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Well ID: 34-127-25986 | Loading map...
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Country: United States | |
State: Ohio | |
County: Perry | |
Municipality: Pike Township | |
Operator Name: FINCK OIL & GAS CO | |
Well Pad ID: | |
Farm/Lease Name: STARNER A | |
License Status: Final Restoration | |
License Date: 2016-09-12 | |
Spud Date: 1983-06-16 | |
Spud Drilling Contractor: BILL FINCK DRLG | |
Final Drill Date: 1983-08-14 | |
Well Total Depth: 3450.00 ft | |
Configuration: Vertical | |
Latitude: 39.670000 | |
Longitude: -82.200000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1983-06-06 | Issued Date 6/6/83 Expired Date 12/3/83 Acres 0020000 Tool Type CT Proposed Formation CLINTON Proposed Depth 03450 Proposed Drill Depth 03450 |
Original Spud | 1983-06-16 | GMM UPDATED PLUG STATUS PER PLUG REPORT |
Completed | 1983-08-14 | GMM UPDATED PLUG STATUS PER PLUG REPORT |
Reached Total Depth | 1983-08-14 | GMM UPDATED PLUG STATUS PER PLUG REPORT |
CO | 1983-08-26 | 58 FINCK OIL & GAS CO GeoDate 6/6/83 |
Completion Report Received | 1983-09-09 | GMM UPDATED PLUG STATUS PER PLUG REPORT |
APP | 2016-09-12 | Proposed Formations:CLINTON SANDSTONE, Issued Date:9/12/2016, Expired Date:9/12/2018 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:HAD, Proposed Well Class: |
Plugged/Abandoned | 2018-07-28 | GMM UPDATED PLUG STATUS PER PLUG REPORT |
Construction Permit Expires | 2018-09-12 | GMM UPDATED PLUG STATUS PER PLUG REPORT |
Record Last Modified | 2019-04-23 | GMM UPDATED PLUG STATUS PER PLUG REPORT |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 3410 | 3440 | 28 |
3410 | 3440 | 28 | |
3410 | 3440 | 28 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 2000 Bbl | 30000 | FRAC : WATER & SAND |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | FINCK OIL & GAS CO | 0.00 | 1238.00 | 0 |
1985 | FINCK OIL & GAS CO | 0.00 | 708.00 | 0 |
2006 | FINCK OIL & GAS CO | 0.00 | 0.00 | 30 |
2007 | FINCK OIL & GAS CO | 0.00 | 301.00 | 365 |
2008 | FINCK OIL & GAS CO | 0.00 | 278.00 | 365 |
2009 | FINCK EXP & DEVELOP CO | 0.00 | 150.00 | 365 |
2010 | FINCK OIL & GAS CO | 0.00 | 0.00 | 0 |
2011 | FINCK OIL & GAS CO | 0.00 | 0.00 | 0 |
2012 | FINCK OIL & GAS CO | 0.00 | 154.00 | 150 |
2013 | FINCK OIL & GAS CO | 0.00 | 0.00 | 0 |
2014 | FINCK OIL & GAS CO | 0.00 | 0.00 | 0 |
2015 | FINCK OIL & GAS CO | 0.00 | 0.00 | 0 |
2016 | FINCK OIL & GAS CO | 0.00 | 0.00 | 0 |
2017 | FINCK OIL & GAS CO | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | FINCK OIL & GAS CO | Brine | 195 | 0 |
1985 | FINCK OIL & GAS CO | Brine | 150 | 0 |
2006 | FINCK OIL & GAS CO | Brine | 0 | 30 |
2007 | FINCK OIL & GAS CO | Brine | 300 | 365 |
2008 | FINCK OIL & GAS CO | Brine | 285 | 365 |
2009 | FINCK EXP & DEVELOP CO | Brine | 75 | 365 |
2010 | FINCK OIL & GAS CO | Brine | 0 | 0 |
2011 | FINCK OIL & GAS CO | Brine | 0 | 0 |
2012 | FINCK OIL & GAS CO | Brine | 80 | 150 |
2013 | FINCK OIL & GAS CO | Brine | 0 | 0 |
2014 | FINCK OIL & GAS CO | Brine | 0 | 0 |
2015 | FINCK OIL & GAS CO | Brine | 0 | 0 |
2016 | FINCK OIL & GAS CO | Brine | 0 | 0 |
2017 | FINCK OIL & GAS CO | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-109718638 | 2017-10-10 0:00 | PW | No Violations | 1.00 |
-2077224595 | 2019-2-15 0:00: | FR | No Violations | 0.50 |
-2142700484 | 2018-12-7 0:00: | FR | No Violations | 1.00 |
0000PL6923 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0109718638 | 2017-10-10 | Production Wells | Violations Noted | I was on location to do a field inspection of this well. During the inspection of this well I found the well is not in production and is incapable of production with all the valves on the wellhead shut in. The motor has been removed from the pumping unit making the pumping unit incapable of operation. No production has been reported on this well since 2012. The well owner/operator shall submit a written plugging schedule to (Justin Smith) at (5880 Memory Road Zanesville, Ohio 43701) within 30 days, per OAC 1501:9-11-05(B), and plug the well within 180 days. The well owner/operator will be notified if the plugging schedule is approved or denied. I called the company today at 12:45 pm and talked with Jim Finck. He did notify me that he has already applied for the plugging permit and it has been issued. He has been in contact with Linn Bell about plugging the well. |
