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Well ID: 34-153-21295 | Loading map...
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Country: United States | |
State: Ohio | |
County: Summit | |
Municipality: Bath Township | |
Operator Name: WINDSOR ASSOCIATES INC | |
Well Pad ID: | |
Farm/Lease Name: GILBERT UNIT | |
License Status: Final Restoration | |
License Date: 2009-09-11 | |
Spud Date: 1982-12-16 | |
Spud Drilling Contractor: NAU DRLG | |
Final Drill Date: 1983-01-23 | |
Well Total Depth: 3677.00 ft | |
Configuration: Vertical | |
Latitude: 41.160000 | |
Longitude: -81.680000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1982-11-30 | Issued Date 11/30/82 Expired Date 5/29/83 Acres 0024876 Tool Type CT Proposed Formation CLINTON Proposed Depth 03677 Proposed Drill Depth 03677 |
Original Spud | 1982-12-10 | |
Completed | 1983-01-23 | |
Reached Total Depth | 1983-01-23 | |
CO | 1983-10-31 | 1422 WINDSOR ASSOCIATES INC GeoDate 11/30/82 |
Completion Report Received | 1983-11-03 | |
APP | 2009-09-11 | Proposed Formations:CLINTON, Issued Date:9/11/2009, Expired Date:9/11/2010 6:00:00 AM, Drilling unit acres:24.876, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2009-10-20 | |
Construction Permit Expires | 2010-09-11 | |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 3554 | 3600 | 0 |
3554 | 3600 | 0 | |
2006-09-11 | 3574 | 3595 | 13 |
3574 | 3595 | 13 | |
3554 | 3600 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 74000 | 50000 | FRAC;74MG H2O,50M# SD |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | WINDSOR ASSOCIATES INC | 1453.00 | 483.00 | 0 |
1985 | WINDSOR ASSOCIATES INC | 5492.00 | 667.00 | 362 |
1986 | WINDSOR ASSOCIATES INC | 3675.00 | 570.00 | 365 |
1987 | WINDSOR ASSOCIATES INC | 3100.00 | 450.00 | 365 |
1989 | WINDSOR ASSOCIATES INC | 2583.00 | 470.00 | 361 |
1990 | WINDSOR ASSOCIATES INC | 1650.00 | 283.00 | 365 |
1991 | WINDSOR ASSOCIATES INC | 288.00 | 360.00 | 150 |
1992 | WINDSOR ASSOCIATES INC | 2042.00 | 406.00 | 365 |
1993 | WINDSOR ASSOCIATES INC | 2305.00 | 196.00 | 362 |
1994 | WINDSOR ASSOCIATES INC | 2102.00 | 194.00 | 351 |
1995 | WINDSOR ASSOCIATES INC | 2088.00 | 201.00 | 348 |
1996 | WINDSOR ASSOCIATES INC | 1336.00 | 113.00 | 330 |
1997 | WINDSOR ASSOCIATES INC | 1406.00 | 0.00 | 360 |
1998 | WINDSOR ASSOCIATES INC | 1445.00 | 138.00 | 360 |
1999 | WINDSOR ASSOCIATES INC | 1266.00 | 169.00 | 350 |
2000 | WINDSOR ASSOCIATES INC | 1040.00 | 165.00 | 350 |
2001 | WINDSOR ASSOCIATES INC | 331.00 | 97.00 | 320 |
2002 | WINDSOR ASSOCIATES INC | 10.00 | 81.00 | 105 |
2003 | WINDSOR ASSOCIATES INC | 0.00 | 0.00 | 0 |
2004 | WINDSOR ASSOCIATES INC | 526.00 | 152.00 | 333 |
2005 | WINDSOR ASSOCIATES INC | 518.00 | 77.00 | 365 |
2006 | WINDSOR ASSOCIATES INC | 624.00 | 83.00 | 365 |
2007 | WINDSOR ASSOCIATES INC | 445.00 | 106.00 | 365 |
2008 | WINDSOR ASSOCIATES INC | 217.00 | 59.00 | 365 |
2009 | WINDSOR ASSOCIATES INC | 29.00 | 0.00 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0000PL4716 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
1251732426 | 2009-08-26 | Production Wells | No Violations | The Uniontown office received a call from Mrs. Dorothy Gilbert about an idle well on her property. The well in question is the Gilbert #1, PN-1295, owned by Windsor Associates and operated by Bass Energy. The last reported production was in 2008. The gear box has been removed from the pump jack rendering it unusable. I met with Ralph Gregory from Bass Energy to discuss the plans for this well. Gregory indicated that a plugging permit will be applied for and the well will be plugged and abandoned. |
1389967746 | 2014-01-14 | Final Restoration | No Violations | I insprcted this location on 1/14/2014. This well was plugged and abandoned on10/20/2009. Upon my inspection I found that all the criteria for Final Restoration were met. |
PL4716 | PL | No Violations |
For data sources see[9]