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34-133-24276

Well Details

Well ID: 34-133-24276
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Country: United States
State: Ohio
County: Portage
Municipality: Atwater Township
Operator Name: WILLIAM S MILLER INC
Well Pad ID:
Farm/Lease Name: MYERS G & L UNIT
License Status: Final Restoration
License Date: 2004-11-02
Spud Date: 2003-09-04
Spud Drilling Contractor: LANDOGS DRILLING
Final Drill Date: 2003-09-13
Well Total Depth: 7617.00 ft
Configuration: Vertical
Latitude: 41.020000
Longitude: -81.140000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2003-05-23 2050 ORION PETRO CORP Proposed Formation ROSE RUN (MAY NOT PRODUCE CLINTON) Issued Date 5/23/2003 Expired Date 5/22/2004 6:00:00 AM
Inspector Comments Cement Job 2003-09-04 11-3/4" conductor was set at 122' on 9/04/03. Ran 18 joints of new, R-3, 23#, 8-5/8" casing (770) set at 780 on 9/05/03. Ran 10 sacks of gel ahead. Good circulation with cement to surface. Plug down at 05:00. Pits lined and in good condition.Cement Ticket Notes Inspector Reporting WORSTALL BOB
Original Spud 2003-09-04
Completed 2003-09-13
Reached Total Depth 2003-09-13
Completion Report Received 2003-10-09
Change of Owner 2003-12-22 Operator changed from 2050, ORION PETRO CORP to 2512, MILLER WILLIAM S INC
APP 2004-11-02 Proposed Formations:TREMPEALEAU, Issued Date:11/2/2004, Expired Date:11/2/2005 6:00:00 AM, Drilling unit acres:51.68, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2004-12-30
Construction Permit Expires 2005-11-02
Record Last Modified 2015-09-24

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2003-11-20 7514 7518 13
2003-11-20 7524 7532 25
7492 7504 37
7514 7518 13
7524 7532 25
7492 7504 37
2003-11-20 7492 7504 37

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 15 57600 Gal 20000 1000 GALLONS HCL ACID…..DRY AFTER TREATMENT….TO BE P&A

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2003 ORION PETRO CORP 0.00 0.00 0
2004 WILLIAM S MILLER INC 968.00 47.00 180

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2003 ORION PETRO CORP Brine 4276 0
2004 WILLIAM S MILLER INC Brine 8363 180

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-888097663 2003-9-8 0:00:0 DD No Violations
-999568745 2003-9-16 0:00: DD No Violations
0219246369 2003-12-02 Production Wells No Violations Status check inspection for preliminary restoration for the well spudded on September 4, 2003. The pits have been closed and the rough graded. According to Buzz West, the well will be transferred to new owners in the near future. No violations at this time.
0888097663 2003-09-08 Drill / Deepen / Reopen No Violations Status check inspection of drilling activity - no violations at this time.
0999568745 2003-09-16 Drill / Deepen / Reopen No Violations The drilling rig has moved off and the pits were being pumped down by Ray Pander Trucking. No violations.
1300772585 2008-01-15 Final Restoration No Violations Final restoration is approved.
219246369 2003-12-2 0:00: PW No Violations

For data sources see[9]

References