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Well ID: 34-133-24081 | Loading map...
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Country: United States | |
State: Ohio | |
County: Portage | |
Municipality: Atwater Township | |
Operator Name: SOUND ENERGY CO INC | |
Well Pad ID: | |
Farm/Lease Name: CRAIN UNIT # 2K-W | |
License Status: Producing | |
License Date: 1996-10-18 | |
Spud Date: 1996-11-16 | |
Spud Drilling Contractor: IPSCO | |
Final Drill Date: 1996-12-02 | |
Well Total Depth: 7550.00 ft | |
Configuration: Vertical | |
Latitude: 41.050000 | |
Longitude: -81.170000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1996-10-18 | 2911 WEINSZ OIL & GAS INC GeoDate 10/18/96 |
Oil and Gas | 1996-10-18 | Issued Date 10/18/96 Expired Date 10/18/97 Acres 0040255 Tool Type RTAF Proposed Formation ROSE RUN Proposed Depth 00000 Proposed Drill Depth 00000 |
Original Spud | 1996-11-16 | RBDMS Rec |
Completed | 1996-12-02 | RBDMS Rec |
Reached Total Depth | 1996-12-02 | RBDMS Rec |
Completion Report Received | 1997-08-05 | RBDMS Rec |
Construction Permit Expires | 1997-10-18 | RBDMS Rec |
Change of Owner | 2004-05-06 | Operator changed from 2911, WEINSZ OIL & GAS INC to 7626, M & M ROYALTY LTD |
Change of Owner | 2015-07-06 | Operator changed from 7626, M & M ROYALTY LTD to 4327, SOUND ENERGY CO INC |
Record Last Modified | 2017-02-15 | RBDMS Rec |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-10-08 | 7350 | 7403 | 93 |
7350 | 7403 | 93 | |
7350 | 7403 | 93 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1800 Bbl | 40000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1997 | WEINSZ OIL & GAS INC | 107177.00 | 76543.00 | 350 |
1998 | WEINSZ OIL & GAS INC | 45382.00 | 21322.00 | 365 |
1999 | WEINSZ OIL & GAS INC | 46685.00 | 9253.00 | 365 |
2000 | WEINSZ OIL & GAS INC | 35100.00 | 5704.00 | 365 |
2001 | WEINSZ OIL & GAS INC | 25023.00 | 4043.00 | 365 |
2002 | WEINSZ OIL & GAS INC | 19239.00 | 2061.00 | 365 |
2003 | WEINSZ OIL & GAS INC | 1532.00 | 0.00 | 365 |
2004 | M & M ROYALTY LTD | 1152.00 | 0.00 | 365 |
2005 | M & M ROYALTY LTD | 8769.00 | 621.00 | 365 |
2006 | M & M ROYALTY LTD | 5628.00 | 458.00 | 365 |
2007 | M & M ROYALTY LTD | 5590.00 | 300.00 | 365 |
2008 | M & M ROYALTY LTD | 4519.00 | 358.00 | 365 |
2009 | M & M ROYALTY LTD | 5879.00 | 310.00 | 365 |
2010 | M & M ROYALTY LTD | 4120.00 | 247.00 | 365 |
2011 | M & M ROYALTY LTD | 2280.00 | 87.00 | 365 |
2012 | M & M ROYALTY LTD | 1211.00 | 66.00 | 366 |
2013 | M & M ROYALTY LTD | 2367.00 | 94.00 | 365 |
2014 | M & M ROYALTY LTD | 1130.00 | 0.00 | 365 |
2015 | SOUND ENERGY CO INC | 347.00 | 0.00 | 213 |
2016 | SOUND ENERGY CO INC | 748.00 | 0.00 | 365 |
2017 | SOUND ENERGY CO INC | 215.00 | 0.00 | 365 |
2018 | SOUND ENERGY CO INC | 358.00 | 0.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1997 | WEINSZ OIL & GAS INC | Brine | 3250 | 350 |
1998 | WEINSZ OIL & GAS INC | Brine | 2405 | 365 |
1999 | WEINSZ OIL & GAS INC | Brine | 1980 | 365 |
2000 | WEINSZ OIL & GAS INC | Brine | 1480 | 365 |
2001 | WEINSZ OIL & GAS INC | Brine | 1042 | 365 |
2002 | WEINSZ OIL & GAS INC | Brine | 680 | 365 |
2003 | WEINSZ OIL & GAS INC | Brine | 155 | 365 |
2004 | M & M ROYALTY LTD | Brine | 0 | 365 |
2005 | M & M ROYALTY LTD | Brine | 420 | 365 |
2006 | M & M ROYALTY LTD | Brine | 420 | 365 |
2007 | M & M ROYALTY LTD | Brine | 420 | 365 |
2008 | M & M ROYALTY LTD | Brine | 520 | 365 |
2009 | M & M ROYALTY LTD | Brine | 422 | 365 |
2010 | M & M ROYALTY LTD | Brine | 490 | 365 |
2011 | M & M ROYALTY LTD | Brine | 210 | 365 |
2012 | M & M ROYALTY LTD | Brine | 329 | 366 |
2013 | M & M ROYALTY LTD | Brine | 345 | 365 |
2014 | M & M ROYALTY LTD | Brine | 250 | 365 |
2015 | SOUND ENERGY CO INC | Brine | 481 | 213 |
2016 | SOUND ENERGY CO INC | Brine | 0 | 365 |
2017 | SOUND ENERGY CO INC | Brine | 0 | 365 |
2018 | SOUND ENERGY CO INC | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-47845124 | 2007-8-2 0:00:0 | PW | No Violations | |
0047845124 | 2007-08-02 | Production Wells | No Violations | Status check inspection found no violations at this time. |
1508764041 | 2017-10-23 | Production Wells | No Violations | I inspected this Rose Run well to follow-up on a reported gas leak from 10/21/17 and incident #NR10211700003462. My inspection found the wellhead equipped with a natural gas powered pumping unit. The tubing and flow valve are open and a gauge indicates a pressure of 120psi on the tubing. The well produces through a horizontal separator and then through a vertical separator. A gauge on the vertical separator indicates a pressure of 120psi. Fluids are produced to a diked tank battery containing one (1) 210 barrel tank and one (1) 100 barrel tank. The posted ID placard indicates Weinsz Oil & Gas as the owner in is incorrect. Sound Energy acquired this well in July of 2015 and the ownership and emergency contact numbers need to be updated. I found a gas leak in the separator area where the flow line from the wellhead is connected with a hammer union. There is a clamp on the end of the flowline at the connection with the hammer union and the steel line is visibly corroded and leaking a small amount of gas. I spoke with the well pumper, Bob Allen, and he told me he responded Saturday (10/21/17) night and relieved the pressure on the line and it is now open and selling gas. He said the sales line was shut-in and had pressured up and began to leak. He told me he would have the ID signage posted today and will have the line repaired by the end of the week. A compliance notice will be issued if the issues found today are not addressed by the end of the week. |
1509108002 | 2017-10-27 | Production Wells | No Violations | I was on location to follow-up on a reported gas leak from 10/21/17, incident #NR10211700003462, and to see if corrective actions had been taken to address the issues found during an inspection on 10/23/17. My inspection today found that the clamped and corroded section of flow line at the separator has been removed and repaired. The required ID signage has been posted as requested. All issues have been resolved. No violations. |
For data sources see[9]