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34-131-20090

Well Details

Well ID: 34-131-20090
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Country: United States
State: Ohio
County: Pike
Municipality: Marion Township
Operator Name: KNOX ENERGY INC.
Well Pad ID:
Farm/Lease Name: BROWN J
License Status: Final Restoration
License Date: 2011-12-05
Spud Date: 2007-11-05
Spud Drilling Contractor: BOWMAN DRILLING
Final Drill Date: 2007-11-07
Well Total Depth: 1135.00 ft
Configuration: Vertical
Latitude: 38.950000
Longitude: -82.810000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2007-09-05 Proposed Formations:OHIO SHALE, Issued Date:9/5/2007, Expired Date:9/4/2008 6:00:00 AM, Drilling unit acres:10, Proposed Well Type:OG, Proposed Well Class:POOL
Completed 2007-11-07
Reached Total Depth 2007-11-07
Completion Report Received 2008-01-24
APP 2008-03-06 8228 PAXTON MADISON LLC Proposed Formation BEREA Issued Date 3/6/2008 Expired Date 3/6/2009 6:00:00 AM
Plugged Back 2008-04-02
Change of Owner 2009-09-01 Operator changed from 8228, PAXTON MADISON LLC to 6295, KNOX ENERGY INC.
APP 2010-07-01 Proposed Formations:OHIO SHALE, Issued Date:7/1/2010, Expired Date:7/1/2011 6:00:00 AM, Drilling unit acres:10, Proposed Well Type:OG, Proposed Well Class:
APP 2011-12-05 Proposed Formations:CLINTON, Issued Date:12/5/2011, Expired Date:12/4/2013 12:00:00 PM, Drilling unit acres:10, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2013-05-17
Construction Permit Expires 2013-12-04
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2008-03-24 813 818 20
2008-03-24 716 722 24
674 680 24
716 722 24
972 977 20
813 818 20
1028 1033 20
1057 1062 20
674 680 24
2008-03-24 674 680 24
2008-03-24 1057 1062 20
2008-03-24 1028 1033 20
2008-03-24 972 977 20

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
N2 0 13 Mscf 14800 STAGE 2 OF 4
N2 8 22 Mscf 39800 STAGE 4 OF 4
N2 8 48 Mscf 17800 STAGE 1 OF 4
N2 8 12 Mscf 14200 STAGE 3 OF 4

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2009 PAXTON MADISON LLC 0.00 0.00 0
2010 KNOX ENERGY INC. 0.00 0.00 0
2012 KNOX ENERGY INC. 0.00 0.00 0
2013 KNOX ENERGY INC. 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2009 PAXTON MADISON LLC Brine 0 0
2010 KNOX ENERGY INC. Brine 0 0
2012 KNOX ENERGY INC. Brine 0 0
2013 KNOX ENERGY INC. Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1967388369 2008-1-11 0:00: PW No Violations
-702156576 2010-3-8 0:00:0 AM No Violations
-715455708 2016-2-15 0:00: FR No Violations 3.50
0477175250 2007-11-06 Drill / Deepen / Reopen No Violations Called out for surface cement job. Arrived on site they were running the 85/8 in the hole. They cross threaded the 6th and 7th joints collar and then tightened it. When they released the slips they lost 6 joints down the hole. Surface job was cancled.
0702156576 2010-03-08 Administrative Inspection No Violations Received call from Bill Mitton. 3:20pm Re: will get identification on wells this week. Will attempt to produce and work with the well this spring. Will be bringing a rig down. If not successful will plug the well while rig is in area.
0715455708 2016-02-15 Final Restoration No Violations I walked to the location of the GPS coordinates and found that they were in a field that has been used for farming of crops. At this time I passed the final restoration of this location in accordance with 1509.072
1045331078 2008-06-05 Preliminary Restoration No Violations Well site has been reclaimed and pits filled in. Land is now being used for agriculture. Production equipment has been installed. Well needs identification.
1368805676 2013-05-17 Plug / Plug Back No Violations Witnessed plugging operations. Packer removed from well and bottom plug spotted through tubing from 1122-338. Top of surface plug set from 102-0.
1369229796 2013-05-16 Plug / Plug Back No Violations Attended the pre plug prep for its eventual plugging the next day (Friday, 05-17-2013). Operator contacted me this morning that they were mobilizing today to start the plugging process on this well. The plugging of this well was delayed originally because the landowner was contemplating taking over ownership of this well. Operator showed up on location with service rig and a truck with flatbed trailer containing a small dozer. When I showed up on location they were removing the production tubing and submersible pump out of the well and getting rigged up to push the bridge plug down hole that was installed between the current producing zone, Berea, and the lower and original producing zone, the Ohio Shale. After pounding on the plug for an hour, the plug released and traveled with gas, water and the apparatus that was used to pound the plug open to the surface. Water and gas shot above the crown sheaves on the service mast. What was considered a bridge plug was in fact a retrievable plug. The company vented gas after they remounted the wellhead. Gas pressure started to ebb and they shut-in the well at approximately 1640 hours. They secured their equipment and left the site.
1370609212 2013-05-31 Final Restoration No Violations Contacted the landowners where this site was located concerning restoration after plugging the well. I talked to Mr. and Mrs. Howard (Shirley) Childers and asked them if they had any concerns about the restoration that Knox Energy performed at the well site. Mr. Child indicated to me that he had no problems with the present condition of the site. He had already plowed and planted soy beans in the area where the well was located. I went to the site to verify the conditions. It appears that the surface where the well was located is in good shape and there was no remnants of a well in the field, or any activity related to the plugging. All material was removed and pit was dewatered and filled in. I asked Knox Energy to submit a waiver form to the landowner for their approval of the restoration since this was not a typical reclamation situation. This field will continue to be used for farming crops on this location.
1967388369 2008-01-11 Production Wells No Violations Production equipment has been installed. Electric service is in place and operating. Electric lines are either on poles or buried in conduit. Whole operation looks good. Well is not connected to production lines yet. They are in a testing phase right now.
2066541035 2007-11-07 Drill / Deepen / Reopen No Violations They recovered all 6 joints of 85/8 that had been dropped. Spud date 11-5-07. TD 618 42 conductor. Ran 600 of 85/8 and cemented to surface. Good circulation and cement returns to the surface. Cement did drop back after pump stopped. They are going to grout it in during the production cement job.
477175250 2007-11-6 0:00: DD No Violations

For data sources see[9]

References