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| Well ID: 34-151-24558 | Loading map...
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| Country: United States | |
| State: Ohio | |
| County: Stark | |
| Municipality: Tuscarawas Township | |
| Operator Name: ENERVEST OPERATING LLC | |
| Well Pad ID: | |
| Farm/Lease Name: LEEMAN | |
| License Status: Final Restoration | |
| License Date: 2014-04-02 | |
| Spud Date: 1989-11-30 | |
| Spud Drilling Contractor: ADVENT DRLG | |
| Final Drill Date: 1989-12-03 | |
| Well Total Depth: 2879.00 ft | |
| Configuration: Vertical | |
| Latitude: 40.740000 | |
| Longitude: -81.630000 |
For data sources see[1]
| Well Status | Well Status Date | Comment |
|---|---|---|
| Oil and Gas | 1989-09-15 | Issued Date 9/15/89 Expired Date 9/15/90 Acres 0020000 Tool Type RTA Proposed Formation BASS ISLAND Proposed Depth 02879 Proposed Drill Depth 02879 |
| Original Spud | 1989-11-30 | |
| Completed | 1989-12-03 | |
| Reached Total Depth | 1989-12-03 | |
| CO | 1990-01-18 | 9 EDC GeoDate 9/15/89 |
| Completion Report Received | 1991-08-29 | |
| Change of Owner | 2008-07-21 | Operator changed from 9, POWER GAS MARKETING & TRANS to 1388, EXCO - NORTH COAST ENERGY INC |
| Change of Owner | 2009-12-14 | Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC |
| APP | 2014-04-02 | Proposed Formations:BASS ISLANDS, Issued Date:4/2/2014, Expired Date:4/1/2016 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class: |
| Plugged/Abandoned | 2015-12-16 | |
| Construction Permit Expires | 2016-04-01 | |
| Record Last Modified | 2017-02-15 |
For data sources see[2]
| Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
|---|---|---|---|
| 1997-06-29 | 2782 | 0 | |
| 2782 | 0 | ||
| 2782 | 0 |
For data sources see[3]
| Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
|---|---|---|---|---|---|---|
| 0 | 0 | 0 | NOT TREATED |
For data sources see[4]
| Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|
| -313072289 | 2019-4-30 0:00: | FR | No Violations | 0.50 |
| 0000PL4891 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
| 0603007891 | 2015-12-15 | Plug / Plug Back | No Violations | I was on location to witness the plugging of this well. The Bishop Service rig ran 1.5 diameter tubing to 2661 and Petroset pumped a 300 75sk Class A 2% gel cement plug and displaced it with 6bbls of fresh water to cover the Big Lime formation. Tubing was pulled to 997 and a 300 75sk Class A 2% gel cement plug was pumped and displaced with 2bbls of fresh water to cover the bottom of the surface casing. The well will be shut in overnight and the top of the wellbore will be grouted with 9sk grout tomorrow 12/16, completing the plug job. |
| 1849958273 | 2015-12-10 | Plug / Plug Back | No Violations | I was on location to check the status of prepping this well for plugging. Bishop Well service will be on location today to rig up and plug this plunger lift well. The 4.5 diameter production casing is set to 2793 with a packer. This well is an open hole completion and the 4.5 casing is not cemented in the wellbore. |
| 603007891 | 2015-12-15 0:00 | PB | No Violations | 5.00 |
| PL4891 | PL | No Violations |
For data sources see[9]