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34-141-20045

Well Details

Well ID: 34-141-20045
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Country: United States
State: Ohio
County: Ross
Municipality: Colerain Township
Operator Name: MURPHY OIL COMPANY INC
Well Pad ID:
Farm/Lease Name: KELLENBERGER UNIT
License Status: Final Restoration
License Date: 2013-06-28
Spud Date: 1995-12-27
Spud Drilling Contractor: WARREN DRLG
Final Drill Date: 1996-01-06
Well Total Depth: 3555.00 ft
Configuration: Vertical
Latitude: 39.420000
Longitude: -82.810000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1995-06-12 516 MURPHY OIL CO GeoDate 6/12/95
Oil and Gas 1995-06-12 Issued Date 6/12/95 Expired Date 6/11/96 Acres 0040000 Tool Type RTAF Proposed Formation TR thru CPRG Proposed Depth 03555 Proposed Drill Depth 03555
Original Spud 1995-12-27
Completed 1996-01-06
Reached Total Depth 1996-01-06
Completion Report Received 1996-02-13
Annular Disposal Well 1996-04-25
Revocation 2006-08-01
APP 2013-06-28 Proposed Formations:ROSE RUN, Issued Date:6/28/2013, Expired Date:6/28/2015 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:TAAD, Proposed Well Class:
Plugged/Abandoned 2014-05-19
Last Compliance Report 2014-09-09
Construction Permit Expires 2015-06-28
Record Last Modified 2019-06-05

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1998-03-19 3324 3370 76
3324 3370 76
2006-09-11 3352 3356 16
3352 3356 16
3324 3370 76
2006-09-11 3365 3370 2

