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Well ID: 34-133-21482 | Loading map...
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Country: United States | |
State: Ohio | |
County: Portage | |
Municipality: Randolph Township | |
Operator Name: BAKERWELL INC | |
Well Pad ID: | |
Farm/Lease Name: HOLLENDONNER-CAPPS UNIT | |
License Status: Producing | |
License Date: 1989-01-20 | |
Spud Date: 1978-08-05 | |
Spud Drilling Contractor: ROSS WELL SERVICE | |
Final Drill Date: 1978-08-24 | |
Well Total Depth: 537.00 ft | |
Configuration: Vertical | |
Latitude: 41.000000 | |
Longitude: -81.220000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1978-06-02 | 432 BAKERWELL INC GeoDate 6/2/78 |
Original Spud | 1978-08-05 | |
Completed | 1978-08-24 | |
Reached Total Depth | 1978-08-24 | |
CO | 1989-01-20 | 432 BAKERWELL INC GeoDate 1/20/89 |
Unknown | 1989-01-20 | Issued Date 1/20/89 Expired Date 1/20/90 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date |
Construction Permit Expires | 1990-01-20 | |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
0 | 0 | 0 | OPEN HOLE COMPLETION | |||
Not Treated | 0 | 0 | 0 |
For data sources see[3]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1985 | CURRY R D PRODUCTION CO | 0.00 | 0.00 | 0 |
1986 | CURRY R D PRODUCTION CO | 0.00 | 0.00 | 0 |
1987 | BAKERWELL INC | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1985 | CURRY R D PRODUCTION CO | Brine | 0 | 0 |
1986 | CURRY R D PRODUCTION CO | Brine | 0 | 0 |
1987 | BAKERWELL INC | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1221255529 | 2014-2-14 0:00: | PW | No Violations | 1.00 |
1221255529 | 2014-02-14 | Production Wells | No Violations | Status check inspection of this Berea Sandstone well. A check of records indicates that no commercial production has been reported for this well over the past 29 years. A plugging permit was issued to Bakerwell in January of 1989 and expired in 1990 without being executed. Attempts to locate the wellhead were unsuccessfull. I walked to the GPS location of the wellhead and could find nothing in the immediate area. An area 30 to the north had stumps and dirt piled up and the wellhead may be located in this area. I found a 2 steel flow/sales line emerging 250 to the northeast that had a 1 line coming off of it and equipped with a regulator. This ran to a drip bottle and then below grade. A gauge on the line past the regulator read 14psi and the valves on the line were open. Further investigation will be necessary to confirm that this well does exist and that this equipment is, in fact, related to this well. |
For data sources see[8]