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Well ID: 34-133-22223 | Loading map...
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Country: United States | |
State: Ohio | |
County: Portage | |
Municipality: Freedom Township | |
Operator Name: KST OIL & GAS CO INC | |
Well Pad ID: | |
Farm/Lease Name: LANGE-STONESTREET ETAL | |
License Status: Final Restoration | |
License Date: 1986-10-15 | |
Spud Date: 1980-03-26 | |
Spud Drilling Contractor: | |
Final Drill Date: 1980-03-31 | |
Well Total Depth: 4678.00 ft | |
Configuration: Vertical | |
Latitude: 41.210000 | |
Longitude: -81.160000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1980-03-24 | 140 KST OIL & GAS CO INC GeoDate 3/24/80 |
Original Spud | 1980-03-26 | CHANGED STATUS OF WELL FROM PR TO FR PER FACILITY REPORT FROM MICHAEL DINSMORE DATED 7/16/2015 F_RESS_PASS ON 11/5/2015 CM. |
Completed | 1980-03-31 | CHANGED STATUS OF WELL FROM PR TO FR PER FACILITY REPORT FROM MICHAEL DINSMORE DATED 7/16/2015 F_RESS_PASS ON 11/5/2015 CM. |
Reached Total Depth | 1980-03-31 | CHANGED STATUS OF WELL FROM PR TO FR PER FACILITY REPORT FROM MICHAEL DINSMORE DATED 7/16/2015 F_RESS_PASS ON 11/5/2015 CM. |
CO | 1985-03-18 | 140 KST OIL & GAS CO INC GeoDate 3/18/85 |
Unknown | 1985-03-18 | Issued Date 3/18/85 Expired Date 9/18/86 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date |
CO | 1985-09-18 | 140 KST OIL & GAS CO INC GeoDate 9/18/85 |
Unknown | 1985-09-18 | Issued Date 9/18/85 Expired Date 9/14/85 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date |
CO | 1986-10-15 | 140 KST OIL & GAS CO INC GeoDate 10/15/86 |
Unknown | 1986-10-15 | Issued Date 10/15/86 Expired Date 10/15/87 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date |
Construction Permit Expires | 1987-10-15 | CHANGED STATUS OF WELL FROM PR TO FR PER FACILITY REPORT FROM MICHAEL DINSMORE DATED 7/16/2015 F_RESS_PASS ON 11/5/2015 CM. |
Record Last Modified | 2019-06-05 | CHANGED STATUS OF WELL FROM PR TO FR PER FACILITY REPORT FROM MICHAEL DINSMORE DATED 7/16/2015 F_RESS_PASS ON 11/5/2015 CM. |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 4420 | 4510 | 18 |
4420 | 4510 | 18 | |
4420 | 4510 | 18 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 115000 Gal | 40000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | KST OIL & GAS CO INC | 2188.00 | 431.00 | 365 |
1985 | KST OIL & GAS CO INC | 180.00 | 0.00 | 365 |
1987 | KST OIL & GAS CO INC | 0.00 | 0.00 | 0 |
1988 | KST OIL & GAS CO INC | 0.00 | 0.00 | 365 |
1989 | KST OIL & GAS CO INC | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | KST OIL & GAS CO INC | Brine | 0 | 365 |
1985 | KST OIL & GAS CO INC | Brine | 283 | 365 |
1987 | KST OIL & GAS CO INC | Brine | 0 | 0 |
1988 | KST OIL & GAS CO INC | Brine | 0 | 365 |
1989 | KST OIL & GAS CO INC | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-2114335522 | 2015-7-16 0:00: | FR | No Violations | 1.00 |
2114335522 | 2015-07-16 | Final Restoration | No Violations | I conducted a final restoration inspection for this well. KST Oil & Gas Co. Inc., ceased operations between 1995 and 1996. Jeff Moore (Moore Well Services) used to work for KST and remembers the well being plugged in the late 1980s. Jeff has gone through all of KSTs files and there are no records of the plugging and abandonment of this well. Also, there are no records on file with the Division of Oil & Gas indicating that the well was plugged. I checked aerial photos on the Portage County Auditors website and photos from 1985 clearly show the well location and tank battery. The next year available on the website was 1990, and shows that the well equipment and tank battery had been removed from the location. Research and a field check of the area indicate that this well was plugged and abandoned between 1985 and 1990. I have determined the location of the well is now under the southeast side of Chesapeake Explorations Murvay Pad where the #8H (PN# 4423-01) was drilled. Based on my findings and the lack of field evidence that the well exists, final restoration is approved. |
For data sources see[9]