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34-127-25787

Well Details

Well ID: 34-127-25787
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Country: United States
State: Ohio
County: Perry
Municipality: Hopewell Township
Operator Name: R C POLING CO INC
Well Pad ID:
Farm/Lease Name: SATTERFIELD RALPH
License Status: Final Restoration
License Date: 2013-06-21
Spud Date: 1982-12-21
Spud Drilling Contractor: SNIDER BROS. DRLG
Final Drill Date: 1983-01-16
Well Total Depth: 3016.00 ft
Configuration: Vertical
Latitude: 39.830000
Longitude: -82.280000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1982-11-26 Issued Date 11/26/82 Expired Date 5/25/83 Acres 0164000 Tool Type CT Proposed Formation CLINTON Proposed Depth 03016 Proposed Drill Depth 03016
Original Spud 1982-12-21
Completed 1983-01-16
Reached Total Depth 1983-01-16
CO 1983-01-29 286 McKEE DON DRILL CO INC GeoDate 11/26/82
Completion Report Received 1983-02-04
Change of Owner 2002-11-12 Operator changed from 286, McKEE DON DRILL CO INC to 236, POLING R C CO INC
APP 2013-06-21 Proposed Formations:CLINTON, Issued Date:6/21/2013, Expired Date:6/21/2015 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:HAD, Proposed Well Class:
Plugged/Abandoned 2013-10-28
Construction Permit Expires 2015-06-21
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 2980 3011 0
2980 3011 0
2980 3011 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1850 Bbl 40000 FRAC;1850BBL H2O,40M# SAND,100G ACID

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 McKEE DON DRILL CO INC 1637.00 670.00 0
1985 McKEE DON DRILL CO INC 1257.00 407.00 365
1986 McKEE DON DRILL CO INC 1016.00 290.00 365
1987 McKEE DON DRILL CO INC 740.00 227.00 365
1988 McKEE DON DRILL CO INC 1198.00 582.00 365
1990 McKEE DON DRILL CO INC 719.00 295.00 365
1991 McKEE DON DRILL CO INC 650.00 350.00 365
1992 McKEE DON DRILL CO INC 639.00 332.00 365
1993 McKEE DON DRILL CO INC 573.00 305.00 365
1994 McKEE DON DRILL CO INC 372.00 207.00 365
1995 McKEE DON DRILL CO INC 321.00 170.00 365
1997 McKEE DON DRILL CO INC 213.00 108.00 365
1998 McKEE DON DRILL CO INC 192.00 177.00 365
1999 McKEE DON DRILL CO INC 230.00 190.00 365
2000 McKEE DON DRILL CO INC 111.00 134.00 365
2001 McKEE DON DRILL CO INC 90.00 181.00 365
2002 McKEE DON DRILL CO INC 0.00 130.00 303
2003 R C POLING CO INC 0.00 478.00 365
2004 R C POLING CO INC 0.00 409.00 365
2005 R C POLING CO INC 0.00 538.00 365
2006 R C POLING CO INC 0.00 318.00 365
2007 R C POLING CO INC 0.00 81.00 365
2009 R C POLING CO INC 0.00 54.00 365
2013 R C POLING CO INC 0.00 50.00 365
2014 R C POLING CO INC 0.00 45.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 McKEE DON DRILL CO INC Brine 0 0
1985 McKEE DON DRILL CO INC Brine 16 365
1986 McKEE DON DRILL CO INC Brine 16 365
1987 McKEE DON DRILL CO INC Brine 0 365
1988 McKEE DON DRILL CO INC Brine 0 365
1990 McKEE DON DRILL CO INC Brine 0 365
1991 McKEE DON DRILL CO INC Brine 0 365
1992 McKEE DON DRILL CO INC Brine 0 365
1993 McKEE DON DRILL CO INC Brine 42 365
1994 McKEE DON DRILL CO INC Brine 28 365
1995 McKEE DON DRILL CO INC Brine 0 365
1997 McKEE DON DRILL CO INC Brine 0 365
1998 McKEE DON DRILL CO INC Brine 0 365
1999 McKEE DON DRILL CO INC Brine 0 365
2000 McKEE DON DRILL CO INC Brine 0 365
2001 McKEE DON DRILL CO INC Brine 0 365
2002 McKEE DON DRILL CO INC Brine 0 303
2003 R C POLING CO INC Brine 345 365
2004 R C POLING CO INC Brine 490 365
2005 R C POLING CO INC Brine 700 365
2006 R C POLING CO INC Brine 840 365
2007 R C POLING CO INC Brine 25 365
2009 R C POLING CO INC Brine 113 365
2013 R C POLING CO INC Brine 43 365
2014 R C POLING CO INC Brine 45 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1353274263 2013-9-17 0:00: PB No Violations 5.00
-1408997236 2008-11-4 0:00: AD No Violations
-769084951 2013-9-23 0:00: PB No Violations 3.00
0000PL7021 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0159461301 2013-10-31 Final Restoration No Violations The final restoration meets 1509.072.
0238111031 2013-10-30 Plug / Plug Back No Violations The clay is at the surface on this plug job. I let Zack Poling know they could cut the well down and put the plate on. They are able to start reclaiming.
0677525123 2013-09-16 Plug / Plug Back No Violations Kenny Wright has moved rig in on location to plug well. They are pulling out rods and tubing today.
0769084951 2013-09-23 Plug / Plug Back No Violations Kenny Wright had his crew back on location to wash in more plugging clay for the surface plug. They washed the clay up to the surface and stopped for the day. They are going to let the plug settle and top the well off again.
1353274263 2013-09-17 Plug / Plug Back No Violations Kenny Wright was on location to plug well. They washed in 500ft of plugging clay for the bottom plug. The 5 was ripped at 2534ft. The rig crew then washed in another 500ft of plugging clay. They then started pulling out the rest of the 5.
1382103623 2013-10-17 Plug / Plug Back No Violations I stopped to check on this well. The clay was still not at the top of the hole. They are out of plugging clay at the site. I contacted Zack Poling and let him know that they would have to get more clay and top the well off.
1408997236 2008-11-04 Annular Disposal No Violations No violations.
159461301 2013-10-31 0:00 FR No Violations 1.00
1732097593 2003-01-03 Production Wells No Violations
2120393846 2013-09-19 Plug / Plug Back No Violations Kenny Wright was on location to plug well. They finished pulling out the 5. They ran in the 7 pre-cast plug to 970ft. The rig crew washed in plugging clay up to the bottom of the 8. They were able to retrieve 114ft of the 8. They will wash in more clay to surface.
238111031 2013-10-30 0:00 PB No Violations 1.50
677525123 2013-9-16 0:00: PB No Violations 2.00
PL7021 PL No Violations

For data sources see[9]

References

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