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Well ID: 34-133-23411 | Loading map...
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Country: United States | |
State: Ohio | |
County: Portage | |
Municipality: Atwater Township | |
Operator Name: BANCEQUITY PETROLEUM CORPORATI | |
Well Pad ID: | |
Farm/Lease Name: BONATH UNIT | |
License Status: Producing | |
License Date: 1985-08-13 | |
Spud Date: 1985-08-20 | |
Spud Drilling Contractor: H.L.H. DRLG | |
Final Drill Date: 1985-08-27 | |
Well Total Depth: 4890.00 ft | |
Configuration: Vertical | |
Latitude: 41.000000 | |
Longitude: -81.150000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1985-08-13 | 260 TWINOAKS OIL & GAS CO GeoDate 8/13/85 |
Oil and Gas | 1985-08-13 | Issued Date 8/13/85 Expired Date 8/13/86 Acres 0040000 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 04890 Proposed Drill Depth 04890 |
Original Spud | 1985-08-20 | |
Completed | 1985-08-27 | |
Reached Total Depth | 1985-08-27 | |
Completion Report Received | 1985-09-13 | |
Construction Permit Expires | 1986-08-13 | |
CO | 1991-10-24 | 631 BT ENERGY CORP GeoDate 8/13/85 |
CO | 1996-04-09 | 4801 BANCEQUITY PETROLEUM CORP GeoDate 8/13/85 |
Correction to Well | 2005-05-06 | CORRECTION TO THE FOLLOWING: 1) UNIT SIZE: 41.60 ACRES; 2) FOOTAGE LOCATION: 120'NL & 1380'EL OF LOT 79; 3) X: 2,371,735; 4) Y: 489,180; 4) ELEV: 1125'. |
Last Compliance Report | 2015-10-05 | |
Record Last Modified | 2019-06-14 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 4678 | 4814 | 0 |
4678 | 4814 | 0 | |
2006-09-11 | 4733 | 4808 | 24 |
4733 | 4808 | 24 | |
4678 | 4814 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1840 Bbl | 60000 | FRAC;H2O,SAND |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-115331628 | 2015-8-3 0:00:0 | TD | No Violations | 0.70 |
-393579337 | 2005-8-23 0:00: | PW | No Violations | |
-44628804 | 2010-4-29 0:00: | AD | No Violations | |
0000PL5975 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0044628804 | 2010-04-29 | Annular Disposal | No Violations | There is no indication that annular disposal is being used at this location. No violations at this time. |
0115331628 | 2015-08-03 | Temporary Abandoned Annular Disposal | No Violations | I inspected this well to check for the use of annular disposal. This wellhead is equipped with a natural gas powered pumping unit and has 50psi on the tubing according to the pressure gauge. This well produces to a diked tank battery shared by PN#23243 and contains four (4) 100 barrel tanks, two (2) horizontal separators and meter runs, and a brine vault. The proper ID signage is posted on each set of tanks. I found no evidence of annular disposal being used at this time. No violations. |
0130928484 | 2005-04-26 | Production Wells | Violations Noted | The affected area related to the pipeline leak south and west of the tank battery has been addressed. The old spill inside of the containment dike has not been corrected. According to Randy Hall, he will be drilling another well on the property and will correct the tank battery issue when he has equipment on site to build the drilling location. |
0393579337 | 2005-08-23 | Production Wells | Violations Noted | The tank battery has been cleaned up and painted. ID will be posted as soon as the paint has dried. The violation is corrected. |
0443224359 | 2005-04-14 | Production Wells | Violations Noted | No significant activity has occurred to remediate the spill. Sorbent pads have been replaced. |
1072285781 | 2003-12-24 | Annular Disposal | No Violations | Status check inspection for annular disposal (AD) use at the request of Tom Tomastik. No AD at this time. |
130928484 | 2005-4-26 0:00: | PW | No Violations | |
1420552919 | 2014-12-15 | Production Wells | No Violations | I received a call from Dan Horning (contract pumper) on 12/14/14 at 5:33pm that they had discovered a flow line leak in the woods between the wellhead and the tank battery around 5:00pm and have shut the well down to stop the leak. At this point, they did not think any Waters of the State were impacted. I was on location the next morning (12/15/14) and met with Tom Fischietto (President of Bancequity) and Dan Horning. I was informed that oil was found ponded in a drainage ditch/creek that empties into Walborn Reservoir and that no oil had reached the reservoir. I assessed the release and found an area, 20 in diameter above the flow line, saturated with oil. An estimated 5-10 barrels of oil was released during the incident. We walked the creek and there were several pockets where oil had collected behind trees and branches. At the farthest point where debris had blocked the flow of oil (700-800 downstream from the leak), an earthen siphon dam was being installed with 2-15 corrugated pipes. I instructed them to install booms further downstream and to construct another siphon dam as a precaution. I walked an unknown distance along the meandering creek and found no evidence that the release had impacted downstream from the first siphon dam or the reservoir. I instructed Tom to call the OEPA spill reporting hotline as this was a reportable spill. As Tom reported the spill, I called Kurt Kollar (OEPA) to notify him of the incident. He said he would call Wade Balser (OEPA) and get him in route to the location. Scott Miller Contracting arrived on location with equipment to assist in clean-up operations. Wade arrived on location and the OEPA assumed authority over containment and remedial operations. I will continue to assist the OEPA in monitoring the location through the spring before containment barriers can be removed and inspect for additional corrections. |
1884794399 | 2005-04-07 | Production Wells | Violations Noted | Received a call from Portage County Emergency Management reporting an oil spill near this tank battery. I contacted Randy Hall who stated that they had a flowline leak just south of the tank battery which they have been working on. The spill came to surface above the flowline and ran approximately 200 feet down gradient to the west. Additional corrective action is necessary. |
443224359 | 2005-4-14 0:00: | PW | No Violations | |
PL5975 | PL | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0130928484 | US-OH-108755 | 2005-04-18 | Well operation causing pollution and contamination | |
0393579337 | US-OH-124182 | 2005-04-18 | Well operation causing pollution and contamination | |
0443224359 | US-OH-124775 | 2005-04-18 | Well operation causing pollution and contamination | |
1884794399 | US-OH-118925 | 2005-04-18 | Well operation causing pollution and contamination |
For data sources see[9]