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34-133-24096

Well Details

Well ID: 34-133-24096
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Country: United States
State: Ohio
County: Portage
Municipality: Nelson Township
Operator Name: STALLION OILFIELD SERVICES LTD
Well Pad ID:
Farm/Lease Name: GROSELLE # 2
License Status: Active Injection
License Date: 2007-03-27
Spud Date: 1998-01-20
Spud Drilling Contractor: MOHAWK DRLG
Final Drill Date: 1998-01-26
Well Total Depth: 4323.00 ft
Configuration: Vertical
Latitude: 41.340000
Longitude: -81.080000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1997-01-21 2911 WEINSZ OIL & GAS INC GeoDate 1/21/97
Oil and Gas 1997-01-21 Issued Date 1/21/97 Expired Date 1/21/98 Acres 0043000 Tool Type RTAF Proposed Formation CLINTON Proposed Depth Proposed Drill Depth
Original Spud 1998-01-20
Completed 1998-01-26
Reached Total Depth 1998-01-26
Change of Owner 2004-05-06 Operator changed from 2911, WEINSZ OIL & GAS INC to 7626, M & M ROYALTY LTD
Change of Owner 2007-02-08 Operator changed from 7626, M & M ROYALTY LTD to 5785, M-J OIL COMPANY INC.
APP 2007-03-27 Proposed Formations:NEWBURG, Issued Date:3/27/2007, Expired Date:3/26/2008 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:SWD, Proposed Well Class:SWIW
Plugged Back 2007-06-04
Last Compliance Report 2007-06-20
Construction Permit Expires 2008-03-26
Completion Report Received 2008-06-13
Change of Owner 2008-08-22 Operator changed from 5785, M-J OIL COMPANY INC. to 8417, SALTYS DISPOSAL WELLS LP
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2007-06-20 4148 4227 31
2007-06-20 3756 3898 117
4148 4227 31
3756 3898 117
3756 3898 117

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 28 1800 Bbl 50000 3000 GALLONS ACID

