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| Well ID: 34-151-23898 | Loading map...
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| Country: United States | |
| State: Ohio | |
| County: Stark | |
| Municipality: Marlboro Township | |
| Operator Name: ENERVEST OPERATING LLC | |
| Well Pad ID: | |
| Farm/Lease Name: ZELLERS K& H | |
| License Status: Producing | |
| License Date: 1983-08-02 | |
| Spud Date: 1983-08-18 | |
| Spud Drilling Contractor: ARMSTRONG DRLG | |
| Final Drill Date: 1983-08-23 | |
| Well Total Depth: 4760.00 ft | |
| Configuration: Vertical | |
| Latitude: 40.940000 | |
| Longitude: -81.290000 |
For data sources see[1]
| Well Status | Well Status Date | Comment |
|---|---|---|
| Oil and Gas | 1983-08-02 | Issued Date 8/2/83 Expired Date 1/29/84 Acres 0051200 Tool Type RTA Proposed Formation CLINTON Proposed Depth 04760 Proposed Drill Depth 04760 |
| Original Spud | 1983-08-18 | |
| Completed | 1983-08-23 | |
| Reached Total Depth | 1983-08-23 | |
| CO | 1983-10-07 | 182 BELDEN & BLAKE CO GeoDate 8/2/83 |
| Completion Report Received | 1983-11-04 | |
| Construction Permit Expires | 1984-01-29 | |
| Change of Owner | 2007-04-27 | Operator changed from 182, BELDEN & BLAKE CORPORATION to 7578, ENERVEST OPERATING LLC |
| Record Last Modified | 2017-02-15 |
For data sources see[2]
| Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
|---|---|---|---|
| 1997-06-29 | 4562 | 4664 | 0 |
| 4562 | 4664 | 0 | |
| 2006-09-11 | 4612 | 4651 | 36 |
| 4612 | 4651 | 36 | |
| 4562 | 4664 | 0 |
For data sources see[3]
| Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
|---|---|---|---|---|---|---|
| H2O | 0 | 96000 Gal | 40000 | FRAC;96MG H2O,40M# SD |
For data sources see[4]
| Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 1984 | BELDEN & BLAKE CORPORATION | 2318.00 | 2828.00 | 0 |
| 1985 | BELDEN & BLAKE CORPORATION | 1914.00 | 1670.00 | 0 |
| 1986 | BELDEN & BLAKE CORPORATION | 1564.00 | 1214.00 | 365 |
| 1987 | BELDEN & BLAKE CORPORATION | 1775.00 | 1131.00 | 365 |
| 1988 | BELDEN & BLAKE CORPORATION | 1393.00 | 979.00 | 358 |
| 1990 | BELDEN & BLAKE CORPORATION | 983.00 | 768.00 | 355 |
| 1991 | BELDEN & BLAKE CORPORATION | 924.00 | 632.00 | 365 |
| 1992 | BELDEN & BLAKE CORPORATION | 995.00 | 641.00 | 311 |
| 1993 | BELDEN & BLAKE CORPORATION | 773.00 | 805.00 | 365 |
| 1994 | BELDEN & BLAKE CORPORATION | 585.00 | 645.00 | 348 |
| 1995 | BELDEN & BLAKE CORPORATION | 520.00 | 505.00 | 365 |
| 1996 | BELDEN & BLAKE CORPORATION | 547.00 | 469.00 | 366 |
| 1997 | BELDEN & BLAKE CORPORATION | 518.00 | 544.00 | 365 |
| 1998 | BELDEN & BLAKE CORPORATION | 455.00 | 313.00 | 365 |
| 1999 | BELDEN & BLAKE CORPORATION | 447.00 | 523.00 | 320 |
| 2000 | BELDEN & BLAKE CORPORATION | 521.00 | 472.00 | 348 |
| 2001 | BELDEN & BLAKE CORPORATION | 500.00 | 251.00 | 369 |
| 2002 | BELDEN & BLAKE CORPORATION | 550.00 | 427.00 | 351 |
| 2003 | BELDEN & BLAKE CORPORATION | 996.00 | 345.00 | 283 |
| 2004 | BELDEN & BLAKE CORPORATION | 1078.00 | 609.00 | 366 |
| 2005 | BELDEN & BLAKE CORPORATION | 1219.00 | 414.00 | 365 |
| 2006 | BELDEN & BLAKE CORPORATION | 1253.00 | 308.00 | 365 |
| 2007 | ENERVEST OPERATING LLC | 1034.00 | 242.00 | 365 |
| 2008 | ENERVEST OPERATING LLC | 951.00 | 352.00 | 365 |
| 2009 | ENERVEST OPERATING LLC | 948.00 | 306.00 | 365 |
| 2010 | ENERVEST OPERATING LLC | 901.00 | 215.00 | 365 |
| 2011 | ENERVEST OPERATING LLC | 1151.00 | 283.00 | 0 |
| 2012 | ENERVEST OPERATING LLC | 1136.00 | 169.00 | 366 |
| 2013 | ENERVEST OPERATING LLC | 1342.00 | 192.00 | 365 |
| 2014 | ENERVEST OPERATING LLC | 1780.00 | 256.00 | 365 |
| 2015 | ENERVEST OPERATING LLC | 1683.00 | 311.00 | 365 |
| 2016 | ENERVEST OPERATING LLC | 1070.00 | 208.00 | 366 |
| 2017 | ENERVEST OPERATING LLC | 436.00 | 317.00 | 365 |
| 2018 | ENERVEST OPERATING LLC | 678.00 | 183.00 | 365 |
| Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|
| -80886062 | 2014-5-6 0:00:0 | PW | No Violations | 6.00 |
| 0000PL5445 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
| 0033379113 | 2002-07-31 | Production Wells | No Violations | NO VIOLATIONS. |
| 0080886062 | 2014-05-06 | Production Wells | No Violations | I was contacted at 11:30am by Doug (330-365-7079), the Enervest Manager, regarding a flow line leak that occurred near the wellhead. I was on location with Inspector Jim Bucksar. Also on site was Joe Little Excavating cleaning up the spill. The affected area was a 120 by 30 area of the plowed field with a small pooling of crude oil on the surface. It is estimated the spill was a total of 4bbls. The affected topsoil was scraped up and put inside of a liner and covered with a tarp on the lease road to ensure it does not erode or leave location. A Kimble Company dumpster will be on location tomorrow to haul away the contaminated soil. The soil has been stabilized with peat sorb and is covered to prevent any rain from affecting the contaminated soil before it will be moved off location. I witnessed the digging up of the flow line. A small pinhole leak was located. The leak was patched, and the flow line pressure tested to ensure there were no more leaks. The flow line was then covered with soil and the area graded. Field grade topsoil is going to be brought on location to cover are the area where the contaminated soil was removed. I will follow up to ensure the topsoil was put back onto the field, that the contaminated soil will be properly disposed, and that no more oil is present on location. |
| 0811952451 | 2014-05-12 | Production Wells | No Violations | I was on location to follow-up to a spill that occurred May 6th. The oil has been remediated and the well has been cleaned up. A flow line patch was used and pressure tested to ensure no more leaks were present in the line. The contaminated soil has been removed off location by Kimble Companies and will be brought to the landfill and proper disposed of. At this time the spill has been cleaned up and the production equipment brought back into working condition properly. There are no violations at this time. |
| 33379113 | 2002-7-31 0:00: | PW | No Violations | 0.50 |
| 811952451 | 2014-5-12 0:00: | PW | No Violations | 2.00 |
| PL5445 | PL | No Violations |
For data sources see[9]