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34-151-20230

Well Details

Well ID: 34-151-20230
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Country: United States
State: Ohio
County: Stark
Municipality: Bethlehem Township
Operator Name: DOVER ATWOOD CORP.
Well Pad ID:
Farm/Lease Name: BENDER ETTA F ET AL
License Status: Producing
License Date:
Spud Date: 2012-09-12
Spud Drilling Contractor:
Final Drill Date: 1943-01-29
Well Total Depth: 4517.00 ft
Configuration: Vertical
Latitude: 40.730000
Longitude: -81.460000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Completed 1943-01-29 QUAD=DOVER
Reached Total Depth 1943-01-29 QUAD=DOVER
CO 1995-04-20 182 BELDEN & BLAKE CO GeoDate
Plugging Plan Approved 1998-02-03 QUAD=DOVER
Change of Owner 2007-04-27 Operator changed from 182, BELDEN & BLAKE CORPORATION to 7578, ENERVEST OPERATING LLC
Change of Owner 2012-08-31 Operator changed from 7578, ENERVEST OPERATING L to 5935, DOVER ATWOOD CORP.
Completion Report Received 2013-09-23 QUAD=DOVER
Record Last Modified 2017-02-15 QUAD=DOVER

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1998-02-03 4481 4511 60
4481 4511 60
4481 4511 60

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
2012-09-19 H2O 0 76113 Gal 0 Producers Service Corporation Brian Levengood (Dover Atwood Corp.) called to discuss the proposed work over/reconditioning plan. This well was completed in 1943 and has five casing strings (10”, 8”, 6”, 5”, & 3”). A cement bond log was completed on 09/12/12. The original perforations (4481’ to 4511’) were covered with sand to prevent cement from entering this zone. Four perforations were shot at 4400’ in order to squeeze cement behind the 3” casing string and into the annulus of the 5” casing. 60 sac
0 0 0

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 DOMINION EAST OHIO 20.00 0.00 0
1985 DOMINION EAST OHIO 0.00 0.00 365
1986 DOMINION EAST OHIO 0.00 0.00 365
1987 DOMINION EAST OHIO 17.00 0.00 0
1988 DOMINION EAST OHIO 20.00 0.00 0
1989 DOMINION EAST OHIO 18.00 0.00 0
1990 DOMINION EAST OHIO 13.00 0.00 365
1991 DOMINION EAST OHIO 0.00 0.00 365
1992 DOMINION EAST OHIO 1.00 0.00 365
1993 DOMINION EAST OHIO 1.00 0.00 365
1994 DOMINION EAST OHIO 1.00 0.00 365
1995 DOMINION EAST OHIO 0.00 0.00 61
1998 DOVER ATWOOD CORP. 0.00 0.00 0
1999 DOVER ATWOOD CORP. 0.00 0.00 0
2000 DOVER ATWOOD CORP. 0.00 0.00 365
2012 DOVER ATWOOD CORP. 0.00 0.00 0
2013 DOVER ATWOOD CORP. 1643.00 360.00 365
2014 DOVER ATWOOD CORP. 992.00 277.00 365
2015 DOVER ATWOOD CORP. 988.00 192.00 365
2016 DOVER ATWOOD CORP. 958.00 193.00 365
2017 DOVER ATWOOD CORP. 649.00 173.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 DOMINION EAST OHIO Brine 0 0
1985 DOMINION EAST OHIO Brine 0 365
1986 DOMINION EAST OHIO Brine 0 365
1987 DOMINION EAST OHIO Brine 0 0
1988 DOMINION EAST OHIO Brine 0 0
1989 DOMINION EAST OHIO Brine 16 0
1990 DOMINION EAST OHIO Brine 0 365
1991 DOMINION EAST OHIO Brine 0 365
1992 DOMINION EAST OHIO Brine 0 365
1993 DOMINION EAST OHIO Brine 0 365
1994 DOMINION EAST OHIO Brine 0 365
1995 DOMINION EAST OHIO Brine 0 61
1998 DOVER ATWOOD CORP. Brine 0 0
1999 DOVER ATWOOD CORP. Brine 0 0
2000 DOVER ATWOOD CORP. Brine 0 365
2012 DOVER ATWOOD CORP. Brine 0 0
2013 DOVER ATWOOD CORP. Brine 85 365
2014 DOVER ATWOOD CORP. Brine 67 365
2015 DOVER ATWOOD CORP. Brine 0 365
2016 DOVER ATWOOD CORP. Brine 0 365
2017 DOVER ATWOOD CORP. Brine 35 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
1348766226 2012-09-18 Work Over Reconditioning No Violations
1497638530 2017-06-15 Production Wells No Violations I conducted a status check inspection on this well. The well is equipped with a hydraulic pumpjack. The tank battery consists of a 100 barrel tank, a plastic brine tank and a vertical separator. The tank battery and well are behind fencing. The well is legibly identified. No compliance issues are noted at this time.

For data sources see[9]

References