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1998 WEINSZ OIL & GAS INC 917.00 408.00 274
1999 WEINSZ OIL & GAS INC 993.00 690.00 365
2000 WEINSZ OIL & GAS INC 797.00 672.00 365
2001 WEINSZ OIL & GAS INC 740.00 504.00 365
2002 WEINSZ OIL & GAS INC 694.00 336.00 365
2003 WEINSZ OIL & GAS INC 63.00 163.00 365
2004 M & M ROYALTY LTD 0.00 0.00 0
2005 M & M ROYALTY LTD 1.00 0.00 365
2006 M & M ROYALTY LTD 219.00 648.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1998 WEINSZ OIL & GAS INC Brine 463 274
1999 WEINSZ OIL & GAS INC Brine 545 365
2000 WEINSZ OIL & GAS INC Brine 352 365
2001 WEINSZ OIL & GAS INC Brine 405 365
2002 WEINSZ OIL & GAS INC Brine 70 365
2003 WEINSZ OIL & GAS INC Brine 0 365
2004 M & M ROYALTY LTD Brine 0 0
2005 M & M ROYALTY LTD Brine 0 365
2006 M & M ROYALTY LTD Brine 442 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1019386027 2016-3-1 0:00:0 SW No Violations
-1067527665 2007-8-7 0:00:0 SW No Violations
-1214170649 2019-5-14 0:00: SW No Violations 0.70
-1315272181 2019-2-26 0:00: SW No Violations 0.80
-1382469469 2007-8-23 0:00: SW No Violations
-1456535334 2014-10-28 0:00 SW No Violations
-1483497142 2007-5-21 0:00: SW No Violations
-14864503 2010-8-26 0:00: SW No Violations
-1526603732 2011-11-3 0:00: SW No Violations
-1535744776 2013-10-17 0:00 SW No Violations
-1543086205 2019-12-30 0:00 SW No Violations 0.90
-1582050269 2010-12-16 0:00 SW No Violations
-1623026476 2016-6-14 0:00: SW No Violations
-166424212 2017-10-24 0:00 SW No Violations 0.40
-1692446724 2014-7-21 0:00: SW No Violations
-1697130417 2007-11-27 0:00 SW No Violations
-1708840972 2008-11-17 0:00 SW No Violations
-1720120469 2009-5-12 0:00: SW No Violations
-1735853786 2020-3-3 0:00:0 SW No Violations 1.30
-1781902439 2020-8-27 0:00: SW No Violations 1.00
-1819235146 2013-7-1 0:00:0 SW No Violations
-200564868 2018-2-12 0:00: SW No Violations 0.80
-2011417827 2019-2-1 0:00:0 SW No Violations 0.40
-2146572833 2016-3-26 0:00: SW No Violations
-219462310 2012-3-7 0:00:0 SW No Violations
-252480123 2014-6-12 0:00: SW No Violations
-283156881 2012-9-7 0:00:0 SW No Violations
-37262628 2017-7-12 0:00: SW No Violations 1.00
-402631818 2015-2-18 0:00: SW No Violations
-410687730 2019-2-11 0:00: SW No Violations
-428955695 2014-12-2 0:00: SW No Violations
-477188260 2018-12-19 0:00 SW No Violations 0.80
-512113710 2013-7-2 0:00:0 SW No Violations
-541331523 2011-11-3 0:00: SW No Violations
-542847355 2009-2-3 0:00:0 SW No Violations
-578448936 2017-1-30 0:00: SW No Violations
-607116022 2015-12-23 0:00 SW No Violations
-608998383 2017-9-29 0:00: SW No Violations
-67878303 2018-4-2 0:00:0 SW No Violations
-703060419 2020-5-27 0:00: SW No Violations 0.40
-742398701 2013-9-6 0:00:0 SW No Violations
-745537005 2019-8-22 0:00: SW No Violations
-801803786 2011-2-15 0:00: SW No Violations
-80312818 2015-7-27 0:00: SW No Violations
-819360186 2020-7-8 0:00:0 SW No Violations 0.50
-829842440 2016-8-1 0:00:0 SW No Violations
0014864503 2010-08-26 Salt Water Injection Well No Violations Status check inspection found no violations at this time.
0037262628 2017-07-12 Salt Water Injection Well No Violations I performed an inspection of the injection well and surface facility found no violations.
0067878303 2018-04-02 Salt Water Injection Well No Violations I was on location for an UIC facility inspection. I found the injection not in operation on the day of my inspection. I observed no leaks or spills. Identification signs are posted. There are no violations at this time.
0071613901 2015-06-04 Salt Water Injection Well No Violations A mechanical integrity test (MIT) was performed on the well. The tubing-casing annulus was pressured up to 960 pounds per square inch. There was pressure of 220 psi. on the tubing. Both pressures remained constant for fifteen minutes. The test demonstrated mechanical integrity.
0073718903 2016-12-30 Salt Water Injection Well No Violations The injection well and surface facility were inspected. The annular pressure was not gauged, because the casing was frozen. There were no violations at the time.
0080312818 2015-07-27 Salt Water Injection Well No Violations The well and surface facility were inspected. There were no violations found at the time of inspection.
0104662198 2014-11-14 Salt Water Injection Well No Violations The injection well and surface facility were inspected. There were no violations found at the time.
0166424212 2017-10-24 Salt Water Injection Well No Violations I was on location to inspect the injection well. I found the proper identification signs posted. The UIC facility is in good repair. There is a chain link fence around the well. There are no violations at this time.
0200564868 2018-02-12 Salt Water Injection Well No Violations I was on location to inspect the UIC well and facility. I found the well not in operation on the day of my inspection. I found no spills or leaks. The proper identification signs are posted. There is a chain link fence surrounding the wellhead. There are no violations at this time.
0219462310 2012-03-07 Salt Water Injection Well No Violations No violatons were found at the time of my inspection of this well site.
0252480123 2014-06-12 Salt Water Injection Well No Violations An inspection of the well and injection facility found no violations.
0283156881 2012-09-07 Salt Water Injection Well No Violations The well was treated with 1500 gallons of Hydrochloric acid.

My inspection of the treatment operation found no violations.

