046090 2014-3-20 0:00: PW No Violations 1.00
-1897181967 2015-6-10 0:00: PW No Violations 1.00
-70964932 2012-3-28 0:00: AD No Violations
0000PL7023 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
001280i174 2002-06-07 Annular Disposal No Violations A.D. Not Being Used.
0051271179 2015-09-28 Production Wells No Violations I returned to this well to do a follow-up inspection on it. The company has set a new production tank and all new flow lines to the well. The well was serviced and has been re-plumbed with a new stuffing box and fittings coming off of the well. The pumping unit still needs a motor put on it and a new gas meter has to be set. I contacted Keith from Stonebridge and he said it should be done soon. He would relay the message for me.
0070964932 2012-03-28 Annular Disposal No Violations On the day of my inspection I found a pumping unit at the well site, the well could be capable of production, there is no permit posted at the well site, the annular on the eight inch is not exposed, there are (2) one hundred barrel production tanks/ knock out/ seperator/ drip/ chart setting inside a containment dike, there is no permit number posted at the well site.
0126565133 2019-01-22 Production Wells No Violations I was on location today to do a field inspection on the well. This well appears to be capable of production at this time. The well has a pumping unit on it with rods and 1.5 inch diameter tubing in it. The valves are open from the wellhead to the tank pad. The identification for this well is located at the production tank. There is 1-100 barrel production tank in the tank pad. There are no violations at this time.
0280617501 2007-01-11 Annular Disposal No Violations Checked AD hook up for Columbus, AD not in use.
1015079808 2015-07-22 Production Wells No Violations I was at this well to do a follow-up inspection on it. There is a service rig on the well at this time. The rig crew was not there during my inspection on the well. I did a walk around and found they have taken the old production tanks out of the dike. I contacted Keith the pumper from Stonebridge and he said they are replacing the tanks. They had Keith Matheney pull out the rods and tubing to service the well. They ran the tubing and rods back in the well and should have everything done by the end of the week.
1042165315 2019-12-26 0:00 PW No Violations 0.50
126565133 2019-1-22 0:00: PW No Violations 0.50
1267167085 2014-12-08 Production Wells No Violations I returned to this well to do a follow-up inspection on it. The well is currently being used by the land owner for domestic gas but the well is still not capable of commercial production. A compliance notice was issued on 3/5/2014 for the being idle and incapable of commercial production. The violation has not been resolved at this time. This is an informal letter to inform you that if the violation is not resolved a Chiefs Order may be issued on the well. If there are any questions about the violations please feel free to contact me. Thanks.
1280i174 2002-6-7 0:00:0 AD No Violations
1283828559 2016-01-05 Production Wells No Violations I returned to this well to do a follow-up inspection on it. The well is still currently in violation. All of the valves are shut at the well making it incapable of production or incapable of providing house gas to the land owner. The pumping unit is still missing a motor to operate it and there is still no sales meter at the tank pad.
1296408559 2014-03-05 Production Wells Violations Noted This well is incapable of production. There is no motor on the pumping unit to run the well, the valves are shut in at the wellhead, the flow line is not hooked up to the production tanks. This well will need to be plugged within 180days.
1350782810 2016-03-24 Production Wells No Violations I returned to this well after receiving a phone call from Keith the pumper letting me know the well was back in production. I went out to do a field inspection on it. The pumping unit now has a motor on it and the well appears to be in operation. All of the valves are open from the well to the production tank. There are no violations at this time.
1500878217 2015-12-22 Production Wells No Violations I returned to this well to do a follow-up inspection on it. The well still is not capable of production. The valves are all shut and the sales meter has not been set yet. The well is still in violation.
1550361049 2018-08-06 Production Wells No Violations I was on location today to do a field inspection on the well. This well appears to be capable of production at this time. The well has a pumping unit on it with rods and 1.5 inch diameter tubing in it. The valves are open from the wellhead to the tank pad. The identification for this well is located at the production tank. There is 1-100 barrel production tank in the tank pad. There are no violations at this time.
1792677816 2017-02-02 Temporary Abandoned Annular Disposal No Violations I was on location today to check the annular disposal for Columbus. The annular disposal is not hooked up at this time.
1805046090 2014-03-20 Production Wells No Violations I stopped by this well today to take some pictures of the well. The well is still idle and not capable of production. The flow line is not connected at the wellhead. There is no motor on the pumping unit to operate it. The production tanks are full of holes. The gas meter in the tank pad is not hooked up and has no gas chart for sales.
1897181967 2015-06-10 Production Wells No Violations I talked with Keith the pumper from Stonebridge and he told me they apparently still own this well so they will be bringing in a service rig this summer to service the well.
1960593426 2016-12-29 Production Wells No Violations I was on location today to do a field inspection on the well. This well appears to be capable of production at this time. The well has a pumping unit on it with rods and tubing in it. The valves are open from the wellhead to the tank pad. The identification for this well is located at the production tank and the well. There is 1-100 barrel production tank in the tank pad. There are no violations at this time.
280617501 2007-1-11 0:00: AD No Violations
51271179 2015-9-28 0:00: PW No Violations 1.00
PL7023 PL No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1296408559 US-OH-108331 2016-08-01 Failure to legibly identify well
1296408559 US-OH-108332 2016-08-01 Well shall be plugged

For data sources see[9]

References