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34-151-23345

Well Details

Well ID: 34-151-23345
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Country: United States
State: Ohio
County: Stark
Municipality: Osnaburg Township
Operator Name: EXCO - NORTH COAST ENERGY INC
Well Pad ID:
Farm/Lease Name: ALLER DONALD
License Status: Final Restoration
License Date: 2007-05-14
Spud Date: 1984-10-25
Spud Drilling Contractor: ARMSTRONG DRLG
Final Drill Date: 1984-11-01
Well Total Depth: 5165.00 ft
Configuration: Vertical
Latitude: 40.800000
Longitude: -81.230000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1980-10-16 9 EDC GeoDate 10/16/80
CO 1984-10-03 9 EDC GeoDate 10/3/84
Oil and Gas 1984-10-03 Issued Date 10/3/84 Expired Date 4/1/85 Acres 0080000 Tool Type RTF Proposed Formation CLINTON Proposed Depth 05165 Proposed Drill Depth 05165
Original Spud 1984-10-25 RI 10-6-84
Completed 1984-11-01 RI 10-6-84
Reached Total Depth 1984-11-01 RI 10-6-84
Completion Report Received 1984-12-05 RI 10-6-84
APP 2007-05-14 Proposed Formations:CLINTON, Issued Date:5/14/2007, Expired Date:5/13/2008 6:00:00 AM, Drilling unit acres:80, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2007-10-31 RI 10-6-84
Construction Permit Expires 2008-05-13 RI 10-6-84
Change of Owner 2008-07-21 Operator changed from 9, POWER GAS MARKETING & TRANS to 1388, EXCO - NORTH COAST ENERGY INC
Record Last Modified 2017-02-15 RI 10-6-84

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 4946 5064 0
4946 5064 0
2006-09-11 4985 5061 38
4985 5061 38
4946 5064 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 290000 Gal 275000 FRAC: H2O,SAND

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1985 POWER GAS MARKETING & TRANS 15648.00 4918.00 365
1986 POWER GAS MARKETING & TRANS 9293.00 1914.00 365
1987 POWER GAS MARKETING & TRANS 9642.00 1558.00 365
1988 POWER GAS MARKETING & TRANS 7481.00 1174.00 365
1989 POWER GAS MARKETING & TRANS 5703.00 796.00 365
1990 POWER GAS MARKETING & TRANS 5358.00 987.00 365
1991 POWER GAS MARKETING & TRANS 4600.00 636.00 365
1992 POWER GAS MARKETING & TRANS 3737.00 680.00 365
1993 POWER GAS MARKETING & TRANS 4140.00 595.00 365
1994 POWER GAS MARKETING & TRANS 3080.00 484.00 0
1995 POWER GAS MARKETING & TRANS 2833.00 366.00 0
1996 POWER GAS MARKETING & TRANS 2375.00 532.00 0
1997 POWER GAS MARKETING & TRANS 581.00 83.00 365
1998 POWER GAS MARKETING & TRANS 0.00 0.00 0
1999 POWER GAS MARKETING & TRANS 0.00 0.00 0
2000 POWER GAS MARKETING & TRANS 0.00 0.00 0
2001 POWER GAS MARKETING & TRANS 0.00 0.00 0
2002 POWER GAS MARKETING & TRANS 0.00 0.00 0
2003 POWER GAS MARKETING & TRANS 0.00 0.00 0
2004 POWER GAS MARKETING & TRANS 0.00 0.00 0
2005 POWER GAS MARKETING & TRANS 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1985 POWER GAS MARKETING & TRANS Brine 2312 365
1986 POWER GAS MARKETING & TRANS Brine 696 365
1987 POWER GAS MARKETING & TRANS Brine 621 365
1988 POWER GAS MARKETING & TRANS Brine 621 365
1989 POWER GAS MARKETING & TRANS Brine 233 365
1990 POWER GAS MARKETING & TRANS Brine 277 365
1991 POWER GAS MARKETING & TRANS Brine 208 365
1992 POWER GAS MARKETING & TRANS Brine 218 365
1993 POWER GAS MARKETING & TRANS Brine 130 365
1994 POWER GAS MARKETING & TRANS Brine 99 0
1995 POWER GAS MARKETING & TRANS Brine 185 0
1996 POWER GAS MARKETING & TRANS Brine 129 0
1997 POWER GAS MARKETING & TRANS Brine 334 365
1998 POWER GAS MARKETING & TRANS Brine 0 0
1999 POWER GAS MARKETING & TRANS Brine 0 0
2000 POWER GAS MARKETING & TRANS Brine 0 0
2001 POWER GAS MARKETING & TRANS Brine 0 0
2002 POWER GAS MARKETING & TRANS Brine 0 0
2003 POWER GAS MARKETING & TRANS Brine 0 0
2004 POWER GAS MARKETING & TRANS Brine 0 0
2005 POWER GAS MARKETING & TRANS Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1301541009 2007-10-29 0:00 PB No Violations
0000PL5636 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
1077118405 2004-02-18 Production Wells Violations Noted The well contains rods and tbg. The pumping unit is gone. The power line is disconnected and rolled up at the power pole. The tbg. valves are shut in. RBDMS shows zero production from 1998 thru 2002. TB contains 1-210 bbl stock tank, 1- concrete brine vault, and a separator. The old EDC I.D. sign cannot be read. GPS WH and TB. Well is idle. Stock tank needs a new I.D. sign. Plug or produce the well.
1193866221 2007-10-31 Plug / Plug Back No Violations This idle well was plugged on 10-31-2007. The N.O.V. has been RESOLVED.
1240842862 2009-04-24 Final Restoration No Violations This well was plugged and abandoned on 10-31-2007. The former well site is reclaimed and is now in cropland. All of the equipment from the tank battery is gone and the former tank battery site is reclaimed. The Final Restoration is PASSED.
1301541009 2007-10-29 Plug / Plug Back No Violations Omega Cementing pumped a 30 sack Clinton plug thru tubing.
PL5636 PL No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1077118405 US-OH-101662 2004-02-18 Failure to legibly identify well
1077118405 US-OH-101663 2004-02-18 Well shall be plugged

For data sources see[9]

References