0364493409 2012-09-05 Salt Water Injection Well No Violations The pump was shut off just prior to pressure measurement.
0379874124 2014-03-18 Salt Water Injection Well No Violations There were no violations at the time of inspection.
0402631818 2015-02-18 Salt Water Injection Well No Violations The tubing/casing annulus was frozen. There were no violations at the time of inspection.
0410687730 2019-02-11 Salt Water Injection Well Violations Noted The Division has not received the 4th quarter brine disposal fees for 2018. Please forward disposal fees and sheets to the Division by 3/12/2019.
0416148764 2017-06-19 Salt Water Injection Well No Violations The injection well and surface facility were inspected. There were no violations found at the time.
0428955695 2014-12-02 Salt Water Injection Well No Violations A water sample (sample SJO #121) was taken from Stallion truck #39186. The load was from the Pitts lease, Columbiana County permit number 2-1816. The sample was sent to the ODNR Laboratory in Cambridge, Ohio.
0435425214 2015-05-06 Salt Water Injection Well No Violations The well and surface facility were inspected. There were no violations found at the time of inspection.
0476656976 2018-06-25 Salt Water Injection Well No Violations I found the injection well not in operation on the day of my inspection. An identification sign is posted. I observed no leaks or spills. There are no violations at this time.
0477188260 2018-12-19 Salt Water Injection Well No Violations I was on location to investigate possible pumping standing water within the diked tank battery onto the ground outside of the diked tank battery. I found no evidence of pumping the water out of the dike. I spoke with the facility operator on location. I was shown by the facility operator that the water in the diked tank battery is pumped by sump pump and garden hose to a floor drain in the pump house which flows into a concrete vault next to the off-loading pad. The water in the concrete vault is then pumped into a storage tank. There are no violations at this time.
0512113710 2013-07-02 Salt Water Injection Well No Violations I witnessed the installation of the packer.
0517951705 2018-11-14 Salt Water Injection Well No Violations
0541331523 2011-11-03 Salt Water Injection Well No Violations I performed a random inspection of the tankers coming into the location. There were no violations at this time.
0542847355 2009-02-03 Salt Water Injection Well No Violations Quarterly status check inspection found no violations at this time.
0578448936 2017-01-30 Salt Water Injection Well No Violations An inspection of the injection well and surface facility found no violations.
0606543304 2011-08-04 Salt Water Injection Well No Violations I performed the quarterly UIC test on the annulus and the injection. The well was running. There were no violations at this time.
0607116022 2015-12-23 Salt Water Injection Well Violations Noted The well was found exceeding the maximum allowable injection pressure. The well tender was instructed to shut down immediately. Rick Rahmoeller, the well owners field supervisor, was instructed to set the pressure shut-off switch at the maximum allowable injection pressure.
0608998383 2017-09-29 Salt Water Injection Well No Violations The injection well and surface facility were inspected. The pump was operating at the time. The tanks and lines had no visible leaks.

There were no violations found.

