X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-139-20201

Well Details

Well ID: 34-139-20201
Loading map...
Country: United States
State: Ohio
County: Richland
Municipality: Worthington Township
Operator Name: COLUMBIA GAS TRANSMISSION LLC
Well Pad ID:
Farm/Lease Name: SNYDER HARVEY C
License Status: Storage Well
License Date: 1960-12-29
Spud Date: 1961-01-13
Spud Drilling Contractor: CO TOOLS
Final Drill Date: 1961-03-07
Well Total Depth: 2471.00 ft
Configuration: Vertical
Latitude: 40.620000
Longitude: -82.410000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Inspector Comments Cement Job 1961-01-13 Colubia Gas Transmission Co. Rig. Re work Gas storage field well. Cement ticket mailed. New seven inch casing run and cemented in place. Original eight inch surface casing 324 ft. pulled and recovered. Job was not witnessed due to holiday. Job ticket summery states no return.Cement Ticket Notes Inspector Reporting
Original Spud 1961-01-13 Colubia Gas Transmission Co. Rig. Re work Gas storage field well. Cement ticket mailed. New seven inch casing run and cemented in place. Original eight inch surface casing 324 ft. pulled and recovered. Job was not witnessed due to holiday. Job ticket summery states no return.Colubia Gas Transmission Co. Rig. Re work Gas storage field well. Cement ticket mailed. New seven inch casing run and cemented in place. Original eight inch surface casing 324 ft. pulled and recovered. Job was not witnessed due to holiday. Job ticket summery states no return.Colubia Gas Transmission Co. Rig. Re work Gas storage field well. Cement ticket mailed. New seven inch casing run and cemented in place. Original eight inch surface casing 324 ft. pulled and recovered. Job was not witnessed due to holiday. Job ticket summery states no return.Colubia Gas Transmission Co. Rig. Re work Gas storage field well. Cement ticket mailed. New seven inch casing run and cemented in place. Original eight inch surface casing 324 ft. pulled and recovered. Job was not witnessed due to holiday. Job ticket summery states no return. STORAGE, GL=1114.5 FDT=2ND.
Completed 1961-03-07 Colubia Gas Transmission Co. Rig. Re work Gas storage field well. Cement ticket mailed. New seven inch casing run and cemented in place. Original eight inch surface casing 324 ft. pulled and recovered. Job was not witnessed due to holiday. Job ticket summery states no return.Colubia Gas Transmission Co. Rig. Re work Gas storage field well. Cement ticket mailed. New seven inch casing run and cemented in place. Original eight inch surface casing 324 ft. pulled and recovered. Job was not witnessed due to holiday. Job ticket summery states no return.Colubia Gas Transmission Co. Rig. Re work Gas storage field well. Cement ticket mailed. New seven inch casing run and cemented in place. Original eight inch surface casing 324 ft. pulled and recovered. Job was not witnessed due to holiday. Job ticket summery states no return.Colubia Gas Transmission Co. Rig. Re work Gas storage field well. Cement ticket mailed. New seven inch casing run and cemented in place. Original eight inch surface casing 324 ft. pulled and recovered. Job was not witnessed due to holiday. Job ticket summery states no return. STORAGE, GL=1114.5 FDT=2ND.
Reached Total Depth 1961-03-07 Colubia Gas Transmission Co. Rig. Re work Gas storage field well. Cement ticket mailed. New seven inch casing run and cemented in place. Original eight inch surface casing 324 ft. pulled and recovered. Job was not witnessed due to holiday. Job ticket summery states no return.Colubia Gas Transmission Co. Rig. Re work Gas storage field well. Cement ticket mailed. New seven inch casing run and cemented in place. Original eight inch surface casing 324 ft. pulled and recovered. Job was not witnessed due to holiday. Job ticket summery states no return.Colubia Gas Transmission Co. Rig. Re work Gas storage field well. Cement ticket mailed. New seven inch casing run and cemented in place. Original eight inch surface casing 324 ft. pulled and recovered. Job was not witnessed due to holiday. Job ticket summery states no return.Colubia Gas Transmission Co. Rig. Re work Gas storage field well. Cement ticket mailed. New seven inch casing run and cemented in place. Original eight inch surface casing 324 ft. pulled and recovered. Job was not witnessed due to holiday. Job ticket summery states no return. STORAGE, GL=1114.5 FDT=2ND.
Completion Report Received 1961-03-17 Colubia Gas Transmission Co. Rig. Re work Gas storage field well. Cement ticket mailed. New seven inch casing run and cemented in place. Original eight inch surface casing 324 ft. pulled and recovered. Job was not witnessed due to holiday. Job ticket summery states no return.Colubia Gas Transmission Co. Rig. Re work Gas storage field well. Cement ticket mailed. New seven inch casing run and cemented in place. Original eight inch surface casing 324 ft. pulled and recovered. Job was not witnessed due to holiday. Job ticket summery states no return.Colubia Gas Transmission Co. Rig. Re work Gas storage field well. Cement ticket mailed. New seven inch casing run and cemented in place. Original eight inch surface casing 324 ft. pulled and recovered. Job was not witnessed due to holiday. Job ticket summery states no return.Colubia Gas Transmission Co. Rig. Re work Gas storage field well. Cement ticket mailed. New seven inch casing run and cemented in place. Original eight inch surface casing 324 ft. pulled and recovered. Job was not witnessed due to holiday. Job ticket summery states no return. STORAGE, GL=1114.5 FDT=2ND.
Record Last Modified 2017-02-15 Colubia Gas Transmission Co. Rig. Re work Gas storage field well. Cement ticket mailed. New seven inch casing run and cemented in place. Original eight inch surface casing 324 ft. pulled and recovered. Job was not witnessed due to holiday. Job ticket summery states no return.Colubia Gas Transmission Co. Rig. Re work Gas storage field well. Cement ticket mailed. New seven inch casing run and cemented in place. Original eight inch surface casing 324 ft. pulled and recovered. Job was not witnessed due to holiday. Job ticket summery states no return.Colubia Gas Transmission Co. Rig. Re work Gas storage field well. Cement ticket mailed. New seven inch casing run and cemented in place. Original eight inch surface casing 324 ft. pulled and recovered. Job was not witnessed due to holiday. Job ticket summery states no return.Colubia Gas Transmission Co. Rig. Re work Gas storage field well. Cement ticket mailed. New seven inch casing run and cemented in place. Original eight inch surface casing 324 ft. pulled and recovered. Job was not witnessed due to holiday. Job ticket summery states no return. STORAGE, GL=1114.5 FDT=2ND.

