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Well ID: 34-139-20059 | Loading map...
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Country: United States | |
State: Ohio | |
County: Richland | |
Municipality: Monroe Township | |
Operator Name: COLUMBIA GAS TRANSMISSION LLC | |
Well Pad ID: | |
Farm/Lease Name: DARLING JEANNIE | |
License Status: Storage Well | |
License Date: | |
Spud Date: 1947-11-26 | |
Spud Drilling Contractor: | |
Final Drill Date: | |
Well Total Depth: | |
Configuration: Vertical | |
Latitude: 40.650000 | |
Longitude: -82.370000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Record Last Modified | 2016-03-07 | RBDMS Rec |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
2016-06-01 | H2O | 0 | 316 Bbl | 24269 | Universal Well Services Inc. | Universal Well Service performed a nitrogen assisted cross linked gel fluid fracture stimulation on the well. The surface production annulus was open during the job and no returns were observed. The job went smoothly. 82,168 cubic feet of nitrogen were pumped with the fluid. |
For data sources see[3]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1008334138 | 2016-3-21 0:00: | SO | No Violations | 1.00 |
-1799182877 | 2020-3-3 0:00:0 | SO | No Violations | |
-1821988484 | 2015-1-14 0:00: | SO | No Violations | 0.50 |
-2144615248 | 2016-3-24 0:00: | SO | No Violations | 4.00 |
-54819450 | 2018-3-30 0:00: | SO | No Violations | |
-732427932 | 2016-2-18 0:00: | SO | No Violations | 1.00 |
0054819450 | 2018-03-30 | Storage Well | No Violations | ID is posted and the location is maintained. The annulus is shut in. The well is equipped with a separator. |
0242825805 | 2016-02-24 | Storage Well | No Violations | The well has been equipped with a new API wellhead. The rig is off location and the workover is completed. The pit has been closed and the location is rough graded. |
0523986264 | 2016-06-01 | Work Over Reconditioning | No Violations | The operator conducted fracture stimulation on the well. See the stimulation report for details. |
0732427932 | 2016-02-18 | Storage Well | No Violations | The rig is pulling drill pipe from the well. Cleanout of the bridge plug is completed. Workover operations will be completed in the next few days. |
0872463592 | 2014-03-12 | Storage Well | No Violations | ID posted, location maintained. The swage on top of the 5 inch has gas leaking around the threads. |
1008334138 | 2016-03-21 | Storage Well | No Violations | Brine water has accumulated around the wellhead. Bubbles were seen coming up through the water and foam is coming from the surface production annulus. Columbia Gas was contacted and responded to the location to investigate. The annulus was shut in by company personnel. |
1821988484 | 2015-01-14 | Storage Well | No Violations | ID posted, location maintained. |
2085932101 | 2017-10-24 | Storage Well | No Violations | ID is posted and the location is maintained. The well is shut in at the gate valve; the annulus is open. The well is equipped with a separator. |
2108331814 | 2019-04-08 | Storage Well | No Violations | Identification is posted . Drip connected to wellhead. Wellsite is maintained. |
2144615248 | 2016-03-24 | Storage Well | No Violations | The operator excavated around the wellhead to the top of the new surface casing. No brine is coming up around the cemented casing. The operator had a culvert running from the wellhead to a pit for workover operations. Water was found to be leaking through the culvert. The culvert was excavated and removed and the trench was backfilled and compacted. The fluid was coming from the backfilled pit. The foam coming from the surface production annulus was corrosion inhibitor. |
242825805 | 2016-2-24 0:00: | SO | No Violations | 0.50 |
523986264 | 2016-6-1 0:00:0 | WR | No Violations | 4.00 |
872463592 | 2014-3-12 0:00: | SO | No Violations | 0.50 |
For data sources see[4]