0635207594 2017-03-10 Salt Water Injection Well No Violations The injection well and surface facility were inspected. There were no violations at the time.
0679506042 2017-02-17 Salt Water Injection Well No Violations An inspection of the injection well and surface facility found no violations.
0730856680 2018-08-09 Salt Water Injection Well No Violations I found the injection well not operating on the day of my inspection. Identification signs are posted at the well and access road entrance. I observed no leaks or spills. I spoke with Chuck Wilson from Stallion on location.
0742398701 2013-09-06 Salt Water Injection Well No Violations My inspection of the well and injection facility found no violations.
0801803786 2011-02-15 Salt Water Injection Well No Violations Quarterly status check inspection found no violations at this time.
0829842440 2016-08-01 Salt Water Injection Well No Violations The injection well and surface facility were inspected. No one was onsite. There were no violations found at the time.
0839252422 2014-09-23 Salt Water Injection Well No Violations An inspection of the well and injection facility found no violations.
0839371641 2013-07-01 Salt Water Injection Well No Violations A new packer and tubing was ran into the well. The tool sat down on an obstruction at 1270 feet.
0846064064 2008-05-14 Salt Water Injection Well No Violations Quarterly status check inspection found no violations at this time.
0905386242 2016-05-12 Salt Water Injection Well No Violations I conducted a quarterly status check inspection of this active injection well and the associated surface facilities with Inspector John Fleming. The pump was currently running and a gauge on the injection tubing indicated 800psi. The facility was currently manned by one (1) Stallion employee. A gauge on the annulus between the 4.5 casing and injection tubing showed the annulus to have no pressure (0psi). The gauge was changed out by the employee and still registered 0psi. The permit for this well requires a minimum of 200psi be maintained on the annulus and monitored monthly to help detect leaks under OAC 1501:9-03-07(F). Inspector Fleming requested that Stallion schedule a pressure test for the annulus and that the Division be notified prior to conducting the test. I will wait to here from Stallion.
0911991856 2015-07-16 Salt Water Injection Well No Violations The well and surface facility were inspected. There were no violations found at the time of inspection.
0984102376 2008-08-19 Salt Water Injection Well No Violations Quarterly status check inspection found no violations at this time. The well continues to operate below the maximum allowable injection pressure.
1019386027 2016-03-01 Salt Water Injection Well Violations Noted The injection well and surface facility were inspected. The two inch valve on the casing was split from freezing. There was nothing leaking from the valve at the time. The well owners field supervisor was instructed to replace the valve.
104662198 2014-11-14 0:00 SW No Violations
1067527665 2007-08-07 Salt Water Injection Well No Violations MJ Oil personnel were on site to place the 20 mil plastic liner over the sand base inside of the brine containment area. The area has received recent significant rainfall so the decision was made to leave the south wall of the containment dike open to allow for rainwater drainage. The open dike will also allow access to the containment area for placing the storage tanks. Before placing the tanks, the liner will be covered with six inches of sand and several inches of gravel. After the tanks have been set, the south end of the liner will be rolled back and the containment wall will be built and the liner placed on top.
111478946 2020-1-21 0:00: SW No Violations 0.40
1139881270 2019-10-22 0:00 WR No Violations 3.10
1171770951 2015-09-04 Salt Water Injection Well No Violations The injection well and surface facility were inspected. There were no violations found at the time.
1174070217 2007-03-01 Production Wells No Violations Status check inspection was completed after the owner applied to covert this production well into a salt water disposal well. The well is located in a soybean field approximately 550 west of SR 88 and adjacent to the Geauga County line. The surface equipment at the wellhead has been removed with rods and tubing remaining. The tank battery is located 75 west of SR 88 at the Geauga County line. There is no evidence of lakes, ponds or streams in the immediate vicinity of the well or the existing tank battery. Several private residences (with water wells) are located east and south of the site. The North Coast disposal well (PN 3343) and equipment yard are located 1000 east of the Groselle #2 well.
