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Well ID: 34-133-21306 | Loading map...
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Country: United States | |
State: Ohio | |
County: Portage | |
Municipality: Ravenna Township | |
Operator Name: EQUITY OIL & GAS FUNDS INC | |
Well Pad ID: | |
Farm/Lease Name: ENLOW | |
License Status: Plugged and Abandoned | |
License Date: 2004-05-06 | |
Spud Date: 1978-05-18 | |
Spud Drilling Contractor: | |
Final Drill Date: 1978-07-07 | |
Well Total Depth: 4470.00 ft | |
Configuration: Vertical | |
Latitude: 41.180000 | |
Longitude: -81.210000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1977-12-23 | 317 INLAND DRILLING CO INC GeoDate 12/23/77 |
Original Spud | 1978-05-18 | R.L. 5-3-78 |
Completed | 1978-07-07 | R.L. 5-3-78 |
Reached Total Depth | 1978-07-07 | R.L. 5-3-78 |
CO | 1992-09-16 | 3877 POG HOLDINGS CO INC GeoDate 12/23/77 |
CO | 1995-07-17 | 1171 EQUITY OIL & GAS FUNDS IN GeoDate 12/23/77 |
APP | 2001-08-17 | Proposed Formations:CLINTON, Issued Date:8/17/2001, Expired Date:8/17/2002 6:00:00 AM, Drilling unit acres:48.55, Proposed Well Type:OG, Proposed Well Class: |
APP | 2004-05-06 | Proposed Formations:CLINTON, Issued Date:5/6/2004, Expired Date:5/6/2005 6:00:00 AM, Drilling unit acres:48.55, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2004-07-15 | R.L. 5-3-78 |
Construction Permit Expires | 2005-05-06 | R.L. 5-3-78 |
Record Last Modified | 2013-03-14 | R.L. 5-3-78 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 4310 | 4372 | 24 |
4310 | 4372 | 24 | |
4310 | 4372 | 24 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 69000 Gal | 150000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1985 | INLAND DRILLING CO INC | 5028.00 | 773.00 | 365 |
1986 | INLAND DRILLING CO INC | 4284.00 | 377.00 | 365 |
1987 | INLAND DRILLING CO INC | 1525.00 | 0.00 | 245 |
1988 | INLAND DRILLING CO INC | 1978.00 | 457.00 | 112 |
1989 | INLAND DRILLING CO INC | 4383.00 | 664.00 | 300 |
1990 | INLAND DRILLING CO INC | 3413.00 | 571.00 | 365 |
1991 | INLAND DRILLING CO INC | 5699.00 | 464.00 | 365 |
1992 | INLAND DRILLING CO INC | 3883.00 | 192.00 | 275 |
1993 | POG HOLDINGS CO INC | 4319.00 | 193.00 | 365 |
1995 | EQUITY OIL & GAS FUNDS INC | 1117.00 | 74.00 | 214 |
1996 | EQUITY OIL & GAS FUNDS INC | 1361.00 | 226.00 | 365 |
1997 | EQUITY OIL & GAS FUNDS INC | 2146.00 | 157.00 | 365 |
1998 | EQUITY OIL & GAS FUNDS INC | 1848.00 | 69.00 | 365 |
1999 | EQUITY OIL & GAS FUNDS INC | 2122.00 | 144.00 | 365 |
2000 | EQUITY OIL & GAS FUNDS INC | 0.00 | 51.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1985 | INLAND DRILLING CO INC | Brine | 1351 | 365 |
1986 | INLAND DRILLING CO INC | Brine | 730 | 365 |
1987 | INLAND DRILLING CO INC | Brine | 0 | 245 |
1988 | INLAND DRILLING CO INC | Brine | 1413 | 112 |
1989 | INLAND DRILLING CO INC | Brine | 1729 | 300 |
1990 | INLAND DRILLING CO INC | Brine | 1427 | 365 |
1991 | INLAND DRILLING CO INC | Brine | 1208 | 365 |
1992 | INLAND DRILLING CO INC | Brine | 660 | 275 |
1993 | POG HOLDINGS CO INC | Brine | 747 | 365 |
1995 | EQUITY OIL & GAS FUNDS INC | Brine | 624 | 214 |
1996 | EQUITY OIL & GAS FUNDS INC | Brine | 769 | 365 |
1997 | EQUITY OIL & GAS FUNDS INC | Brine | 1202 | 365 |
1998 | EQUITY OIL & GAS FUNDS INC | Brine | 238 | 365 |
1999 | EQUITY OIL & GAS FUNDS INC | Brine | 688 | 365 |
2000 | EQUITY OIL & GAS FUNDS INC | Brine | 177 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1455902859 | 2013-7-19 0:00: | FR | No Violations | |
-1843569352 | 2004-7-29 0:00: | PB | No Violations | |
-1975611139 | 2004-7-28 0:00: | PB | No Violations | |
0673912297 | 2004-07-19 | Plug / Plug Back | No Violations | The well was plugged and abandoned on July 15, 2004 and was found to be leaking. The proposal at this time is to drill out and replace the top plug or plugs. The work will begin as soon as equipment can be scheduled. |
1091641540 | 2004-07-30 | Plug / Plug Back | No Violations | Top plug drilled out and the second plug drilled out to 525 feet. The top two plugs apparently fell approximately 150 feet. The hole bailed dry and there was no evidence of oil or gas. The plan is to check again on 8-02 and bail dry. If everything goes as planned, grouting is scheduled for the afternoon of 8-02. Grout will be placed from 525 to surface. |
1455902859 | 2013-07-19 | Final Restoration | No Violations | My inspection showed no evidence of the well, tank(s), separator or line associated with this permit number. I did find 4 line with 1.5 supply line (valve closed) above ground ~150 feet from the well site. I The area around the well has been graded and vegetation has been re-established. The lease road has been removed and vegetation has been re-established. Final restoration pending investigation of transmission line. |
1843569352 | 2004-07-29 | Plug / Plug Back | No Violations | The drill-out through the top plug is continuing. Should be through later today. Will evaluate at that time. |
1975611139 | 2004-07-28 | Plug / Plug Back | No Violations | Bishop Well Service has started drilling out the top plug. The rig operator reported that a small amount of oil (< 1 bbl) had circulated to surface while drilling. |
673912297 | 2004-7-19 0:00: | PB | No Violations |
For data sources see[9]