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| Well ID: 34-151-24463 | Loading map...
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| Country: United States | |
| State: Ohio | |
| County: Stark | |
| Municipality: Nimishillen Township | |
| Operator Name: ENERVEST OPERATING LLC | |
| Well Pad ID: | |
| Farm/Lease Name: KOLM | |
| License Status: Producing | |
| License Date: 1988-10-24 | |
| Spud Date: 1989-01-28 | |
| Spud Drilling Contractor: CUBBY DRLG | |
| Final Drill Date: 1989-02-01 | |
| Well Total Depth: 5193.00 ft | |
| Configuration: Vertical | |
| Latitude: 40.840000 | |
| Longitude: -81.200000 |
For data sources see[1]
| Well Status | Well Status Date | Comment |
|---|---|---|
| Oil and Gas | 1988-10-24 | Issued Date 10/24/88 Expired Date 10/24/89 Acres 0040000 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 05193 Proposed Drill Depth 05193 |
| Original Spud | 1989-01-27 | |
| Completed | 1989-02-01 | |
| Reached Total Depth | 1989-02-01 | |
| Completion Report Received | 1989-06-28 | |
| CO | 1989-07-06 | 139 MB OPERATING CO INC GeoDate 10/24/88 |
| Construction Permit Expires | 1989-10-24 | |
| Change of Owner | 2000-06-30 | Operator changed from 139, MB OPERATING CO INC to 6674, GREAT LAKES ENERGY PTNSHP LLC |
| Change of Owner | 2010-08-25 | Operator changed from 6674, RANGE RESOURCES-APPALACHIA LLC to 7578, ENERVEST OPERATING LLC |
| Correction to Well | 2014-03-27 | UNIT SIZE DECREASED TO 20 ACRES. |
| Record Last Modified | 2019-06-14 |
For data sources see[2]
| Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
|---|---|---|---|
| 1997-06-29 | 4930 | 5062 | 0 |
| 4930 | 5062 | 0 | |
| 2006-09-11 | 4956 | 5023 | 28 |
| 4956 | 5023 | 28 | |
| 4930 | 5062 | 0 |
For data sources see[3]
| Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
|---|---|---|---|---|---|---|
| H2O | 0 | 4618 Bbl | 0 | SLICKWATER FRAC |
For data sources see[4]
| Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 1989 | MB OPERATING CO INC | 654.00 | 882.00 | 365 |
| 1990 | MB OPERATING CO INC | 2233.00 | 1695.00 | 365 |
| 1992 | MB OPERATING CO INC | 1781.00 | 1038.00 | 366 |
| 1993 | MB OPERATING CO INC | 1340.00 | 799.00 | 365 |
| 1994 | MB OPERATING CO INC | 1414.00 | 721.00 | 365 |
| 1995 | MB OPERATING CO INC | 1337.00 | 687.00 | 365 |
| 1996 | MB OPERATING CO INC | 1225.00 | 687.00 | 366 |
| 1997 | MB OPERATING CO INC | 1192.00 | 579.00 | 365 |
| 1999 | MB OPERATING CO INC | 526.00 | 375.00 | 273 |
| 2000 | RANGE RESOURCES-APPALACHIA LLC | 1721.00 | 577.00 | 365 |
| 2001 | RANGE RESOURCES-APPALACHIA LLC | 92.00 | 580.00 | 306 |
| 2002 | RANGE RESOURCES-APPALACHIA LLC | 8.00 | 473.00 | 304 |
| 2003 | RANGE RESOURCES-APPALACHIA LLC | 2.00 | 450.00 | 212 |
| 2004 | RANGE RESOURCES-APPALACHIA LLC | 0.00 | 265.00 | 93 |
| 2005 | RANGE RESOURCES-APPALACHIA LLC | 123.00 | 349.00 | 303 |
| 2006 | RANGE RESOURCES-APPALACHIA LLC | 418.00 | 583.00 | 365 |
| 2007 | RANGE RESOURCES-APPALACHIA LLC | 463.00 | 474.00 | 365 |
| 2008 | RANGE RESOURCES-APPALACHIA LLC | 333.00 | 471.00 | 365 |
| 2009 | RANGE RESOURCES-APPALACHIA LLC | 344.00 | 356.00 | 365 |
| 2010 | ENERVEST OPERATING LLC | 168.00 | 361.00 | 365 |
| 2011 | ENERVEST OPERATING LLC | 179.00 | 394.00 | 0 |
| 2012 | ENERVEST OPERATING LLC | 244.00 | 305.00 | 366 |
| 2013 | ENERVEST OPERATING LLC | 221.00 | 247.00 | 365 |
| 2014 | ENERVEST OPERATING LLC | 172.00 | 357.00 | 365 |
| 2015 | ENERVEST OPERATING LLC | 31.00 | 240.00 | 365 |
| 2016 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 366 |
| 2017 | ENERVEST OPERATING LLC | 210.00 | 119.00 | 365 |
| 2018 | ENERVEST OPERATING LLC | 240.00 | 500.00 | 365 |
| Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|
| 0000PL4972 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
| 1538739959 | 2018-09-29 | Production Wells | Violations Noted | I received phone calls from Kyle Fink (Enervest) and Fred Romeo (Emergency Response - Oil & Gas) concerning and tank battery overflow in which oil got into a tributary of the East Branch Nimishillen Creek. The estimated spill was two barrels of oil. When I arrived on location I met with Mike Burkhart (Enervest) and Kyle Fink. The oil in the creek was contained using booms and a siphon dam and clean-up operation were underway. The leak into the creek started at the tank battery. There was no sign of overflow of the containment dike. The oil entered the stream by perking down through the steam bank soil - Leak location +/- 9 (40.84740, -81.20991). The estimated stream effacement is 600 Ft. The reported cause of the overflow was a timer at the well malfunctioned. I inspected the well and the electrical switch was in the OFF position. Repair well components as needed so the timer functions as designed. Ensure the tank battery is cleaned-up and repaired so any future leaks are contained in the dike. Continue with downstream oil mitigation until such a time there is no evidence of oil in the stream. |
| 1575680603 | 2018-10-04 | Production Wells | No Violations | I met with Kyle Fink (Enervest) and Tim McConaha (Enervest) on location. Clean-up is still progressing. I did not notice any more oil purging from the stream bank below the tank battery. |
| 2146257413 | 2018-11-23 | Production Wells | No Violations | My inspection found no sign of oil in the stream or on the stream bank. The siphon dam and down stream booms have been removed. The Compliance Notice issued on 09-29-2018 is Passed. |
| PL4972 | PL | No Violations |
| Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
|---|---|---|---|---|
| 1538739959 | US-OH-114855 | 2019-01-15 | 9-1-07 | Well operation causing pollution and contamination |
For data sources see[9]