1180728535 2007-05-22 Salt Water Injection Well No Violations Witness cement bond log for proposed salt water injection well conversion. The bond log indicated that the top of the cement was approximately 100 feet above the proposed injection zone. Additional cement will need to be squeezed into the annular space above the cement top.
1181083204 2007-06-04 Salt Water Injection Well No Violations The purpose of this inspection was to observe the conversion of a production well into a salt water injection well. The first objective was to set a bottom cement plug in the Clinton Sandstone formation. Appalachian Well Surveys set a retainer in the 4-1/2 diameter casing at the depth of 4000. Bubs Well Service ran 2-3/8 diameter tubing with a retainer stinger to bottom. Prior to stinging into the retainer, I pressure tested the 4-1/2 casing. 1540 psi was held on the casing for 15 minutes with zero pressure loss. The service rig stung into the retainer and Universal Well Services mixed and pumped a 29 sack bottom plug thru the tubing. Displacement pressure reached 1000 psi. We waited 10 minutes and tried to pump again. The formation pressured up to 2500 psi. The bottom plug was set. The service rig stung out of the retainer; Universal reverse circulated to flush out any residual cement that was in the casing; then the tubing was pulled. A minimum of 300 of cement is required to be above the top of the Newburg formation for injection requirements. Appalachian Well Surveys ran a cement bond log across the Newburg formation to determine the top of cement. The top of cement was located at 3634. A cement squeeze job was necessary. Appalachian perforated with 3 shots at 3614. Universal pumped on the 4-1/2 casing and established circulation out of the 8-5/8 casing valve. The rate was 3-4 barrel per minute at 1200 psi. Universal mixed and pumped 2 barrels of cement slurry, then blew a hydraulic line. The 2 barrels of cement slurry was circulated out of the 4-1/2 casing. A replacement hydraulic line was brought in from Wooster. Universal mixed and pumped cement a second time; the slurry weight was insufficient; the cement slurry was circulated out of the casing; Universal was out of bulk cement. Another cement truck and bulk truck were called out to the job. I left the location at 0215 hrs on 6-5-2007. I called Craig Norton (330-697-2373), who was overseeing the job for M &
1182177138 2007-06-15 Salt Water Injection Well No Violations Bubs Well Service, Appalachian Survey and Superior were on site to complete the conversion of this Clinton production well into a Newburg salt water disposal well. The cement retainer and Clinton plug was set on June 4, 2007. On June 15, Appalachian perforated with 29 shots from 3898 to 3870, with 45 shots from 3856 to 3814 and with 43 shots from 3798 to 3756. After perforating, the hole was swabbed down and a Baker Lockset packer was run in the hole with 2-7/8 tubing to a depth of 3900. Superior spotted 500 gallons of 28% HCl. The packer was pulled up to 3737, 50 bbl of inhibitor was mixed and circulated and the packer was set. The annular space was pressured to 1000 psi. After five minutes, the pressure was 990 psi and after 15 minutes the pressure was 960 psi, for a total loss of 4%. The MIT passed. The well was then treated with 2500 more gallons of 28% HCl and 1000 bbls of salt water. The formation broke at 1582 psi. The average treating pressure was 2931 psi with initial shut in pressure of 264 psi. The 5 minute shut in pressure was on vacuum.
1228811486 2019-3-13 0:00: SW No Violations 0.80
1256461018 2016-07-13 Salt Water Injection Well No Violations The injection well and surface facility were inspected. The pump was down for repair. There were no violations found at the time.
1266162158 2019-6-25 0:00: SW No Violations 0.40
1267545990 2013-03-07 Salt Water Injection Well No Violations My inspection of the injection well and surface facility found no violations.
1305829019 2011-05-18 Salt Water Injection Well No Violations I went with Bob Worstall to check pressures on this well. There were no violations at this time.
1372773464 2013-07-02 Salt Water Injection Well No Violations A camera was ran down to 1290 feet. There was no sign of any obstruction.
1372790943 2013-07-02 Salt Water Injection Well No Violations The Baker Lokset packer was set at 3731 feet.

