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34-151-21515

Well Details

Well ID: 34-151-21515
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Country: United States
State: Ohio
County: Stark
Municipality: Osnaburg Township
Operator Name: RANDELL OIL CO
Well Pad ID:
Farm/Lease Name: MIDDAUGH
License Status: Plugged and Abandoned
License Date: 2016-08-30
Spud Date: 1968-03-30
Spud Drilling Contractor:
Final Drill Date: 1968-04-11
Well Total Depth: 4938.00 ft
Configuration: Vertical
Latitude: 40.800000
Longitude: -81.290000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1801-01-02 201 GREEN GAS CO
Oil and Gas 1802-01-01
Original Spud 1968-03-30 KB=1111.5 UPDATED COORDINATES PER SURVEYOR-12/27/16 ALE.
Completed 1968-04-11 KB=1111.5 UPDATED COORDINATES PER SURVEYOR-12/27/16 ALE.
Reached Total Depth 1968-04-11 KB=1111.5 UPDATED COORDINATES PER SURVEYOR-12/27/16 ALE.
Change of Owner 2001-10-09 Operator changed from 201, GREEN GAS CO to 2409, RANDELL OIL CO
APP 2011-12-09 Proposed Formations:CLINTON, Issued Date:12/9/2011, Expired Date:12/8/2013 12:00:00 PM, Drilling unit acres:10, Proposed Well Type:OG, Proposed Well Class:
APP 2016-08-30 Proposed Formations:CLINTON, Issued Date:8/30/2016, Expired Date:8/30/2018 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2016-11-28 KB=1111.5 UPDATED COORDINATES PER SURVEYOR-12/27/16 ALE.
Record Last Modified 2016-12-27 KB=1111.5 UPDATED COORDINATES PER SURVEYOR-12/27/16 ALE.
Construction Permit Expires 2018-08-30 KB=1111.5 UPDATED COORDINATES PER SURVEYOR-12/27/16 ALE.

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 4792 4826 21
4792 4826 21
4792 4826 21

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 59000 Gal 58500 MCF

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1985 GREEN GAS CO 0.00 100.00 0
1986 GREEN GAS CO 0.00 231.00 365
1988 GREEN GAS CO 0.00 189.00 365
1989 GREEN GAS CO 0.00 166.00 365
1990 GREEN GAS CO 0.00 65.00 365
1991 GREEN GAS CO 0.00 86.00 365
1992 GREEN GAS CO 0.00 0.00 365
1993 GREEN GAS CO 0.00 87.00 365
1994 GREEN GAS CO 0.00 0.00 365
1995 GREEN GAS CO 0.00 78.00 365
1996 GREEN GAS CO 0.00 0.00 365
1997 GREEN GAS CO 0.00 0.00 365
1998 GREEN GAS CO 0.00 0.00 365
1999 GREEN GAS CO 0.00 0.00 365
2000 GREEN GAS CO 0.00 0.00 0
2014 RANDELL OIL CO 0.00 76.00 365
2016 RANDELL OIL CO 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1985 GREEN GAS CO Brine 70 0
1986 GREEN GAS CO Brine 0 365
1988 GREEN GAS CO Brine 120 365
1989 GREEN GAS CO Brine 70 365
1990 GREEN GAS CO Brine 0 365
1991 GREEN GAS CO Brine 80 365
1992 GREEN GAS CO Brine 100 365
1993 GREEN GAS CO Brine 50 365
1994 GREEN GAS CO Brine 75 365
1995 GREEN GAS CO Brine 35 365
1996 GREEN GAS CO Brine 0 365
1997 GREEN GAS CO Brine 0 365
1998 GREEN GAS CO Brine 0 365
1999 GREEN GAS CO Brine 0 365
2000 GREEN GAS CO Brine 0 0
2014 RANDELL OIL CO Brine 17 365
2016 RANDELL OIL CO Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-2074631427 2016-11-16 0:00 PB No Violations
0815043664 2016-11-17 Plug / Plug Back No Violations Thompson Well Service (TWS) tagged the top of the Clinton plug at 4601 (225 above the top perf ). TWS parted the 4.5 casing at 3450 and recovered 105 joints of 4.5 casing. The 2.375 work string was lowered into the borehole to 3250 for the Big Lime plug. Operations were shut down until 11/21 due to waiting on cementers.
1470400833 2016-08-03 Production Wells Violations Noted I conducted a status check inspection on this well. The RBDMS record shows the well had no production reports submitted from 2001 through 2013 and in 2014 production was reported. Also the record shows a Plugging permit was issued on 12-19--11-05(B), and plug the well within 180 days. The well owner/operator will be notified if the plugging schedule is approved or denied.
1480539707 2016-11-29 Plug / Plug Back No Violations An inspection was conducted to assess the cement top of the Middaugh # 4 well after the recent plugging and abandonment of the well. I check the cement top on the 8.625 surface casing and found it to be solid, hard and free of any signs of leakage. No violations identified during this inspection.
2074631427 2016-11-16 Plug / Plug Back No Violations Thompson Well Services ( TWS ) was the plugging contractor for the well. The well was completed as a pumping well so TWS removed the rods from the 2.375 EUE tubing. The tubing was set at 4841 which was below the bottom perf by 15 feet. An attempt to lower the tubing further was decided against due lack of rathole. Petroset Cementing Services (PCS) was the cementing contractor for the well. PCS circulated approximately 45 barrels of water ( 52 barrels annular capacity ) to clean the casing. Approximately 20 barrels of oil was recovered. PCS mixed and displaced a 25 sack ( Class A blended with 2% gel ) cement slurry through the interval 4841 to 4469. TWS removed 48 joints of tubing and shut down overnight.
815043664 2016-11-17 0:00 PB No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1470400833 US-OH-113526 2016-08-17 Failure to legibly identify well
1470400833 US-OH-113527 2016-08-17 Well shall be plugged

For data sources see[9]

References