If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.
powered by ChangeDetection
Well ID: 34-127-27237 | ![]() Sorry, we have no imagery here. Sorry, we have no imagery here. Sorry, we have no imagery here. ![]() |
Country: United States | |
State: Ohio | |
County: Perry | |
Municipality: Hopewell Township | |
Operator Name: HOUGHTON INVESTMENTS LLC | |
Well Pad ID: | |
Farm/Lease Name: BORNTREGER-HANN UNIT | |
License Status: Dry and Abandoned | |
License Date: 2001-01-09 | |
Spud Date: 2001-01-13 | |
Spud Drilling Contractor: PROFESSIONAL WELL SVC-PWS | |
Final Drill Date: 2001-04-27 | |
Well Total Depth: 4820.00 ft | |
Configuration: Vertical | |
Latitude: 39.900000 | |
Longitude: -82.300000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2001-01-09 | 6227 HOUGHTON INVESTMENTS, L.L.C. Proposed Formation ROSE RUN (MAY NOT PRODUCE CLINTON) Issued Date 1/9/01 Expired Date 1/9/02 6:00:00 AM |
Original Spud | 2001-01-13 | RBDMS Rec |
Completed | 2001-04-27 | RBDMS Rec |
Reached Total Depth | 2001-04-27 | RBDMS Rec |
Plugged/Abandoned | 2001-05-07 | RBDMS Rec |
Completion Report Received | 2001-10-18 | RBDMS Rec |
Construction Permit Expires | 2002-01-09 | RBDMS Rec |
Record Last Modified | 2015-09-24 | RBDMS Rec |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
Not Treated | 0 | 0 | 0 | SWABBED FM THROUGH 5 1/2 CASING & RECOVERED 200 BBL SALT WATER & ESTIMATED 10 MCF/DAY GAS…PLUG & ABANDON |
For data sources see[3]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
1343795108 | 2003-06-17 | Preliminary Restoration | No Violations |
For data sources see[4]