If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.
powered by ChangeDetection
Well ID: 34-151-24055 | Loading map...
{"type":"SATELLITE","minzoom":false,"maxzoom":false,"types":["ROADMAP","SATELLITE","HYBRID","TERRAIN"],"mappingservice":"googlemaps3","width":"100%","height":"350px","centre":false,"title":"","label":"","icon":"","visitedicon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"wmsoverlay":false,"copycoords":false,"static":false,"zoom":14,"layers":[],"controls":["pan","zoom","type","scale","streetview","rotate"],"zoomstyle":"DEFAULT","typestyle":"DEFAULT","autoinfowindows":false,"resizable":false,"kmlrezoom":false,"poi":true,"markercluster":false,"clustergridsize":60,"clustermaxzoom":20,"clusterzoomonclick":true,"clusteraveragecenter":true,"clusterminsize":2,"imageoverlays":[],"kml":[],"gkml":[],"searchmarkers":"","enablefullscreen":false,"scrollwheelzoom":false,"locations":[{"text":"","title":"","link":"","lat":40.85,"lon":-81.11,"icon":""}]} |
Country: United States | |
State: Ohio | |
County: Stark | |
Municipality: Washington Township | |
Operator Name: PETROX, INC | |
Well Pad ID: | |
Farm/Lease Name: RAMSER | |
License Status: Final Restoration | |
License Date: 2014-04-17 | |
Spud Date: 1985-01-08 | |
Spud Drilling Contractor: [[JL COATS [COATS-GOFF]]] | |
Final Drill Date: 1985-01-17 | |
Well Total Depth: 5476.00 ft | |
Configuration: Vertical | |
Latitude: 40.850000 | |
Longitude: -81.110000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1984-08-09 | 1754 SUTTON ENTERPRISES INC GeoDate 8/9/84 |
Oil and Gas | 1984-08-09 | Issued Date 8/9/84 Expired Date 2/5/85 Acres 0044858 Tool Type RTA Proposed Formation CLINTON Proposed Depth 05476 Proposed Drill Depth 05476 |
Original Spud | 1985-01-08 | |
Completed | 1985-01-17 | |
Reached Total Depth | 1985-01-17 | |
Completion Report Received | 1985-02-04 | |
CO | 1993-10-22 | 2172 NATLAND ENERGY CORP GeoDate 8/9/84 |
Change of Owner | 1997-10-28 | Operator changed from 2172, NATLAND ENERGY CORP to 182, BELDEN & BLAKE CORPORATION |
Change of Owner | 2002-08-12 | Operator changed from 182, BELDEN & BLAKE CORPORATION to 1966, PETROX INC |
APP | 2008-07-25 | Proposed Formations:CLINTON, Issued Date:7/25/2008, Expired Date:7/25/2009 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class: |
APP | 2014-04-17 | Proposed Formations:CLINTON, Issued Date:4/17/2014, Expired Date:4/16/2016 12:00:00 PM, Drilling unit acres:45, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2014-05-23 | |
Construction Permit Expires | 2016-04-16 | |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 5258 | 5314 | 8 |
5258 | 5314 | 8 | |
5258 | 5314 | 8 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 680 Bbl | 35000 | FRAC;H2O,SAND |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1985 | SUTTON ENTERPRISES INC | 6605.00 | 395.00 | 270 |
1986 | SUTTON ENTERPRISES INC | 4835.00 | 231.00 | 365 |
1987 | SUTTON ENTERPRISES INC | 2334.00 | 105.00 | 365 |
1988 | SUTTON ENTERPRISES INC | 1753.00 | 149.00 | 365 |
1989 | SUTTON ENTERPRISES INC | 1586.00 | 87.00 | 365 |
1990 | SUTTON ENTERPRISES INC | 1337.00 | 76.00 | 365 |
1991 | SUTTON ENTERPRISES INC | 1129.00 | 172.00 | 365 |
1993 | SUTTON ENTERPRISES INC | 1601.00 | 0.00 | 365 |
1994 | SUTTON ENTERPRISES INC | 762.00 | 135.00 | 365 |
1995 | SUTTON ENTERPRISES INC | 485.00 | 60.00 | 365 |
1996 | SUTTON ENTERPRISES INC | 930.00 | 68.00 | 365 |
1997 | BELDEN & BLAKE CORPORATION | 252.00 | 0.00 | 49 |
1998 | BELDEN & BLAKE CORPORATION | 441.00 | 114.00 | 329 |
1999 | BELDEN & BLAKE CORPORATION | 184.00 | 0.00 | 132 |
2001 | BELDEN & BLAKE CORPORATION | 0.00 | 0.00 | 366 |
2002 | PETROX, INC | 0.00 | 0.00 | 0 |
2003 | PETROX, INC | 0.00 | 0.00 | 0 |
2004 | PETROX, INC | 0.00 | 0.00 | 0 |
