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34-153-20964

Well Details

Well ID: 34-153-20964
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Country: United States
State: Ohio
County: <County>
Municipality:
Operator Name: LANDMARK 4 LLC
Well Pad ID:
Farm/Lease Name: BOWERS UNIT
License Status: Producing
License Date: 1981-05-07
Spud Date: 1981-08-01
Spud Drilling Contractor:
Final Drill Date: 1981-08-07
Well Total Depth: 3910.00 ft
Configuration: Vertical
Latitude: 41.180000
Longitude: -81.520000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1981-05-07 140 KST OIL & GAS CO INC GeoDate 5/7/81
Original Spud 1981-08-01
Completed 1981-08-07
Reached Total Depth 1981-08-07
CO 1995-12-05 182 BELDEN & BLAKE CO GeoDate 5/7/81
Change of Owner 2001-05-24 Operator changed from 182, BELDEN & BLAKE CORPORATION to 5601, MOORE WELL SERVICES INC
Record Last Modified 2019-06-04

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 3710 3754 18
3710 3754 18
3710 3754 18

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 115000 Gal 0

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 KST OIL & GAS CO INC 6698.00 1046.00 365
1985 KST OIL & GAS CO INC 5585.00 920.00 365
1986 KST OIL & GAS CO INC 4255.00 390.00 365
1987 KST OIL & GAS CO INC 2827.00 526.00 365
1988 KST OIL & GAS CO INC 2495.00 246.00 365
1989 KST OIL & GAS CO INC 1803.00 344.00 365
1990 KST OIL & GAS CO INC 1633.00 257.00 365
1991 KST OIL & GAS CO INC 1344.00 198.00 365
1993 KST OIL & GAS CO INC 916.00 149.00 365
1994 KST OIL & GAS CO INC 860.00 149.00 365
1995 KST OIL & GAS CO INC 574.00 124.00 365
1996 BELDEN & BLAKE CORPORATION 936.00 195.00 209
1997 BELDEN & BLAKE CORPORATION 874.00 184.00 338
1998 BELDEN & BLAKE CORPORATION 858.00 129.00 197
1999 BELDEN & BLAKE CORPORATION 927.00 120.00 293
2000 BELDEN & BLAKE CORPORATION 309.00 0.00 266
2001 MOORE WELL SERVICES INC 0.00 38.00 222
2002 MOORE WELL SERVICES INC 878.00 118.00 351
2003 MOORE WELL SERVICES INC 1017.00 184.00 351
2004 MOORE WELL SERVICES INC 1252.00 147.00 365
2005 MOORE WELL SERVICES INC 1085.00 122.00 365
2006 MOORE WELL SERVICES INC 991.00 140.00 357
2007 MOORE WELL SERVICES INC 1003.00 134.00 359
2008 MOORE WELL SERVICES INC 903.00 179.00 365
2009 MOORE WELL SERVICES INC 1169.00 175.00 365
2010 MOORE WELL SERVICES INC 1275.00 168.00 365
2011 MOORE WELL SERVICES INC 1405.00 140.00 325
2012 MOORE WELL SERVICES INC 723.00 75.00 297
2013 MOORE WELL SERVICES INC 309.00 40.00 365
2014 MOORE WELL SERVICES INC 753.00 64.00 365
2015 MOORE WELL SERVICES INC 1224.00 70.00 365
2016 MOORE WELL SERVICES INC 567.00 0.00 365
2017 MOORE WELL SERVICES INC 665.00 0.00 365
2018 MOORE WELL SERVICES INC 385.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 KST OIL & GAS CO INC Brine 0 365
1985 KST OIL & GAS CO INC Brine 218 365
1986 KST OIL & GAS CO INC Brine 203 365
1987 KST OIL & GAS CO INC Brine 160 365
1988 KST OIL & GAS CO INC Brine 213 365
1989 KST OIL & GAS CO INC Brine 169 365
1990 KST OIL & GAS CO INC Brine 120 365
1991 KST OIL & GAS CO INC Brine 107 365
1993 KST OIL & GAS CO INC Brine 83 365
1994 KST OIL & GAS CO INC Brine 110 365
1995 KST OIL & GAS CO INC Brine 109 365
1996 BELDEN & BLAKE CORPORATION Brine 98 209
1997 BELDEN & BLAKE CORPORATION Brine 59 338
1998 BELDEN & BLAKE CORPORATION Brine 105 197
1999 BELDEN & BLAKE CORPORATION Brine 77 293
2000 BELDEN & BLAKE CORPORATION Brine 0 266
2001 MOORE WELL SERVICES INC Brine 34 222
2002 MOORE WELL SERVICES INC Brine 210 351
2003 MOORE WELL SERVICES INC Brine 188 351
2004 MOORE WELL SERVICES INC Brine 175 365
2005 MOORE WELL SERVICES INC Brine 203 365
2006 MOORE WELL SERVICES INC Brine 920 357
2007 MOORE WELL SERVICES INC Brine 2336 359
2008 MOORE WELL SERVICES INC Brine 1804 365
2009 MOORE WELL SERVICES INC Brine 1621 365
2010 MOORE WELL SERVICES INC Brine 1400 365
2011 MOORE WELL SERVICES INC Brine 1104 325
2012 MOORE WELL SERVICES INC Brine 664 297
2013 MOORE WELL SERVICES INC Brine 1121 365
2014 MOORE WELL SERVICES INC Brine 1208 365
2015 MOORE WELL SERVICES INC Brine 1030 365
2016 MOORE WELL SERVICES INC Brine 0 365
2017 MOORE WELL SERVICES INC Brine 5 365
2018 MOORE WELL SERVICES INC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0402517585 2006-09-14 Production Wells No Violations The Uniontown office received a call from Don Froelich (330-472-4319) with Dominion East Ohio reporting a natural gas leak in front of 3478 Haas Road in Northampton Township. The property owner is Joe Leighton (330-923-2346). Dominion has a line on the east side of Haas with residential service crossing under the road and continuing to the Leighton home. The nearest producing oil/gas well is Moore Well Services Bowers #1. Initial conversations with Jeff and Bob Moore indicated that their salesline from this well crossed Haas 200 north of the leak and that they had no lines in this area. However, they agreed to send a crew over in the morning, with a gas sniffer, to test the area. Dominion will also recheck the area to be sure that it is not their distribution or residential lines. No NOV will be issued pending further investigation.
0452962878 2006-09-15 Production Wells No Violations Met on site with employees from Moore Well Service to check for gas leaks along the west side of Haas Road. The gas sniffer indicated natural gas in a 15 section along the west side of Haas. Moore still maintained that their pipeline was well north of the leak. Later the same day, Jeff Moore called and reported that he walked their salesline and found that it was further south than either their maps or memory indicated. He will have a crew over later today to repair the leak. Due to their extra effort and prompt response, a NOV will not be issued to Moore.
1264885991 2006-09-21 Production Wells No Violations The area affected by the leak repair has been graded, seeded and mulched. No violations.
402517585 2006-9-14 0:00: PW No Violations
452962878 2006-9-15 0:00: PW No Violations

For data sources see[9]

References