Two gallons of corrosion inhibitor were mixed with 40 barrels of fresh water and pumped down the tubing-casing annulus. Five barrels were circulated up the tubing, leaving five barrel on the truck.

A pressure of 1040 psi. was placed on the tubing-casing annulus. During a fifteen minute period, the pressure held without a loss.

1382469469 2007-08-23 Salt Water Injection Well No Violations There has been little activity at this site since the storage tanks were set on August 10. Since then, the electric drop has been made at the road. The tanks still need to be plumbed together, the underground vault installed and the loading pad installed.
1401071955 2010-05-20 Salt Water Injection Well No Violations Quarterly status check inspection found no violations at this time.
1404111837 2017-06-08 Salt Water Injection Well No Violations The injection well and surface facility were inspected. There were no violations found at the time.
1456535334 2014-10-28 Salt Water Injection Well No Violations The injection well and surface facility were inspected. Tubing and casing pressures indicated mechanical integrity. There were no violations found at the time.
1462520530 2009-11-13 Salt Water Injection Well No Violations Quarterly status check inspection found no violations at this time. Met with Saltys on site attendant who reported no problems with the operation. A Stallion tanker truck arrived while we were talking to offload brine.
1468786366 2007-10-22 Salt Water Injection Well No Violations Work is progressing slowly on constructing the disposal facility. The loading pad, drain and concrete vault have been installed (without the required inspector notification). The pump house is under contruction and the storage tanks have been plumbed together.
1483497142 2007-05-21 Salt Water Injection Well No Violations Bubs Well Service is on site to pull rods and tubing prior to running a cement bond log in the well. M-J Oil is proposing to convert this production well into a Newburg salt water injection well.
1497636918 2017-04-13 Salt Water Injection Well No Violations The injection well and surface facility were inspected. The pump was in operation at the time. There were no violations found.
1502793130 2008-02-21 Salt Water Injection Well No Violations Quarterly status check inspection of this salt water injection well found no violations at this time. The well was surrounded by frozen straw bales which prevented access to measure the annulus pressure.
1506428663 2017-09-25 Salt Water Injection Well No Violations Status check inspection of this salt water disposal well. I was on location with DOGRM District Supervisor Steve Ochs to conduct quarterly status checks for the UIC Program. The well was currently injecting at a pressure of 700psi. The pressure on the annulus between the 2.75 injection tubing and 4.5 casing was 320psi. The facility supervisor (Rick) was on location and we discussed operations with him. No violations.
1510851474 2017-04-06 Salt Water Injection Well No Violations The injection well and surface facility were inspected. There were no violations found at the time.
1519308673 2010-03-18 Salt Water Injection Well No Violations Quarterly status check inspection found no violations at this time.
1523495146 2017-05-04 Salt Water Injection Well No Violations The injection well and surface facility were inspected. There were no violations found at the time.
1526603732 2011-11-03 Salt Water Injection Well No Violations I performed the quarterly UIC test on the annulus and the injection. The well was running. There were no violations at this time.
1534149429 2016-03-16 Salt Water Injection Well No Violations The injection well and surface facility were inspected. There was a new two inch valve installed on the casing. The well was in compliance.
1535744776 2013-10-17 Salt Water Injection Well No Violations No violations were found at the time of inspection.
1537925210 2014-05-13 Salt Water Injection Well No Violations A solvent truck was used to pump up the pressure on the tubing/casing annulus. There was pressure of 440 psi. on the tubing and 1015 psi. of pressure on the annulus. There was a decline of 10 psi. on the tubing and no loss on the annulus observed during a fifteen minute period.
1541077542 2018-11-01 Salt Water Injection Well No Violations

-up inspection to gauge the injection tubing will be conducted.

