X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-133-21306

Well Details

Well ID: 34-133-21306
Loading map...
Country: United States
State: Ohio
County: Portage
Municipality: Ravenna Township
Operator Name: EQUITY OIL & GAS FUNDS INC
Well Pad ID:
Farm/Lease Name: ENLOW
License Status: Plugged and Abandoned
License Date: 2004-05-06
Spud Date: 1978-05-18
Spud Drilling Contractor:
Final Drill Date: 1978-07-07
Well Total Depth: 4470.00 ft
Configuration: Vertical
Latitude: 41.180000
Longitude: -81.210000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1977-12-23 317 INLAND DRILLING CO INC GeoDate 12/23/77
Original Spud 1978-05-18 R.L. 5-3-78
Completed 1978-07-07 R.L. 5-3-78
Reached Total Depth 1978-07-07 R.L. 5-3-78
CO 1992-09-16 3877 POG HOLDINGS CO INC GeoDate 12/23/77
CO 1995-07-17 1171 EQUITY OIL & GAS FUNDS IN GeoDate 12/23/77
APP 2001-08-17 Proposed Formations:CLINTON, Issued Date:8/17/2001, Expired Date:8/17/2002 6:00:00 AM, Drilling unit acres:48.55, Proposed Well Type:OG, Proposed Well Class:
APP 2004-05-06 Proposed Formations:CLINTON, Issued Date:5/6/2004, Expired Date:5/6/2005 6:00:00 AM, Drilling unit acres:48.55, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2004-07-15 R.L. 5-3-78
Construction Permit Expires 2005-05-06 R.L. 5-3-78
Record Last Modified 2013-03-14 R.L. 5-3-78

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 4310 4372 24
4310 4372 24
4310 4372 24

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 69000 Gal 150000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1985 INLAND DRILLING CO INC 5028.00 773.00 365
1986 INLAND DRILLING CO INC 4284.00 377.00 365
1987 INLAND DRILLING CO INC 1525.00 0.00 245
1988 INLAND DRILLING CO INC 1978.00 457.00 112
1989 INLAND DRILLING CO INC 4383.00 664.00 300
1990 INLAND DRILLING CO INC 3413.00 571.00 365
1991 INLAND DRILLING CO INC 5699.00 464.00 365
1992 INLAND DRILLING CO INC 3883.00 192.00 275
1993 POG HOLDINGS CO INC 4319.00 193.00 365
1995 EQUITY OIL & GAS FUNDS INC 1117.00 74.00 214
1996 EQUITY OIL & GAS FUNDS INC 1361.00 226.00 365
1997 EQUITY OIL & GAS FUNDS INC 2146.00 157.00 365
1998 EQUITY OIL & GAS FUNDS INC 1848.00 69.00 365
1999 EQUITY OIL & GAS FUNDS INC 2122.00 144.00 365
2000 EQUITY OIL & GAS FUNDS INC 0.00 51.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1985 INLAND DRILLING CO INC Brine 1351 365
1986 INLAND DRILLING CO INC Brine 730 365
1987 INLAND DRILLING CO INC Brine 0 245
1988 INLAND DRILLING CO INC Brine 1413 112
1989 INLAND DRILLING CO INC Brine 1729 300
1990 INLAND DRILLING CO INC Brine 1427 365
1991 INLAND DRILLING CO INC Brine 1208 365
1992 INLAND DRILLING CO INC Brine 660 275
1993 POG HOLDINGS CO INC Brine 747 365
1995 EQUITY OIL & GAS FUNDS INC Brine 624 214
1996 EQUITY OIL & GAS FUNDS INC Brine 769 365
1997 EQUITY OIL & GAS FUNDS INC Brine 1202 365
1998 EQUITY OIL & GAS FUNDS INC Brine 238 365
1999 EQUITY OIL & GAS FUNDS INC Brine 688 365
2000 EQUITY OIL & GAS FUNDS INC Brine 177 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1455902859 2013-7-19 0:00: FR No Violations
-1843569352 2004-7-29 0:00: PB No Violations
-1975611139 2004-7-28 0:00: PB No Violations
0673912297 2004-07-19 Plug / Plug Back No Violations The well was plugged and abandoned on July 15, 2004 and was found to be leaking. The proposal at this time is to drill out and replace the top plug or plugs. The work will begin as soon as equipment can be scheduled.
1091641540 2004-07-30 Plug / Plug Back No Violations Top plug drilled out and the second plug drilled out to 525 feet. The top two plugs apparently fell approximately 150 feet. The hole bailed dry and there was no evidence of oil or gas. The plan is to check again on 8-02 and bail dry. If everything goes as planned, grouting is scheduled for the afternoon of 8-02. Grout will be placed from 525 to surface.
1455902859 2013-07-19 Final Restoration No Violations My inspection showed no evidence of the well, tank(s), separator or line associated with this permit number. I did find 4 line with 1.5 supply line (valve closed) above ground ~150 feet from the well site. I The area around the well has been graded and vegetation has been re-established. The lease road has been removed and vegetation has been re-established. Final restoration pending investigation of transmission line.
1843569352 2004-07-29 Plug / Plug Back No Violations The drill-out through the top plug is continuing. Should be through later today. Will evaluate at that time.
1975611139 2004-07-28 Plug / Plug Back No Violations Bishop Well Service has started drilling out the top plug. The rig operator reported that a small amount of oil (< 1 bbl) had circulated to surface while drilling.
673912297 2004-7-19 0:00: PB No Violations

For data sources see[9]

References