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34-129-20244

Well Details

Well ID: 34-129-20244
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Country: United States
State: Ohio
County: Pickaway
Municipality: Jackson Township
Operator Name: MARKSMEN ENERGY USA INC
Well Pad ID:
Farm/Lease Name: Bj-78
License Status: Producing
License Date: 2014-06-03
Spud Date: 2014-06-09
Spud Drilling Contractor: G & L DRILLING
Final Drill Date: 2014-06-15
Well Total Depth: 2580.00 ft
Configuration: Vertical
Latitude: 39.610000
Longitude: -83.030000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2014-06-03 Proposed Formations:TRENTON, BLACK RIVER, TREMPEALEAU, Issued Date:6/3/2014, Expired Date:6/2/2016 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:POOL
Reached Total Depth 2014-06-15
Completion Report Received 2014-08-11
Construction Permit Expires 2016-06-02
Change of Owner 2017-01-04 Operator changed from 6227, HOUGHTON INVESTMENTS LLC to 9491, MARKSMEN ENERGY USA INC
Record Last Modified 2019-06-11

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2014-08-11 2452 2456 13
2452 2456 13
2452 2456 13

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
2014-06-19 ACID 15 400 Gal 0 Producers Service Corporation

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2014 HOUGHTON INVESTMENTS LLC 0.00 26.00 168
2015 HOUGHTON INVESTMENTS LLC 0.00 33.00 168
2016 HOUGHTON INVESTMENTS LLC 0.00 0.00 168
2017 MARKSMEN ENERGY USA INC 0.00 0.00 0
2018 MARKSMEN ENERGY USA INC 0.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2014 HOUGHTON INVESTMENTS LLC Brine 8701 168
2015 HOUGHTON INVESTMENTS LLC Brine 15 168
2016 HOUGHTON INVESTMENTS LLC Brine 125 168
2017 MARKSMEN ENERGY USA INC Brine 0 0
2018 MARKSMEN ENERGY USA INC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1281031933 2014-6-11 0:00: CS No Violations 6.50
-751542629 2014-9-25 0:00: PL No Violations
0751542629 2014-09-25 Preliminary Restoration No Violations - Inspection, ID on tank

- Pump unit on well, tubing and rods on pipe rack at well location - All drilling equipment removed from the location, pits filled and the area has been graded. - Dike area free of debris, two 210 barrel tanks in dike area -

1151983496 2014-06-12 Casing String Witnessed No Violations This is a continuation report of the cementing the surface casing to surface on this well. The 7 is cemented to surface. Formation and the rig crew set up to do a pressure test on the well. We were unsuccessful on the pressure test. The pressure head that formation had was leaking. We has to let the cement set up and pressure test it later. We pressure tested the well at 650lbs for 30 min. The test passed with a 1lb decline. The drilling crew is getting ready to starting drilling again at this point.
1281031933 2014-06-11 Casing String Witnessed No Violations I was at this well to witness the surface casing being cemented to surface. I covered this job for Mike Mitchell. There was 633ft of 7 ran in the hole. Formation cementing came out to do the cement job. The job went good. The cement circulated to surface.
1402418727 2014-06-10 Drill / Deepen / Reopen No Violations G&L Drilling on site with rig number 3. They have set the conductor today. They are drilling on fluid. Light rain today.

For data sources see[9]

References