2005 | PETROX, INC | 0.00 | 0.00 | 0 |
2007 | PETROX, INC | 0.00 | 0.00 | 0 |
2008 | PETROX, INC | 0.00 | 0.00 | 0 |
2012 | PETROX, INC | 0.00 | 0.00 | 0 |
2013 | PETROX, INC | 0.00 | 0.00 | 0 |
2014 | PETROX, INC | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1985 | SUTTON ENTERPRISES INC | Brine | 180 | 270 |
1986 | SUTTON ENTERPRISES INC | Brine | 76 | 365 |
1987 | SUTTON ENTERPRISES INC | Brine | 55 | 365 |
1988 | SUTTON ENTERPRISES INC | Brine | 59 | 365 |
1989 | SUTTON ENTERPRISES INC | Brine | 43 | 365 |
1990 | SUTTON ENTERPRISES INC | Brine | 1177 | 365 |
1991 | SUTTON ENTERPRISES INC | Brine | 36 | 365 |
1993 | SUTTON ENTERPRISES INC | Brine | 0 | 365 |
1994 | SUTTON ENTERPRISES INC | Brine | 0 | 365 |
1995 | SUTTON ENTERPRISES INC | Brine | 0 | 365 |
1996 | SUTTON ENTERPRISES INC | Brine | 0 | 365 |
1997 | BELDEN & BLAKE CORPORATION | Brine | 0 | 49 |
1998 | BELDEN & BLAKE CORPORATION | Brine | 37 | 329 |
1999 | BELDEN & BLAKE CORPORATION | Brine | 0 | 132 |
2001 | BELDEN & BLAKE CORPORATION | Brine | 0 | 366 |
2002 | PETROX, INC | Brine | 0 | 0 |
2003 | PETROX, INC | Brine | 0 | 0 |
2004 | PETROX, INC | Brine | 0 | 0 |
2005 | PETROX, INC | Brine | 0 | 0 |
2007 | PETROX, INC | Brine | 0 | |
2008 | PETROX, INC | Brine | 0 | 0 |
2012 | PETROX, INC | Brine | 0 | 0 |
2013 | PETROX, INC | Brine | 0 | 0 |
2014 | PETROX, INC | Brine | 75 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1452449557 | 2015-10-26 0:00 | FR | No Violations | 1.50 |
0000PL5312 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0098517307 | 2014-05-22 | Plug / Plug Back | No Violations | I was on location to witness the setting of the bottom plug for this well. The plunger was present in the 2 7/8 tubing and had to be circulated out to be removed. Once the rabbit was circulated out of the well tubing a bottom plug of 25sks Class A cement was pumped through tubing from 5353-5058. The well was shut in for an hour and the rig began to pull tubing from the well. They will set the Big Lime and surface plugs tomorrow after the tubing is out of the well. |
1401900962 | 2014-05-23 | Plug / Plug Back | No Violations | I was on location to witness the plugging of this well. The 4.5 casing was ripped at 3966 and the Big Lime plug was set on the way out of the hole. A 300 86sk lime plug was set. The 4.5 was then pulled to 949 and a 200 bottom of surface casing plug was set with 60sks. The remainder of the 4.5 casing was pulled from the well and a 200 surface plug was circulated and topped off with 62sks of cement. Nicks will now cut the casing below grade and weld on an identifying cap with the API# on it. |
1452449557 | 2015-10-26 | Final Restoration | No Violations | I was on location to check the status of final restoration. The location has been reclaimed and vegetation has been established. All of the production equipment has been removed and there are no signs of the well leaking. A plugging report is on file for this well. At this time final restoration has been passed. |
1570147130 | 2014-05-15 | Production Wells | No Violations | I received a call from the landowner regarding the preparation for the plugging of this well. Petro has removed the tank battery and covered the area with topsoil. A permit to plug and abandon the well was issued in April 2014 and is on schedule to be plugged this summer by Nicks Well Plugging. I explained to the landowner that the well, production equipment and flow lines would be removed before a final restoration would be passed after the well is plugged. I addressed his concerns and provided my contact information should he have any more questions. |
98517307 | 2014-5-22 0:00: | PB | No Violations | 6.00 |
PL5312 | PL | No Violations |
For data sources see[9]