X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-151-23194

Well Details

Well ID: 34-151-23194
Loading map...
Country: United States
State: Ohio
County: Tuscarawas
Municipality: Lawrence Township
Operator Name: GAS ACQUISITION COMPANY LTD
Well Pad ID:
Farm/Lease Name: LAUTZENHEISER UNIT
License Status: Final Restoration
License Date: 2004-05-06
Spud Date: 1980-05-16
Spud Drilling Contractor:
Final Drill Date: 1980-05-21
Well Total Depth: 4585.00 ft
Configuration: Vertical
Latitude: 40.650000
Longitude: -81.470000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1980-05-09 139 MB OPERATING CO INC GeoDate 5/9/80
Original Spud 1980-05-16
Completed 1980-05-21
Reached Total Depth 1980-05-21
APP 1999-05-10 Proposed Formations:CLINTON, Issued Date:5/10/99, Expired Date:5/9/2000 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:
Change of Owner 2000-06-30 Operator changed from 139, MB OPERATING CO INC to 6674, GREAT LAKES ENERGY PTNSHP LLC
Change of Owner 2004-04-22 Operator changed from 6674, GREAT LAKES ENERGY PTNSHP LLC to 6805, GAS ACQUISITION COMPANY LTD
APP 2004-05-06 Proposed Formations:CLINTON, Issued Date:5/6/2004, Expired Date:5/6/2005 6:00:00 AM, Drilling unit acres:123.73, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2004-05-21
Construction Permit Expires 2005-05-06
Record Last Modified 2013-03-14

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 4385 4493 19
4385 4493 19
4385 4493 19

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 4690 Bbl 0

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 MB OPERATING CO INC 10940.00 101.00 0
1985 MB OPERATING CO INC 6275.00 84.00 365
1986 MB OPERATING CO INC 4583.00 0.00 365
1987 MB OPERATING CO INC 4514.00 0.00 365
1988 MB OPERATING CO INC 4383.00 86.00 366
1989 MB OPERATING CO INC 1850.00 0.00 365
1990 MB OPERATING CO INC 2209.00 0.00 365
1991 MB OPERATING CO INC 696.00 0.00 365
1992 MB OPERATING CO INC 0.00 0.00 366
1993 MB OPERATING CO INC 0.00 0.00 365
1994 MB OPERATING CO INC 0.00 0.00 365
1995 MB OPERATING CO INC 5.00 0.00 365
1996 MB OPERATING CO INC 0.00 0.00 366
1997 MB OPERATING CO INC 0.00 0.00 365
1998 MB OPERATING CO INC 0.00 0.00 365
1999 MB OPERATING CO INC 0.00 0.00 273

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 MB OPERATING CO INC Brine 0 0
1985 MB OPERATING CO INC Brine 175 365
1986 MB OPERATING CO INC Brine 70 365
1987 MB OPERATING CO INC Brine 278 365
1988 MB OPERATING CO INC Brine 245 366
1989 MB OPERATING CO INC Brine 14 365
1990 MB OPERATING CO INC Brine 305 365
1991 MB OPERATING CO INC Brine 35 365
1992 MB OPERATING CO INC Brine 0 366
1993 MB OPERATING CO INC Brine 0 365
1994 MB OPERATING CO INC Brine 0 365
1995 MB OPERATING CO INC Brine 0 365
1996 MB OPERATING CO INC Brine 0 366
1997 MB OPERATING CO INC Brine 70 365
1998 MB OPERATING CO INC Brine 0 365
1999 MB OPERATING CO INC Brine 0 273

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1650312509 2004-2-24 0:00: PW No Violations
001288i509 2002-04-22 Production Wells No Violations Routine inspection revealed no violations at this time .
1085328633 2004-05-21 Production Wells No Violations N.O.V. has been RESOLVED. Well was P&A on 5-21-2004.
1288i509 2002-4-22 0:00: PW No Violations 0.50
1650312509 2004-02-24 Production Wells No Violations Inspected the WH and TB. The tank battery is overgrown with vegetation. There is an old MB Operating I.D. sign on the stock tank and the gas meter has been removed. A Balon casing valve is shut-in on the wellhead. One 2 dia. casing valve is shut-in. The other 2 dia. casing valve is open. The well appears to be idle. RBDMS shows zero production since 1998. PLUG or PRODUCE the well. GPS 1-210 bbl oil stock tank and 1- buried steel brine tank.
1932872909 2004-10-19 Final Restoration No Violations Well was P&A on 5-21-2004. The Final Restoration is PASSED.

For data sources see[9]

References