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34-127-26815

Well Details

Well ID: 34-127-26815
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Country: United States
State: Ohio
County: Perry
Municipality: Reading Township
Operator Name: NGO DEVELOPMENT CORP.
Well Pad ID:
Farm/Lease Name: SWINEHART
License Status: Final Restoration
License Date: 2017-08-24
Spud Date: 1987-08-19
Spud Drilling Contractor: LEES DRLG
Final Drill Date: 1987-10-07
Well Total Depth: 2746.00 ft
Configuration: Vertical
Latitude: 39.830000
Longitude: -82.380000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1987-08-19
Completed 1987-10-07
Reached Total Depth 1987-10-07
Completion Report Received 1987-10-10
CO 1987-10-14 1111 MERIDIAN ENERGY COMPANY GeoDate 6/1/87
CO 1993-01-26 424 NATIONAL PRODUCTION CORP GeoDate 6/1/87
CO 1996-03-04 98 NGO DEVELOPMENT CORP. GeoDate 6/1/87
APP 2017-08-24 Proposed Formations:CLINTON, Issued Date:8/24/2017, Expired Date:8/24/2019 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2017-11-20
Record Last Modified 2018-04-16
Construction Permit Expires 2019-08-24

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 2702 2728 0
2702 2728 0
2702 2728 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
ACID 15 100 0 FRAC W/74M GAL H20 & 300 SX SAND
H2O 0 74000 Gal 30000 1/4 GAL. HAI 60, 17 GAL. LO SURF 300, 17 GAL. CLA-STA B, BD @ 1250 PSI, TREATING PRESS @ 1700 PSI, INJUCTION RATE 30 BPM, ISIP @ 900 PSI;

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1987 MERIDIAN ENERGY COMPANY 2888.00 60.00 78
1988 MERIDIAN ENERGY COMPANY 24273.00 657.00 365
1993 NGO DEVELOPMENT CORP. 6724.00 0.00 365
1994 NGO DEVELOPMENT CORP. 10893.00 73.00 365
1995 NGO DEVELOPMENT CORP. 0.00 0.00 365
1996 NGO DEVELOPMENT CORP. 9989.00 0.00 365
1997 NGO DEVELOPMENT CORP. 7470.00 0.00 365
1998 NGO DEVELOPMENT CORP. 7655.00 0.00 365
1999 NGO DEVELOPMENT CORP. 9217.00 79.00 365
2000 NGO DEVELOPMENT CORP. 7129.00 0.00 0
2001 NGO DEVELOPMENT CORP. 7908.00 30.00 365
2002 NGO DEVELOPMENT CORP. 5136.00 0.00 365
2003 NGO DEVELOPMENT CORP. 5328.00 0.00 365
2004 NGO DEVELOPMENT CORP. 5095.00 0.00 365
2005 NGO DEVELOPMENT CORP. 4170.00 42.00 365
2006 NGO DEVELOPMENT CORP. 4288.00 0.00 365
2007 NGO DEVELOPMENT CORP. 3715.00 64.00 365
2008 NGO DEVELOPMENT CORP. 1370.00 0.00 365
2009 NGO DEVELOPMENT CORP. 2481.00 0.00 365
2010 NGO DEVELOPMENT CORP. 2620.00 0.00 365
2011 NGO DEVELOPMENT CORP. 2779.00 0.00 365
2012 NGO DEVELOPMENT CORP. 518.00 0.00 366
2013 NGO DEVELOPMENT CORP. 0.00 0.00 365
2014 NGO DEVELOPMENT CORP. 0.00 0.00 365
2015 NGO DEVELOPMENT CORP. 0.00 0.00 365
2016 NGO DEVELOPMENT CORP. 0.00 0.00 365
2017 NGO DEVELOPMENT CORP. 0.00 0.00 324