1543240161 2018-11-26 Salt Water Injection Well No Violations I found the injection well in operation on the day of my inspection. There was a facility operator on location. There are identification signs posted. I observed no spills or leaks. A Stallion brine truck arrived on location and had the proper UIC number displayed (#25-368).
1549288976 2019-02-04 Salt Water Injection Well No Violations I was on location to assess Compliance Notice # -
1555940309 2019-4-22 0:00: SW No Violations 0.80
1562484960 2019-2-7 0:00:0 SW No Violations 0.70
1572274707 2019-10-28 0:00 SW No Violations 1.20
1582050269 2010-12-16 Salt Water Injection Well No Violations Quarterly status check inspection found no violations at this time.
1623026476 2016-06-14 Salt Water Injection Well No Violations With 230 psi. of pressure on the tubing, the casing was pressured up to 680 psi. and shut-in. Both pressures remained constant for fifteen minutes, indicating mechanical integrity.
1663500429 2011-05-18 Salt Water Injection Well No Violations Quarterly status check inspection found no violations at this time.
1684395689 2009-08-27 Salt Water Injection Well No Violations Quarterly status check inspection found no violations at this time.
1692446724 2014-07-21 Salt Water Injection Well No Violations The pump was not operating. No violations were found at the time.
1697130417 2007-11-27 Salt Water Injection Well No Violations The well was just activated and started injecting.
1708840972 2008-11-17 Salt Water Injection Well No Violations Quarterly status check inspection found no violations at this time.
1714742232 2020-4-21 0:00: SW No Violations
1720120469 2009-05-12 Salt Water Injection Well No Violations Quarterly status check inspection found no violations at this time.
1814704198 2017-12-12 Salt Water Injection Well No Violations I found the injection and facility in good repair on the day of my inspection. I observed no leaks or spills. An identification sign is posted at the facility. There are no violations at this time.
1819235146 2013-07-01 Salt Water Injection Well No Violations I was on location to inspect workover operations at this disposal well. Inspectors Steve Ochs, Rick Skidmore and ODNR interns were on location as well. Whipstocks service rig was tripping tubing out of the hole. They thought they had hit an obstruction when running into the hole and Stallion personel decided to run a downhole camera tomorrow to see if there was anything inside the casing. No violations.
1888309800 2013-05-15 Salt Water Injection Well No Violations I witnessed a mechanical integrity test. The annular pressure went from 540 psi. to 260 psi., in fifteen minutes. The well failed the test.
1965303806 2012-07-25 Salt Water Injection Well No Violations My inspection of the well site and injection facility found no violations. The pump was operating at the time.
1984224904 2016-09-01 Salt Water Injection Well No Violations The injection well and surface facility were inspected. There were no violations found at the time.
2011417827 2019-02-01 Salt Water Injection Well Violations Noted I found the injection well operating and over the maximum allowable pressure during my inspection. There was a facility operator on location. I instructed the facility operator to reduce the injection well pressure immediately. The facility operator reduced the operating pressure on the injection well. I informed the facility a compliance notice will be issued for operating over pressure. Identification signs are posted. I observed no leaks or spills. A follow-up inspection will be conducted by February 4, 2019.
2049205924 2007-08-10 Salt Water Injection Well No Violations M-J Oil personnel were on site to place eight 210 bbl storage tanks inside the containment area. The liner was protected with a layer of sand. The next action will close the southern containment wall and extend the liner over the dike wall.
2078464824 2015-04-29 Salt Water Injection Well No Violations The well and surface facility were inspected. The well was equipped with a new two inch valve on the casing. There were no violations found at the time of inspection.
2085607264 2013-05-15 Salt Water Injection Well No Violations I was on location with UIC Inspector Steve Ochs to witness a mechanical integrity test (MIT) requested by Stallion personell. Stallion believed that the tubing packer had failed and was leaking into the annulus between the tubing and the 4.5 casing. 550psi was placed on the pipe at 8:19am and at 8:25am, the pressure had dropped to 400psi. By 8:29am, the pressure was down to 340psi and failed the MIT required by OAC 1501:9-3-07 which allows for no more than a 5% decline over a 15 minute testing period. Steve Ochs verbally suspended injection operations and will issue a compliance notice that operations may not commence until the well is repaired and Stallion demonstrates mechanical integrity.
2146572833 2016-03-26 Salt Water Injection Well No Violations The injection well and surface facility were inspected. There were no violations found at the time.
364493409 2012-9-5 0:00:0 SW No Violations
379874124 2014-3-18 0:00: SW No Violations
416148764 2017-6-19 0:00: SW No Violations
435425214 2015-5-6 0:00:0 SW No Violations
476656976 2018-6-25 0:00: SW No Violations 0.40
517951705 2018-11-14 0:00 SW No Violations 0.30
606543304 2011-8-4 0:00:0 SW No Violations
635207594 2017-3-10 0:00: SW No Violations
679506042 2017-2-17 0:00: SW No Violations
71613901 2015-6-4 0:00:0 SW No Violations
730856680 2018-8-9 0:00:0 SW No Violations 1.00
73718903 2016-12-30 0:00 SW No Violations
839252422 2014-9-23 0:00: SW No Violations
839371641 2013-7-1 0:00:0 SW No Violations
846064064 2008-5-14 0:00: SW No Violations
905386242 2016-5-12 0:00: SW No Violations 0.50
911991856 2015-7-16 0:00: SW No Violations
984102376 2008-8-19 0:00: SW No Violations
iDIAN00039 1998-09-09 Preliminary Restoration No Violations
iDIAN000392 1998-9-9 0:00:0 PL No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0410687730 US-OH-124346 2019-04-08 Failure to report disposal fees
0607116022 US-OH-126864 2016-04-22 Exceeding maximum allowable injection pressure
1019386027 US-OH-100543 2016-04-22 Pollution/Contamination
2011417827 US-OH-120418 2019-02-08 9-3-07(D) Exceeding maximum allowable injection pressure

For data sources see[9]

References