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34-143-20324

Well Details

Well ID: 34-143-20324
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Country: United States
State: Ohio
County: Sandusky
Municipality: Rice Township
Operator Name: FO ENERGY LLC
Well Pad ID:
Farm/Lease Name: K & B KING UNIT
License Status: Producing
License Date: 2014-08-19
Spud Date: 2014-10-22
Spud Drilling Contractor: POULSON DRILLING
Final Drill Date: 2014-10-23
Well Total Depth: 1657.00 ft
Configuration: Vertical
Latitude: 41.420000
Longitude: -83.090000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2014-08-19 Proposed Formations:TRENTON-KNOX, Issued Date:8/19/2014, Expired Date:8/18/2016 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:EDPW
Reached Total Depth 2014-10-23
Completion Report Received 2015-03-13
Change of Owner 2015-11-03 Operator changed from 7626, M & M ROYALTY LTD to 9312, FO ENERGY LLC
Construction Permit Expires 2016-08-18
Record Last Modified 2017-10-23

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2015-10-29 1425 1470 72
1425 1470 72
1425 1470 72

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
2014-11-07 H2O 0 1364 Bbl 20050 Universal Well Services Inc. Witnessed stimulation of well by Universal Well Services Inc. Formation broke down at 1750 PSI. Used 1364 BBLs of water with 20050 lbs of propant sand and 250 gallons of Hydrochloric Acid.

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2015 M & M ROYALTY LTD 0.00 0.00 0
2016 FO ENERGY LLC 5.00 433.00 75
2017 FO ENERGY LLC 484.00 1287.00 365
2018 FO ENERGY LLC 1448.00 1338.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2015 FO ENERGY LLC Brine 0 0
2016 FO ENERGY LLC Brine 23 75
2017 FO ENERGY LLC Brine 0 365
2018 FO ENERGY LLC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-2063096663 2017-3-27 0:00: PW No Violations
0292340972 2017-12-20 Production Wells No Violations Identification is posted at well. Recent excavation between storage tanks and well indicates that well is not producing enough natural gas to run natural gas motor on pumpjack. One inch plastic line that was recently installed and is now connected to the natural gas pipeline.
1189244846 2015-02-19 Production Wells No Violations Did follow-up on oil spill from previous day. Contractor removed storage tanks from dike area and removed oil soaked gravel and oil from dike area. Inspection revealed oil cleanup complete.
1424695169 2015-02-17 Preliminary Restoration No Violations During inspection for preliminary restoration, found broken valve at storage tanks. Contacted operator and met with operator (Matt) about clean up. Will have contractor at site tomorrow to clean up. Approximate amount of oil loss was less than a barrel and oil did not leave dike area.
1429714418 2015-04-22 Production Wells No Violations Cleanup from brokrn valve on 100 BBl tank complete. Owner removed oil from inside dike and also gravel. Replaced gravel and ell is capable of production. Identification is posted at site.
2063096663 2017-03-27 Production Wells No Violations Identification is posted and no observed violations at the present time.
292340972 2017-12-20 0:00 PW No Violations

For data sources see[9]

References