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
ACID 15 950 Gal 0

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1996 MURPHY OIL COMPANY INC 11938.00 0.00 240
1997 MURPHY OIL COMPANY INC 5793.00 0.00 365
1998 MURPHY OIL COMPANY INC 4329.00 0.00 365
2001 MURPHY OIL COMPANY INC 2346.00 0.00 365
2002 MURPHY OIL COMPANY INC 1770.00 0.00 365
2003 MURPHY OIL COMPANY INC 1127.00 0.00 365
2004 MURPHY OIL COMPANY INC 1028.00 0.00 365
2005 MURPHY OIL COMPANY INC 635.00 0.00 365
2006 MURPHY OIL COMPANY INC 687.00 0.00 365
2007 MURPHY OIL COMPANY INC 479.00 0.00 365
2008 MURPHY OIL COMPANY INC 53.00 0.00 60
2009 MURPHY OIL COMPANY INC 390.00 0.00 80
2010 MURPHY OIL COMPANY INC 0.00 0.00 0
2011 MURPHY OIL COMPANY INC 0.00 0.00 0
2014 MURPHY OIL COMPANY INC 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1996 MURPHY OIL COMPANY INC Brine 0 240
1997 MURPHY OIL COMPANY INC Brine 0 365
1998 MURPHY OIL COMPANY INC Brine 0 365
2001 MURPHY OIL COMPANY INC Brine 0 365
2002 MURPHY OIL COMPANY INC Brine 0 365
2003 MURPHY OIL COMPANY INC Brine 242 365
2004 MURPHY OIL COMPANY INC Brine 0 365
2005 MURPHY OIL COMPANY INC Brine 0 365
2006 MURPHY OIL COMPANY INC Brine 0 365
2007 MURPHY OIL COMPANY INC Brine 0 365
2008 MURPHY OIL COMPANY INC Brine 0 60
2009 MURPHY OIL COMPANY INC Brine 0 80
2010 MURPHY OIL COMPANY INC Brine 0 0
2011 MURPHY OIL COMPANY INC Brine 0 0
2014 MURPHY OIL COMPANY INC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1048222520 2014-8-19 0:00: FR No Violations 5.00
-1633759868 2014-4-10 0:00: AM No Violations 0.20
-1756188272 2014-5-7 0:00:0 PB No Violations 11.00
-2009581042 2012-5-24 0:00: AD No Violations 3.00
-790121628 2013-6-7 0:00:0 PW No Violations 2.50
0283274710 2012-10-24 Production Wells No Violations FOLLOW UP TO NOV # 1356370186 There is no (0) well production reported in RBDMS for the last two reporting periods 2010 and 2011. According to 1509:.062A; Nonproduction; Well shall be plugged or produced. At the intermediate casing head, the packer between this casing and production tubing is leaking small amounts of gas. 1501:9-9-05(A)1/1509:20 Well insufficiently equipped to prevent escape of oil and gas. Need to stop the release of gas to the environment.
0435941094 2012-10-24 Annular Disposal No Violations Followed up on Andy Thomas inspection on May 24, 2012. The operator put a ball valve on the vent line as Andy requested. Well is presently shut in. At the intermediate casing head, the packer between this casing and production tubing is leaking small amounts of gas.
0790121628 2013-06-07 Production Wells No Violations This is a follow up inspection on the NOV of this well. Nothing has changed at this well. Road access to this well has been blocked by the new landowners according to John Murphy. This and other circumstances have forced him to obtain a permit to plug this well. In light of this I will not pursue further action. I will continue to monitor the progress of this situation to ensure his company has applied for the permit.
1048222520 2014-08-19 Final Restoration No Violations Final restoration inspection. The well has been plugged and the site is planted in crops. The production equipment has been removed. The final restoration is passed.
1166461318 2006-12-13 Annular Disposal No Violations Checked AD for Columbus, AD not in use.
1272343147 2007-04-26 Production Wells No Violations No violations were noted.
1356370186 2012-10-24 Production Wells Violations Noted There is no (0) well production reported in RBDMS for the last two reporting periods 2010 and 2011. According to 1509:.062A; Nonproduction; Well shall be plugged or produced. At the intermediate casing head, the packer between this casing and production tubing is leaking small amounts of gas. 1501:9-9-05(A)1/1509:20 Well insufficiently equipped to prevent escape of oil and gas. Need to stop the release of gas to the environment.
1397162095 2014-04-10 Production Wells No Violations Upon inspection, this well is still shut in and the production records for this well show 0 for the past 3 years. I contacted John Murphy and explained that the well needs to be either put into production, or plugged in the next 60 days. John stated that Murphy Oil Co. has the plugging permit for this well and they plan on having Knox Energy plug the well as soon as the ground firms up.
1399400491 2014-05-06 Plug / Plug Back No Violations Knox Energy is on site tripping out tubing. Separator and tanks have been removed. No fluid was found in the well bore. Bottom plug will be set on 05/07/2014 by the bull head method.
1633759868 2014-04-10 Administrative Inspection No Violations I spoke on the phone with John Murphy of Murphy Oil Co. at 10:35 a.m., and we discussed any plans to plug or produce this well. John explained that Murphy Oil Co. has the plugging permit for this well and they have contracted Knox Energy to perform the plugging operations. John stated that they plan on having the well plugged as soon as the ground firms up and before the field it sits in is planted for the year.
1756188272 2014-05-07 Plug / Plug Back No Violations Knox Energy and a Cemenco on site. Bottom plug set using the bullhead method. After the plug was landed, the well began to unload the salt water used to follow the plug. I spoke with Bill Mitten and told Bill I would require the bottom plug to be tagged. The cement was tagged at 2955.
2009581042 2012-05-24 Annular Disposal No Violations Performed inspection for the purpose of checking to make sure that the annular disposal was not in use. Annulus had fittings in it and a 1 inch black plastic line that ran to the top of a 50 barrel tank. This was used as a vent. The 1 inch line was cracked. I contacted Mr John Murphy at 3:56 pm and he stated that he would have his pumper put a valve on it with a plug.
2031130193 2014-05-08 Plug / Plug Back No Violations Knox Energy on site plugging this rose run well. Formation cementing on site at 1431 hours. 71 barrel of oil was circulated out of the well, Knox Energy geologist believes it is coming from the Queenston formation. They have stopped plugging the well at 1455. There is 300 of cement covering the Clinton formation. I told John Murphy he would need to apply for a plug back permit.
2062070540 2014-05-19 Plug / Plug Back No Violations Knox Energy on site to finish plugging this well. Bottom plug and Clinton sandstone plug set on 05/07/14. Lime plug, bottom of surface and surface plug set. Well was cut off and identification plate was placed on the well pipe.
283274710 2012-10-24 0:00 PW No Violations
435941094 2012-10-24 0:00 AD No Violations 2.00
iDIAN00386 2000-05-02 Preliminary Restoration No Violations
iDIAN003863 2000-5-2 0:00:0 PL No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1356370186 US-OH-110306 2013-01-02 Well insufficiently equipped to prevent escape of oil and gas
1356370186 US-OH-110307 2013-01-02 Well shall be plugged
1356370186 US-OH-110308 2013-01-02 Nonproduction; well shall be plugged or placed in temporary inactive status
1356370186 US-OH-110309 2013-01-02 Statement of annual production not filed

For data sources see[9]

References