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34-139-20059

Well Details

Well ID: 34-139-20059
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Country: United States
State: Ohio
County: Richland
Municipality: Monroe Township
Operator Name: COLUMBIA GAS TRANSMISSION LLC
Well Pad ID:
Farm/Lease Name: DARLING JEANNIE
License Status: Storage Well
License Date:
Spud Date: 1947-11-26
Spud Drilling Contractor:
Final Drill Date:
Well Total Depth:
Configuration: Vertical
Latitude: 40.650000
Longitude: -82.370000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Record Last Modified 2016-03-07 RBDMS Rec

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
2016-06-01 H2O 0 316 Bbl 24269 Universal Well Services Inc. Universal Well Service performed a nitrogen assisted cross linked gel fluid fracture stimulation on the well. The surface production annulus was open during the job and no returns were observed. The job went smoothly. 82,168 cubic feet of nitrogen were pumped with the fluid.

For data sources see[3]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1008334138 2016-3-21 0:00: SO No Violations 1.00
-1799182877 2020-3-3 0:00:0 SO No Violations
-1821988484 2015-1-14 0:00: SO No Violations 0.50
-2144615248 2016-3-24 0:00: SO No Violations 4.00
-54819450 2018-3-30 0:00: SO No Violations
-732427932 2016-2-18 0:00: SO No Violations 1.00
0054819450 2018-03-30 Storage Well No Violations ID is posted and the location is maintained. The annulus is shut in. The well is equipped with a separator.
0242825805 2016-02-24 Storage Well No Violations The well has been equipped with a new API wellhead. The rig is off location and the workover is completed. The pit has been closed and the location is rough graded.
0523986264 2016-06-01 Work Over Reconditioning No Violations The operator conducted fracture stimulation on the well. See the stimulation report for details.
0732427932 2016-02-18 Storage Well No Violations The rig is pulling drill pipe from the well. Cleanout of the bridge plug is completed. Workover operations will be completed in the next few days.
0872463592 2014-03-12 Storage Well No Violations ID posted, location maintained. The swage on top of the 5 inch has gas leaking around the threads.
1008334138 2016-03-21 Storage Well No Violations Brine water has accumulated around the wellhead. Bubbles were seen coming up through the water and foam is coming from the surface production annulus. Columbia Gas was contacted and responded to the location to investigate. The annulus was shut in by company personnel.
1821988484 2015-01-14 Storage Well No Violations ID posted, location maintained.
2085932101 2017-10-24 Storage Well No Violations ID is posted and the location is maintained. The well is shut in at the gate valve; the annulus is open. The well is equipped with a separator.
2108331814 2019-04-08 Storage Well No Violations Identification is posted . Drip connected to wellhead. Wellsite is maintained.
2144615248 2016-03-24 Storage Well No Violations The operator excavated around the wellhead to the top of the new surface casing. No brine is coming up around the cemented casing. The operator had a culvert running from the wellhead to a pit for workover operations. Water was found to be leaking through the culvert. The culvert was excavated and removed and the trench was backfilled and compacted. The fluid was coming from the backfilled pit. The foam coming from the surface production annulus was corrosion inhibitor.
242825805 2016-2-24 0:00: SO No Violations 0.50
523986264 2016-6-1 0:00:0 WR No Violations 4.00
872463592 2014-3-12 0:00: SO No Violations 0.50

For data sources see[4]

References