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Well ID: 34-133-22101 | Loading map...
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Country: United States | |
State: Ohio | |
County: Portage | |
Municipality: Ravenna Township | |
Operator Name: ENERGY DEVELOPMENT CORPORATION | |
Well Pad ID: | |
Farm/Lease Name: DUDAK MICHAEL | |
License Status: Producing | |
License Date: 1979-11-13 | |
Spud Date: 1980-01-16 | |
Spud Drilling Contractor: | |
Final Drill Date: 1980-01-21 | |
Well Total Depth: 4510.00 ft | |
Configuration: Vertical | |
Latitude: 41.200000 | |
Longitude: -81.240000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1979-11-13 | 2817 ENERGY DEVELOP CORP GeoDate 11/13/79 |
Original Spud | 1980-01-16 | |
Completed | 1980-01-21 | |
Reached Total Depth | 1980-01-21 | |
Construction Permit Expires | 1980-11-12 | |
Record Last Modified | 2013-10-03 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 4340 | 4385 | 16 |
4340 | 4385 | 16 | |
4340 | 4385 | 16 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 56000 Gal | 55000 |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1033082415 | 2005-4-18 0:00: | PW | No Violations | |
-1948202074 | 2005-7-12 0:00: | PW | No Violations | |
-706932294 | 2010-10-6 0:00: | PW | No Violations | |
0290838947 | 2005-04-15 | Production Wells | Violations Noted | Received a call from Dominion East Ohio reporting a gas leak at 7850 SR 44 in Shalersville Township. The Dudek well is located west of the leak. I contacted Mark Smith (contract pumper) and requested that the well be shut in and the leak repaired as soon as possible. |
0706932294 | 2010-10-06 | Production Wells | No Violations | I received a gas odor complaint report from Dominion East Ohio who investigated and determined that the source was not their line. The complaint was from 7850 SR 44. The Dudak well is located west of the complaint. The same pipeline was involved in a complaint in 2005. I again contacted Mark Smith (contract pumper) and asked that the wells be shut in until the line is repaired or replaced. |
0746671253 | 2005-04-26 | Production Wells | Violations Noted | The pipeline leak has been repaired but the site needs to be reclaimed. |
1033082415 | 2005-04-18 | Production Wells | Violations Noted | The well has been shut in but the pipeline has not yet been repaired. |
1517616984 | 2017-06-12 | UrbanProduction Wells | No Violations | I conducted a status check inspection of this Clinton Sandstone well. My inspection found the well equipped and operating with the aid on a natural gas powered pumping unit. The timer on the unit was set to cycle in 8 minutes and the pumping unit kicked on at this time. A gauge on the tubing indicated a pressure of 180psi and there was no gauge on the 4.5 production casing. There was a domestic tap on the 4.5 casing port equipped with a regulator and there were two (2) 1 supply lines with open valves supplying domestic gas. The well produces to a diked tank battery containing one (1) 210 barrel tank, a concrete brine vault, and a horizontal separator. The chart in the meter box is currently recording production and the chart was changed on 6/7/2017. The required ID is posted on the tank. No violations. |
1948202074 | 2005-07-12 | Production Wells | Violations Noted | CASE 05-013 The salesline leak has been repaired and the violation is corrected. |
2128009476 | 2019-7-11 0:00: | UP | No Violations | 0.90 |
290838947 | 2005-4-15 0:00: | PW | No Violations | |
746671253 | 2005-4-26 0:00: | PW | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0290838947 | US-OH-123021 | 2005-04-26 | Inadequate pipeline strength | |
0746671253 | US-OH-128487 | 2005-04-26 | Inadequate pipeline strength | |
1033082415 | US-OH-100026 | 2005-04-26 | Inadequate pipeline strength | |
1948202074 | US-OH-119644 | 2005-04-26 | Inadequate pipeline strength |
For data sources see[9]