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1987 MERIDIAN ENERGY COMPANY Brine 6 78
1988 MERIDIAN ENERGY COMPANY Brine 10 365
1993 NGO DEVELOPMENT CORP. Brine 0 365
1994 NGO DEVELOPMENT CORP. Brine 30 365
1995 NGO DEVELOPMENT CORP. Brine 0 365
1996 NGO DEVELOPMENT CORP. Brine 0 365
1997 NGO DEVELOPMENT CORP. Brine 0 365
1998 NGO DEVELOPMENT CORP. Brine 30 365
1999 NGO DEVELOPMENT CORP. Brine 56 365
2000 NGO DEVELOPMENT CORP. Brine 0
2001 NGO DEVELOPMENT CORP. Brine 10 365
2002 NGO DEVELOPMENT CORP. Brine 0 365
2003 NGO DEVELOPMENT CORP. Brine 0 365
2004 NGO DEVELOPMENT CORP. Brine 0 365
2005 NGO DEVELOPMENT CORP. Brine 30 365
2006 NGO DEVELOPMENT CORP. Brine 35 365
2007 NGO DEVELOPMENT CORP. Brine 0 365
2008 NGO DEVELOPMENT CORP. Brine 0 365
2009 NGO DEVELOPMENT CORP. Brine 0 365
2010 NGO DEVELOPMENT CORP. Brine 0 365
2011 NGO DEVELOPMENT CORP. Brine 45 365
2012 NGO DEVELOPMENT CORP. Brine 0 366
2013 NGO DEVELOPMENT CORP. Brine 0 365
2014 NGO DEVELOPMENT CORP. Brine 0 365
2015 NGO DEVELOPMENT CORP. Brine 0 365
2016 NGO DEVELOPMENT CORP. Brine 0 365
2017 NGO DEVELOPMENT CORP. Brine 0 324

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1315474089 2013-5-23 0:00: PW No Violations 1.00
-1495587272 2017-11-17 0:00 PB No Violations
-1988627978 2008-3-25 0:00: AD No Violations
-453355738 2017-11-20 0:00 PB No Violations 2.00
-580194375 2019-11-7 0:00: FR No Violations 0.50
-761112021 2013-9-11 0:00: PW No Violations 1.00
-821404144 2017-11-21 0:00 PB No Violations 1.00
0000PL6504 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0453355738 2017-11-20 Plug / Plug Back No Violations I was back on location today to witness the plugging of this well. The rig crew tagged the surface plug at 65 feet today. We tried to top the well off with Class A cement but it kept settling back down the hole. The company has decided to let the cement setup again and come back in to top it off.
0761112021 2013-09-11 Production Wells No Violations The identification has been fixed on the well. The well is now in compliance.
0821404144 2017-11-21 Plug / Plug Back No Violations I returned to this well today to witness the plugging of this well. Today the rig crew topped the well off with bagged quickrete to the surface. The cement stayed at the surface and did not settle. The well is now plugged.
1293709189 2018-12-31 Final Restoration No Violations I returned to this well today to do the follow-up inspection on it. There is still some production equipment located at the tank pad. I will make a call to the company to see if they will be removing it.
1315474089 2013-05-23 Production Wells Violations Noted This well is capable of production. It has rods and 1.5 tubing in it. There is no identification at the well. I called NGO to let them no about the issue.
1495587272 2017-11-17 Plug / Plug Back No Violations I was back on location today to witness the plugging of this well. After ripping the 4.5 inch casing at 1856 feet the rig crew pulled the 4.5 inch casing from the well. The rig crew then tried to run the tubing back in the well but the hole had caved in. They were only able to get down to 900 feet. The hole was caving in as they were pulling the casing from the well. We had to set extra cement for the next plug.
1510665823 2017-11-14 Plug / Plug Back No Violations Knox Energy has moved their service rig in on this well to plug it. The rig crew has already removed the rods from the well and are now working on getting the rest of the 1.5 inch diameter tubing out of the well and the 2-7/8 inch diameter tubing from the well. They are planning on setting the bottom plug tomorrow.
1510752608 2017-11-15 Plug / Plug Back No Violations I was on location today to witness the bottom plug being set on this well. The bottom plug was set through 2-7/8 inch diameter tubing. A 30 sack Class A cement plug was set for the bottom plug and then the 2-7/8 inch tubing was removed from the well so the rig crew could work on retrieving the 4.5 inch casing.
1988627978 2008-03-25 Annular Disposal No Violations No violations.
2083941624 2018-02-01 Final Restoration No Violations I was on location today to do a final restoration on this well. I was unable to complete it at this time because there is still a separator left on the property. I contacted Bill Mitton and he told me he would be finishing up everything on them soon and would call me to let me know it was done.
PL6504 PL No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1315474089 US-OH-108985 2014-04-23 Failure to legibly identify well

For data sources see[9]

References

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