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34-151-23056

Well Details

Well ID: 34-151-23056
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Country: United States
State: Ohio
County: Stark
Municipality: Nimishillen Township
Operator Name: ENERVEST OPERATING LLC
Well Pad ID:
Farm/Lease Name: JANELLO C
License Status: Producing
License Date: 1979-08-30
Spud Date: 1979-10-14
Spud Drilling Contractor:
Final Drill Date: 1979-10-19
Well Total Depth: 4786.00 ft
Configuration: Vertical
Latitude: 40.900000
Longitude: -81.290000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1979-08-30 182 BELDEN & BLAKE CO GeoDate 8/30/79
Original Spud 1979-10-14 GL=1117.5, DF=1126.5, KB=1127.5
Completed 1979-10-19 GL=1117.5, DF=1126.5, KB=1127.5
Reached Total Depth 1979-10-19 GL=1117.5, DF=1126.5, KB=1127.5
Change of Owner 2007-04-27 Operator changed from 182, BELDEN & BLAKE CORPORATION to 7578, ENERVEST OPERATING LLC
Record Last Modified 2019-06-04 GL=1117.5, DF=1126.5, KB=1127.5

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 4598 4677 2
4598 4677 2
4598 4677 2

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 84000 Gal 50000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 BELDEN & BLAKE CORPORATION 2321.00 1558.00 0
1985 BELDEN & BLAKE CORPORATION 1914.00 1237.00 0
1986 BELDEN & BLAKE CORPORATION 1673.00 1082.00 365
1987 BELDEN & BLAKE CORPORATION 1538.00 839.00 365
1988 BELDEN & BLAKE CORPORATION 1393.00 810.00 366
1989 BELDEN & BLAKE CORPORATION 1308.00 503.00 357
1990 BELDEN & BLAKE CORPORATION 989.00 719.00 346
1991 BELDEN & BLAKE CORPORATION 925.00 640.00 365
1992 BELDEN & BLAKE CORPORATION 866.00 692.00 347
1993 BELDEN & BLAKE CORPORATION 773.00 672.00 365
1994 BELDEN & BLAKE CORPORATION 585.00 515.00 365
1995 BELDEN & BLAKE CORPORATION 520.00 562.00 365
1996 BELDEN & BLAKE CORPORATION 547.00 350.00 366
1997 BELDEN & BLAKE CORPORATION 518.00 516.00 365
1998 BELDEN & BLAKE CORPORATION 455.00 164.00 365
1999 BELDEN & BLAKE CORPORATION 447.00 420.00 362
2000 BELDEN & BLAKE CORPORATION 521.00 387.00 352
2001 BELDEN & BLAKE CORPORATION 500.00 276.00 365
2002 BELDEN & BLAKE CORPORATION 550.00 255.00 365
2003 BELDEN & BLAKE CORPORATION 505.00 238.00 365
2004 BELDEN & BLAKE CORPORATION 414.00 241.00 359
2005 BELDEN & BLAKE CORPORATION 595.00 252.00 365
2006 BELDEN & BLAKE CORPORATION 555.00 219.00 365
2007 ENERVEST OPERATING LLC 483.00 134.00 365
2008 ENERVEST OPERATING LLC 465.00 199.00 365
2009 ENERVEST OPERATING LLC 408.00 210.00 365
2010 ENERVEST OPERATING LLC 440.00 133.00 365
2011 ENERVEST OPERATING LLC 500.00 132.00 0
2012 ENERVEST OPERATING LLC 404.00 116.00 366
2013 ENERVEST OPERATING LLC 386.00 138.00 365
2014 ENERVEST OPERATING LLC 335.00 142.00 365
2015 ENERVEST OPERATING LLC 287.00 119.00 365
2016 ENERVEST OPERATING LLC 191.00 85.00 366
2017 ENERVEST OPERATING LLC 172.00 71.00 353
2018 ENERVEST OPERATING LLC 95.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 BELDEN & BLAKE CORPORATION Brine 0 0
1985 BELDEN & BLAKE CORPORATION Brine 442 0
1986 BELDEN & BLAKE CORPORATION Brine 385 365
1987 BELDEN & BLAKE CORPORATION Brine 458 365
1988 BELDEN & BLAKE CORPORATION Brine 391 366
1989 BELDEN & BLAKE CORPORATION Brine 340 357
1990 BELDEN & BLAKE CORPORATION Brine 231 346
1991 BELDEN & BLAKE CORPORATION Brine 485 365
1992 BELDEN & BLAKE CORPORATION Brine 404 347
1993 BELDEN & BLAKE CORPORATION Brine 289 365
1994 BELDEN & BLAKE CORPORATION Brine 411 365
1995 BELDEN & BLAKE CORPORATION Brine 381 365
1996 BELDEN & BLAKE CORPORATION Brine 399 366
1997 BELDEN & BLAKE CORPORATION Brine 308 365