0409394441 | 2018-05-16 | Production Wells | No Violations | I was back on location today to do a follow-up inspection on this well for being idle and incapable of production. At this time there has been no change in the status of this well. The well is still sitting here idle and incapable of production. I talked with Jim Finck today and he has been in contact with Kenny Wright to plug the well. I will be talking with Kenny to see when he can get here to do it. I was able to get ahold of Kenny today and he is planning on having the well plugged by the end of July. |
1405868882 | 2018-02-22 | Production Wells | No Violations | I was back on location today to do a follow-up inspection on this well. The well is still currently sitting idle and incapable of production. The well does have a plugging permit issued for it and the owner of the well has talked with Linn Bell about plugging the well. I called Linn to see if he was planning on the well. Linn told me that he was not going to plug it and that Finck Oil and Gas would have to find someone else. I called Jim Finck to let him know he would have to find someone else to plug the well. Jim asked me for some other plugging companies so I gave him 3 contacts. Jim will contact me back when he has a company lined up to plug the well. |
1532359260 | 2018-07-23 | Plug / Plug Back | No Violations | Kenny Wright has moved his plugging rig in on this well today to plug it. Today the rig crew is working on getting the rods and tubing out of the well. If they are able to get the rods and tubing out of the well they will wash in the bottom plug tomorrow with plugging clay. |
1532443191 | 2018-07-24 | Plug / Plug Back | No Violations | I was on location today to witness the plugging of this well. Today the rig crew washed in 500 feet of plugging clay from Belden Brick Company. They loaded the hole full of water after this so they can rip the 4.5 inch diameter casing. |
1767297649 | 2019-04-09 | Final Restoration | No Violations | I was on location today to do a final restoration on this well today. The final restoration meets 1509.072(B). |
1909200437 | 2018-07-26 | Plug / Plug Back | No Violations | I was back on location today to witness the plugging of this well. Yesterday I was unable to make to the location because I had a monthly meeting at the Zanesville office. Kenny informed me that they ran the pre-cast plug down to 1170 feet. From here they started to wash in plugging clay. The clay will fill the hole from the 1170 feet to the surface. I was on location today to witness some of the clay being washed in the hole but we ran out of clay. They will have to get another load of clay to finish plugging this well. |
1956597421 | 2018-07-30 | Plug / Plug Back | No Violations | I was on location today to check to see if the plugging clay had settled at all. The clay was still at the surface. It did not settle at all over the weekend. I will let the company know that they can start the reclaiming on this location. |
2077224595 | 2019-02-15 | Final Restoration | Violations Noted | I was back on location today to do the final restoration on this well. I was unable to complete the final restoration because the production equipment is still down on location and there is plastic pipe located where the production tanks were. You have 6 months to complete the final restoration once the plugging is finished. The plugging on this well was completed on 7/30/2018. The equipment will need to be removed and the reclaiming will need to be done before I can finish the final restoration. I will make a phone call to the company. |
2142700484 | 2018-12-07 | Final Restoration | No Violations | I was back on location today to do the final restoration. At this time I can not pass the final restoration because the production equipment is still down at the well site. The production tanks have been removed from the lease road. I will check back after 1/30/2019 to see if it has been completed. |
409394441 | 2018-5-16 0:00: | PW | No Violations | |
PL6923 | PL | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0109718638 | US-OH-102322 | 2019-04-16 | NONE | Well shall be plugged |
2077224595 | US-OH-121200 | 2019-04-16 | NONE3 | Failure to complete final restoration within six months |
2077224595 | US-OH-121201 | 2019-04-16 | NONEA | Failure to remove production equip. within 6 mos. REPLACE |
2077224595 | US-OH-121202 | 2019-04-16 | NONEB | Failure to restore land surface within 6 months (CHANGE) |
For data sources see[9]