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
0 0 0
Not Treated 0 0 0

For data sources see[3]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1154423359 2014-4-22 0:00: SO No Violations 0.50
-155576457 2015-12-8 0:00: SO No Violations 0.50
-1644030478 2016-12-22 0:00 SO No Violations 0.50
-2107454622 2017-12-7 0:00: SO No Violations
-45513462 2002-10-17 0:00 DD No Violations
-94676713 2002-10-10 0:00 DD No Violations
0045513462 2002-10-17 Drill / Deepen / Reopen No Violations Site inspection. Columbia gas redrilled well. Drilling and resetting activities completed, beginning to pull drill rods out of well.
0094676713 2002-10-10 Drill / Deepen / Reopen No Violations Inspect drilling site. Drilling activity to refit well for storage capabilities. Surface cement job will be performed on Monday October 14, 2002.
0155576457 2015-12-08 Storage Well No Violations ID is posted and the location is maintained. The well is shut in at the gate valve; the annulus is open.
0288378164 2002-11-22 Drill / Deepen / Reopen No Violations Well inspection. Well not in service. Pits open.
1082545735 2020-3-9 0:00:0 SO No Violations
1154423359 2014-04-22 Storage Well No Violations ID posted, location maintained.
1529040527 2019-04-23 Storage Well No Violations Identification is posted . Drip is connected to the well. Remote electronic pressure sensing equipment attached to annulus and wellhead. Area maintained around wellsite.
1644030478 2016-12-22 Storage Well No Violations ID is posted and the location is maintained. The well is shut in at the gate valve; the annulus is open. The well is equipped with a separator.
1979755394 2018-12-04 Storage Well No Violations Identification is posted. No violations observed. Large drip installed at well. Access road is clear.
2107454622 2017-12-07 Storage Well No Violations ID is posted and the location is maintained. The well is shut in at the gate valve; the annulus is open. The well is equipped with a separator.
288378164 2002-11-22 0:00 DD No Violations

For data sources see[4]

References