1998 BELDEN & BLAKE CORPORATION Brine 465 365
1999 BELDEN & BLAKE CORPORATION Brine 650 362
2000 BELDEN & BLAKE CORPORATION Brine 267 352
2001 BELDEN & BLAKE CORPORATION Brine 321 365
2002 BELDEN & BLAKE CORPORATION Brine 238 365
2003 BELDEN & BLAKE CORPORATION Brine 218 365
2004 BELDEN & BLAKE CORPORATION Brine 278 359
2005 BELDEN & BLAKE CORPORATION Brine 308 365
2006 BELDEN & BLAKE CORPORATION Brine 223 365
2007 ENERVEST OPERATING LLC Brine 185 365
2008 ENERVEST OPERATING LLC Brine 216 365
2009 ENERVEST OPERATING LLC Brine 214 365
2010 ENERVEST OPERATING LLC Brine 158 365
2011 ENERVEST OPERATING LLC Brine 230
2012 ENERVEST OPERATING LLC Brine 153 366
2013 ENERVEST OPERATING LLC Brine 224 365
2014 ENERVEST OPERATING LLC Brine 50 365
2015 ENERVEST OPERATING LLC Brine 204 365
2016 ENERVEST OPERATING LLC Brine 145 366
2017 ENERVEST OPERATING LLC Brine 0 353
2018 ENERVEST OPERATING LLC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1644590577 2015-6-16 0:00: PW No Violations 1.00
0930265929 2015-06-04 Production Wells No Violations I was on location to follow up to the sales line leak for this well that has released approximately 5 gallons of crude oil into a ditch that leads into Nimishillen Creek. The sales line was clamped and is no longer leaking. Adsorbent pads were used to remove free oil on the creek surface and covered vegetation was removed for disposal. Oil adsorbent booms were installed in the ditch to catch and control and free oil that may have been missed. There is a small amount of oil still pooling in the ditch. Enervest has been checking and removing the oil twice a day. The booms are still present in the ditch and have prevented any oil from leaving the ditch. No oil is currently leaving the ditch. The booms will be left in the ditch and monitored daily to make sure the oil cleanup is complete.
1504363331 2015-06-02 Production Wells No Violations I was contacted by Kyle Fink of Enervest at 10:15am indicating that the sales line for this well has broken and released approximately 5 gallons of crude oil into a ditch that leads into Nimishillen Creek. The Ohio EPA, LEPC and local fire departments were contacted and informed of the spill. A J-Hawk vacuum truck was on location and removed all the free oil from the creek. The sales line was clamped and is no longer leaking. Adsorbent pads were used to remove free oil on the creek surface and covered vegetation was removed for disposal. Oil adsorbent booms were installed in the ditch to catch and control and free oil that may have been missed. The lease road for the well is a shared agricultural drive and is stable. The tank battery is shared with well #22667, is surrounded by a dike, is properly identified and contains two (2) 210bbl production tanks, two (2) vertical mechanical separators, two (2) chart boxes and a concrete brine vault. The electric driven pumpjack is identified and is in good mechanical condition. The booms will be left in the ditch and monitored daily to make sure the oil cleanup is complete.
1644590577 2015-06-16 Production Wells No Violations I was on location to follow up to a spill that occurred on 6/2/2015. The sales line for this well

broke and released approximately 5 gallons of crude oil into a ditch that leads into Nimishillen Creek. At this time the ditch is free of any oil and the sales line has been fixed. There is no free oil in the ditch or Nimishillen Creek. The booms that has been placed in the creek have been removed. There are no violations at this time.

930265929 2015-6-4 0:00:0 PW No Violations 1.50

For data sources see[9]

References